whirl jarge centrifugal cowpbessor

15
EXPERIMENTAL ON-STREAM ELIMINATION OF RESONANT WHIRL IN A JARGE CENTRIFUGAL COWPBESSOR G. I. Bhat and R. G. Eierman Exxon Chemical Company Baytown, Texas 77520 In October 1982, a severe resonant whirl condition was experienced when a multi- stage centr ifbgal compressor was first operated at higher than originally anticipated speeds and loads. Diagnosis of this condition was made easy by a large-scale computerized Machinery Condition Monitoring System ("MACMOS") . This computerized system was- immediateiy able to- verify t h a the predominant subsynchronous whirl frequency locked in on the first resonant frequency of the compressor rotor and did not vary with compressor speed. Compressor stability calculations showed the rotor system had excessive bearing stiffness as well as inadequate effective damping. An optimum bearing design was developed t o minimize the unbalance response and t o maximize the stability threshold. The above experience is not unusual and parallels that of many process plants using large centrifugal gas cmpression machinery. Of interest, however, is the approach taken by the plant to find a temporary remedy. The effective compressor bearing loading and effective clearance characteristics were modified with the machine continuing its process operation at normal load and speed. This approach involved the controlled application of heat to the compressor support legs while closely monitoring machine behavior. The experiment established the feasibility of extend- ing the onset of rotor instability in the event that plant operations would call for higher speeds before the optimized bearings became available. DISCUSSION OF PROBLEM UNIT Description of Unit The compressor is a two stage eight impeller horizontally split machine driven by a steam turbine. Oil seals are used at both ends and labyrinth seals are used at the center. The compresser runs at 175 psig inlet and 575 psig discharge. The r o t o r is supported by five shoe tilting pad load between pad bearings with 0.5 preload. The rotor has an unusually large ratio of bearing span to shaft diameter (99 in/5 in). The compressor train is safeguarded against high vibration with dual voting logic vibration trip circuits which shut the compressor down if vibration amplitude exceeds 4.5 mls at any time (Figure 1). A Kingsbury thrust bearing is used to absorb the thrust. The compressor is driven through a Bendix type diaphragm coupling incorporating a torque meter and 81

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Page 1: WHIRL JARGE CENTRIFUGAL COWPBESSOR

EXPERIMENTAL ON-STREAM ELIMINATION OF RESONANT

WHIRL IN A JARGE CENTRIFUGAL COWPBESSOR

G. I. Bhat and R. G. Eierman Exxon Chemical Company Baytown, Texas 77520

In October 1982, a severe resonant whirl condi t ion was experienced when a m u l t i - s t a g e centr i f b g a l compressor was f i r s t o p e r a t e d a t h i g h e r t h a n o r i g i n a l l y a n t i c i p a t e d s p e e d s and l o a d s . D i a g n o s i s o f t h i s c o n d i t i o n was made easy by a large-scale computerized Machinery Condition Monitoring System ("MACMOS") . This computerized s y s t e m was- immediateiy a b l e to- v e r i f y t h a t h e predominant subsynchronous whirl frequency locked i n on t h e f irst resonant frequency o f t he compressor r o t o r and d id no t v a r y with compressor speed.

Compressor s t a b i l i t y c a l c u l a t i o n s showed t h e r o t o r s y s t e m had excessive bearing s t i f f n e s s as well as inadequate e f f e c t i v e damping. An optimum bearing design was developed t o minimize the unbalance response and t o maximize t h e s t a b i l i t y threshold.

The above experience is not unusual and p a r a l l e l s t h a t o f many process p l a n t s using l a r g e c e n t r i f u g a l g a s cmpress ion machinery. O f i n t e r e s t , however, is t h e approach taken by t h e p l an t t o f ind a temporary remedy. The e f f e c t i v e compressor bearing loading and e f f e c t i v e clearance c h a r a c t e r i s t i c s were modified with t h e machine continuing its process operat ion a t normal load and speed. This approach involved t h e control led app l i ca t ion o f heat t o t h e compressor support l e g s while c lose ly monitoring machine behavior. The experiment e s t ab l i shed t h e f e a s i b i l i t y o f extend- ing t h e onset o f r o t o r i n s t a b i l i t y i n t h e event t h a t p l an t ope ra t ions would ca l l f o r higher speeds before t h e optimized bearings became avai lable .

DISCUSSION OF PROBLEM U N I T

Description of Unit

The compressor is a two s t a g e e i g h t impeller ho r i zon ta l ly s p l i t machine dr iven by a steam turb ine . O i l seals are used a t both ends and l abyr in th seals are used a t t h e center . The compresser runs a t 175 ps ig i n l e t and 575 ps ig discharge. The r o t o r is supported by f ive shoe t i l t i n g pad load between pad bearings with 0.5 preload. The r o t o r has an unusually l a r g e r a t i o o f bearing span t o s h a f t diameter (99 in/5 in ) . The compressor t r a i n is safeguarded aga ins t high v ib ra t ion with dua l voting l o g i c v ib ra t ion t r i p circuits which shu t t h e compressor down i f v ib ra t ion amplitude exceeds 4.5 m l s a t any time (Figure 1).

A Kingsbury t h r u s t bearing is used t o absorb t h e th rus t . The compressor is driven through a Bendix type diaphragm coupling incorporat ing a torque meter and

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h o t al ignment tubes. The compressor and the d r i v e r a re supported on a s o l i d concrete foundation.

P r o b l e m

P r i o r t o the f i r s t h a l f o f 1982 t h e compressor was running with s a t i s - f a c t o r y performance a t base capaci ty opera t ing cond i t ions o f 6000 rpn as the maximum speed (F igure 2). The r o t o r was subsequently mod i f ied f o r a d i f f e r e n t mole weight gas with a rev ised maximum speed o f 6500 rpm. The manufacturers' l a t e r a l c r i t i c a l speed and r o t o r s e n s i t i v i t y s tud ies d i d n o t r e v e a l any p o t e n t i a l problems (F igure 3 ) . The r o t o r was h i g h speed balanced a t 6700 rpm with an except ional balance q u a l i t y o f 2 oz-in. r e s i d u a l unbalance (F igure 4).

However, when an attempt was made t o increase the speed above 6000 rpm w i t h an increase i n load, a severe change i n s h a f t v i b r a t i o n was n o t i c e d (ampl i tude increase from l e s s than 1 m i l t o 3.6 mils) . Below 6000 rpm the compressor was running a t l e s s than 1 m i l v i b r a t i o n . Analysis o f v i b r a t i o n spect ra obtained from a computerized Machinery Condi t ion Moni tor ing System ( "MACMOS") revealed t h a t the h i g h v i b r a t i o n ampli tudes- o c c u r r e d a t a predzminant frequency o f 46.5 Hz (2760 cpm), which co inc ides w i t h t h e f i r s t resonant frequency ( c r i t i c a l speed) o f the compressor r o t o r (F igure 5). Varying the r a t e o f b u f f e r gas i n j e c t i o n t o the sea ls produced s i g n i f i c a n t changes i n the v i b r a t i o n ampl i tude suggesting t h a t t h i s so c a l l e d resonant wh i r l c o n d i t i o n was aerodynamical ly induced. Aerodynamic impulses created by gas e x i t i n g i m p e l l e r vanes ( l o a d dependent) p rov ide e x c i t a t i o n fo rce which, f o r systems wi th inadequate damping, can ampl i f y t h e v i b r a t i o n behavior a t t h e f i r s t c r i t i c a l speed o f the r o t o r . I t i s a l s o be l ieved t h a t the low r e s i d u a l unbalance i n th i s machine al lowed a f o r c i n g impulse o ther than unbalance t o pre- dominate and thus e x c i t e the f i r s t resonant mode o f the r o t o r .

A d e t a i l e d a n a l y s i s o f the rotor -bear ing system i n d i c a t e d excessive bear ing s t i f f n e s s as w e l l as inadequate e f f e c t i v e damping. A computerized study revealed t h a t a four pad load between pad bear ing i s an optimum design f o r the machine which would maximize t h e s t a b i l i t y th resho ld speed wh i le y i e l d i n g accepta- b l e unbalance response (Table 1).

However, s i n c e the new f o u r pad bear ings were n o t r e a d i l y ava i lab le , t h e approach taken by t h e p l a n t t o f i n d a temporary remedy with t h e machine cont inu ing i t s process opera t ion a t normal load and speed, i s innovat ive and worth sharing.

EXPERIMENTAL PROCEDURE

The goa l was t o e s t a b l i s h the f e a s i b i l i t y o f inc reas ing the r o t o r s t a b i - l i t y threshold, as p l a n t operat ions would r e q u i r e inc reas ing the r o t o r speed be fore t h e opt imized bear ings became ava i lab le .

It was a n t i c i p a t e d t h a t the goal cou ld be achieved b y modi fy ing e f f e c t i v e compressor bear ing load ing and e f f e c t i v e c learance c h a r a c t e r i s t i c s w i thout s h u t t i n g t h e compressor down.

For the purpose o f t h i s experiment, t h e four compressor support l e g s were provided with i n d u c t i o n heat ing elements which were wrapped with i n s u l a t i n g mater ia l . I n add i t ion , d i a l i n d i c a t o r s were s e t up t o moni tor v e r t i c a l and h o r i - z o n t a l movement o f the compressor casing. Power supply and temperature c o n t r o l

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r e s p o n s i b i l i t y were assigned t o the truck-mounted laboratory , which was pos i t ioned near t h e compressor p la t form.

Dur ing t h e t e s t r e l e v a n t process parameters were h e l d constant and were cont inuously monitored by MACMOS on a second-by-second bas is and then converted t o s ix-minute averages, The v i b r a t i o n behavior o f t h e machine was, o f course, a l s o logged by an automated computer and a FM tape recorder dur ing t h e e n t i r e tes t .

The a c t u a l t e s t was conducted by step-wise heat ing o f compressor l e g s i n t h e f o l l o w i n g sequence: (1) inboard l e g s only , (2) outboard l e g s only, (3) a l l four legs, and (4) two d iagona l ly opposi te l e g s a t a t ime. Temperatures s t a r t e d a t 150°F and were r a i s e d a t 50°F increments u n t i l f i n a l support l e g temperatures o f approximately 400'F were reached. The v i b r a t i o n ampl i tude behavior was c o n t i n u a l l y monitored on platform-mounted v i b r a t i o n moni tors and readings conf i rmed by simul- taneously observing t h e computer-generated log. The taped v i b r a t i o n s i g n a l s were subsequently analyzed and t h e i r spect ra p l o t t e d as shown i n Figure 6.

The onset o f h i g h v i b r a t i o n was noted on MACMOS p r i n t o u t s as t y p i c a l l y shown i n F igure 7, Whenever a p reset l i m i t i s exceeded f o r a g iven parameter, an alarm occurs and da ta logging i s i n i t i a t e d . Relevant da ta can then be r e t r i e v e d and examined.

F igure 7 shows excessive averaqe v i b r a t i o n o f the compressor outboard bear ing as monitored by an eddy c u r r e n t probe. A la rm- in i t ia ted da ta logg ing was a c t u a l l y t r i g g e r e d be fore 10:27:39 by v i b r a t i o n spikes which must have exceeded the preset l i m i t o f 3.2 m i l s . Note t h a t outboard eddy c u r r e n t probe readings are represented by the numberal 1t8tt whose second-by-second values a r e hand-connected f o r eas ier v iewing i n F igure 8 .

The experiment demonstrated t h a t low-v ib ra t ion opera t ion a t t r a i n speeds o f approximately 6,360 RPM was f e a s i b l e with compressor outboard support l e g s heated t o approximately 375°F. A t these condi t ions, t h e compressor outboard end had grown 32 m i l s i n the v e r t i c a l , and 4 m i l s i n the h o r i z o n t a l d i r e c t i o n . The subsynchronous (2,760 cpm) v i b r a t i o n component was smal ler than the once-per- r e v o l u t i o n component a t t h i s speed. This i s g r a p h i c a l l y i l l u s t r a t e d i n Figure 9, which shows compressor outboard spect ra obtained under s i m i l a r loads and speeds, wi th d i s s i m i l a r support l e g temperatures. A t ambient temperatures, t h e subsynchro- nous frequency r e g i s t e r s an uncomfortable 2.8 m i l s on the v e r t i c a l eddy c u r r e n t probe. When the compressor outboard l e g s were heated t o approximately 375'F, t h e once-per-revolut ion and subsynchronous v i b r a t i o n components dropped below 0.35 m i l s .

CONCLUSION

Severe a e r o d y n a m i c a l l y induced subsynchronous v i b r a t i o n prob lems developed when the normal opera t ing speed o f a l a r g e c e n t r i f u g a l compressor was increased. An experiment was c a r r i e d o u t t o extend t h e onset o f r o t o r i n s t a b i l i t y t o h igher speeds on- l ine, wi thout changing t h e bas ic r o t o r bear ing system charac- t e r i s t i c s . The t e s t r e s u l t s i n d i c a t e d t h a t the e f f e c t i v e compressor bear ing support c h a r a c t e r i s t i c s c o u l d be mod i f ied and t h e s t a b i l i t y th resho ld be increased t o an acceptable l e v e l .

This experiment has demonstrated t h a t with proper inst rumentat ion and monitor ing, i t i s f e a s i b l e t o extend t h e s t a b i l i t y th resho ld speed o f c e n t r i f u g a l compressor, w i thout r e q u i r i n g a shutdown o f the equipment.

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ACKNOWLEDGEMENT

5 SLBP L/D = .3/PLF = .5

5 Si8P L/D = .43/PLF = .O

5 SLBP (55 percent o f f s e t )

3 SLOP

5 SLBP

5 SLOP

4 SLBP

7 SLOP TRESS-32

7 SLOP TRESS-68

The authors acknowledge M r . H . P. Bloch, M r . H. G. E l l i o t t , Mr . D, G. Stroud, and Mr . R. H . Schmaus f o r t h e i r support dur ing t h i s t e s t and subsequent data reduction.

11.4

8.10

8.97

11.8

10.96

15.5

6.11

10.96

17.24

REFERENCES

"Four Pad T i l t i n g Pad Bearing Design and Appl icat ion for Mult is tage Ax ia l Compressors", J. C. Nicholas and R. G . Kirk, ASME Paper, 81-LUB-12, 1981.

"Select ion and Design o f T i l t i n g Pad and Fixed Lobe Journal Bearings f o r Optimum Turborotor Dynamics", J. C. Nicholas and R. G. K i rk , Proceedings o f the Eighth Turbomachinery Symposium, Texas A&M Univers i ty , ed, P. E. Jenkins, November, 1979.

"The In f luence o f T i l t i n g Pad Bearing Character is t ics on the S t a b i l i t y o f High Speed Rotor Bearing Systems:, J. C. Nicholas, E. J. Gunter, and L. E. Barnett, Topics i n F l u i d F i lm Bearing and Rotor Bearing System Desiqn and Optimization, an ASME spec ia l publ icat ion, 1978, pp. 55-78.

"Optimum Bearing and Support Damping for Unbalance Response and S t a b i l i t y of Rotat ing Machinery", L. E. Bar re t t , E . J. Gunter, P. E. A l l a i re , ASME Paper NO. 77-GT-27.

TABLE I. - SUMMARY OF POTENTIAL ALTERNATE BEARING PERFORMANCE

-.c c< tl) Bearing Case

1 0) COPT

0.24

0.45

0.40

0.69

0.70

0.63

1.12

0.86

0.59

AMPLZ.

-93.6)

22.0

53.7

15.1

25.7

24.6

8.7

12.6

31.5

-0.034

0.143

0.058

0.208

0.122

0.128

0.362

0.251

0.100

2,451

2,399

2,431

2,403

2,415

2,439

2,421

2,415

2,446

Ref: (1) "Optimun Bearing and Support Damping for Unbalance Response and S t a b i l i t y o f Rotat ing Machinery", L. E. Earret t , E. J. Gunter, P. E. A l l a i re , ASME Paper No. 77-GT-27.

" S t a b i l i t y and Damped C r i t i c a l Speeds o f a F l e x i b l e Rotor i n F lu id-F i lm Bearings",

(2) J. W. Lund, ASME Paper No. 73-DET-103.

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I *

Figure 1. - Compressor X-section.

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FREQUENCY (EMNTS44IN x lm0)

(a) Cascade plot- Figure 2. - Base operating conditions.

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CROBE 01 ID: CO?lPREfSOR<OTD VERT) ORIENTATION- 43.

CROBE 02 ID: CO?iPRESSOR(OTB MORT) ORIENTATION= 133.

UNFILTERED

nnx nnr- 0.49 nxLs PK-PK

mnx nnp- 0.62 nILs PK-PK

UT 1 ; : : : : i : : ' i . * ............................................................. .......... .......................

AHP SCALE- 0.10 ?IILS/DIV AHP SCALE= 9.19 ?lILS/DIV TIHE SCALE- 10.99 HSEC/DIV

ROTATION: CU RPfl<STRRT>= 4863 RPM<END)= 4857

PROBE 01 ID: COMPRESbOR(0TB VERT) ORIEMTATION= 4SO i x VECTOR- 0.87 nxLs PK-PK e-1160

?ROBE 02 ID: COf4PRESSOR(OtB MORZ) ORIENTATION= 1330

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(b ) O r b i t s .

Figure 2. - Concluded.

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Figure 3. - Critical speed map.

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Figure 4 . - High speed balance p lo t .

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f"

(a) Cascade plot.

Figure 5. - Uprated operating conditions.

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?ROBE 01 ID: COHPREtSOR(0Tl) VERT) ORIENl i l l IOM* 4s.

PROBE 02 ID: COHPRESCOR(0Tl) MORT) ORltNTIlTIOM* 1350

UWFILTERED

m x nnp= 6.60 n i L s PK-PK

mnx nip- 6 . ~ 0 niLs PK-PK

K

IIHP SCRLE= 6.18 HILS/DIV

ROTCITION: CY

IIHP SCRLEI 0.10 HILS/DIV T IHE SCRLE- S.60 HSEC/DIV RPn(STIIRl>* 6 0 2 4 RPtl<END)- 6025

?ROBE 01 ID: COlPRESSOR(0TB VERT) ORIENTRTION* 450 ix VECTOR= e.07 n u s PK-PK e-1480

?ROBE 02 ID: COHPRESSOR<OTB MORT) ORIENTRTION* 1350

1X FILTERED ix VECTOR. e.21 ~ I L S PK-PK 0-740

K

m P 8CIILEm 0.bS RXLWDIV ( I lP SCIILE. 6.W I I I L S / D I V T l l E SCRLE- S.6B HEEWDIV

aotniiom: cu R?l<STCIRT>* Cb24 R?)I(END>= 6026

(b) Orbits . Figure 5 . - Concluded.

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a. sx 1x ax

FREQLENCY (EKNlS/t i lN x 1000)

Figure 6. - Uprated operating conditions with heated legs: Cascade plot.

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