water shuoff techniques in air or gas drilling
TRANSCRIPT
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Water shutoff Techniques in Air or Gas Drilling t
C H R L E S
K
SUFALL
ABSTRACT
Water-shutoff
techniques
have reached a point where
they ar e generally accepted f or field us age ~f economlc
galn can be reallzed The success, both econonl~cal
and t ha t of shu ttl ng off permeable zones, 1s a tr lbute to
the plannlng of a job and the fine work done by the
research and servlce organlzatlons. Several types of
shutoff nlaterlal are now readily available through the
servlce companies as a re th e tools and techniques needed
to complete a water-shutoff job.
INTRODUCTION
Alr and g as drllling is economically 11mlted In use to
areas where format~onwaters do not present too great
a problem. Aerated mud and the use of surfactants to
mist drlll have helped where competent fonnatlons are
penetrated
1
However, almost all economlc failures In
alr or gas drllling are caused by for mat ~onwaters.
A fa st , lnexpenslve method of shu ttl ng off wa ter has
been a major objective for many research or ga n~ za t~ on s.
This report is Intended a s a revlew of the mat erials
and niechanlcs now
111
use for the purpose of shuttl ng
off format~onwaters.
HISTORY
The f irs t t ~ m e water-bear~ng ormation was pene-
trated with ai r or gas a s a drllling flu~d , he idea of
water shutoff arose. The old standby, cement, was first
used in the early attempts to plug the water zone. A
few jobs were successful; however, the cost Involved In
waltin g time made thls approach unacceptable
Gels and
emulsions
that had been used In selective
complet~onwork were tried with no degree of success.
Another approach was to form a sheath in a n enlarged
well bore where low-pressure zones were encountered.
Thls
technique
used hlgh-velocity air to erode the hole
through the water-bearing section. A length of
plastic
plpe w ~ t h up-type packers spaced to cover the interval
to be treated would be filled with an epoxy resin and
spotted op pos ~te he zone see Flg.
1
The resin was
then displaced Into the enlarged hole and chemically
tlmed to set
according
to the temperature. Therefore,
no appreciable w a ~ t l n g ~ n ~ eas required The resln
Techn~cal Dr ~l l~ ngervrce, Inc M~dla nd,Texas
;Presented at the sprlng meetlng of the Rocky Mountaln D ~ s t r ~ c t
D ~ v ~ s ~ o nf Product~on.Casper. y o Ap r~l
960
References are a t the end of th e paper
expanded while setting to as much as five tllnes ~ t sng-
lnal volume. After the resin had set up, the drlll pipe
was rotated to break a neck on the plastlc plpe. A blt
was then run to drill a hole through the plastlc plpe and
resln, thus leavlng an impermeable sheath to exclude
the water.
T h ~ sechn~qu e howed some success, but was hm ~t ed
to low-pressure format ~ons.As research capaclty was
hmited,
attention
was dlrected to ot her shutoff methods.
Research a t thls polnt was dlrected toward a lnaterlal
tha t could be squeezed Into the fo nn at ~o n t relatively
low pressures.
Thls material would need a very low
v~scosityu n t ~ l t was squeezed i nto place. Thus placed
Into the formation ~t would set up elther on contact
w ~ t h he water or through the chem~c al lmer.
s B r e o k off Ne ck
by
R o l o t ~ n g P
Plost~cP ~ p e
Fig
1
Resin Displaced into the Eroded Well Bore
with a Culculated Hydrostatic Head of Water
and Allowed to Set
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After the inater ia l has se t up w ~ t h ~ nhe water zone
tt will be subjected to co ns~de rabl e ~ffe rent ial ressures
once t he hole
IS
unloaded and relleved of its hydrostat~c
head. Therefore, a prime character~st~cor the set-up
nlater~alwould be e~ t h er reat strength or deep pene-
t r a t ~ o nnto the permeable zone.
Also, the material must not be affected by contaml-
nants The method of mixture and ~nject~onhould be
ea s~ ly ccompllshed on locatlo~lw ~ t h hm~ter l mount
of special equ~pment.The se t t ~ng e r~odmust be easily
regulated to prevent pres ett ~ng r t o a vo ~d ostly wait-
lng t ime. F~nal ly , he ~n at er ~a lould need to be safe
enough to be handled on locat~onw ~ t h ormal safety
precaut~ons.
Two products were ~nt rodu ced o the field wh ~c h on-
t a ~ n e dmost of the foregoing
characteristics.
One was
a wa ter gel th at i s pumped in a 11qu1d form The gel
sets with the use of a chenlical t ~ n ~ e rnd w ~ t hempera-
ture. Dilution w ~ t h ater tends to accelerate ~ t setting
t ~ m e he other product
IS
a pl as t~ c h~ ch s also sensl-
tlve to water. Both
of these products have had wide
u sa ge w ~ t home remarka ble successes
A d~f fer ent pproach was the use of a liqutd and gas.
The.liqu~dwas fi rst ~ntroduced n t ohe permeable zone
and was followed by the g as \vl ~~cl ieactecl to form an
insoluble precipitate. Thus, with the perlneab~ll ty ealed
off, water shutoff had been acconlpl~shed
The use of g as alone as a shutoff n le d~ u~ nas devel-
oped after the successful acco~npl~shmentf the l ~ q u ~ d
and gas. The gas In t h ~ s ase 1s s~licotl etrafluor~de
which reacts with wate r In the form at ~o n o form a gel
and thereby seals off the permeabil~ ty T h ~ s airly
recent technique has seen w~ d e sage w ~ t h coils~der-
able degree of s~ c c e s s . ~ , ~
The most recent approach to water shutoff is a l~quld
which combines w ~ t h ater to form a gel
T h ~ s a t er ~ al
has just been released to the field and ~ t sharacter~stics
are not ava~lable.However.
~t
s known that the ~nitial
field trials of the liqu~d ave been highly successful
ECONOMICS
The pr~maryconsideration for in~tiattnga water-
shutoff procedure s economics R I ~~ m e s generally
the lar gest cost factor Therefore, by the use of advanced
planning much trine can be saved If geological data
~ n d ~ c a t epotentla1 a qu ~f er s to be penetrated and the
a v a ~ l a b ~ l ~ t yf m at er~ als nd tools needed fo r a water
shutoff ar e known In advance, the clownt~tne ol the rtg
may be cut to 24 hours or less
depending
upon well
depth.
The cost of water-shutoff in at er ~a lwould depend upon
the zone ~tse lf. n other words, the zone detern i~ne s he
amount of shutoff m at er ~a l eeded
Other costs would include a pump truck, a n~trogen
truc k, a plughead an d pump-down plug, diesel or alcohol
a s a s w e e p ~n g ~ a t e r ~ a l , packer, and a h~gh-pressure
compressor. I t should be noted, however, th at on mos t
jobs only a portion of this equipment would be neces-
sary. Generally, th e total cost, ~nc ludl ng lg time, would
rang e from 2,000 to 6,000 de pe nd ~n g pon depth and
formation character~st~cs.
Several cons~derationscan eliminate lost time. The
id en t~ ty f t he wa ter zone can be cl~fficult.The top can
usually be p~ck ed y nottng the depth penetrated when
the well stops du st ~n gThe lower portion of t he perme-
able zone can be picked by the use of geological info r-
ma t~ on nd the change In dri ll ~ng ates In some cases
a s ~n al l one may n ot be noticed while drilling a t fas t
rates and will show up after a trip or when the drilling
rate decreases So n~ et ~m eslog may be needed to define
the permeable zone.
Some hole should be made below the water zone to
act as a reservoir for wet cuttings and sloughing mate-
r ~ a lo accumulate. The hole should be cleaned as much
as poss~ble r io r to pu l l~ng he b ~ t
h ~ s ay be best
accompllshed by a dd ~n g foaming agent to wate r and
~nje ctln g nto the alr stream The hole clea ~nn g lso
allows the formation to ~~r odu cet sluid which a t t~ m e s
may draw down the zone's pressure, and thus allow the
shutoff nlaterial to enter the zone at a lower pressure
The packer se at should be p~c ked n a co~ilpetent one
as near a s poss~ble o the permeable s ect~ on
The job should be planned so as to use a mlnlmum
amount of fl u~dLo ad ~n g he hole can charge up a zone
above the packer that would bleed back into the well
bore dur ~ng ry~ng-up pe ra t~ons T h ~ s ould result in
l o s t t ~ men d r y ~ n g p the hole, and could also glve a
false evaluat~onof the shutoff Several shutoffs have
been aceompl~sheduslng only d~esel s a sweep ~ng lu~d
and air, gas, or nitrogen as the flush No other flu ~dwas
used. An inflatable-type fortnat~onpacker 1s used to
w~ths tand he h ~ g h ~ f fe ren t~a lressures
All poss~ble recautions should be taken to allow the
squeeze mat er~ al o enter the for mat~ ons t as low a
v ~ s c o s ~ t ys poss~ble A swee p~ngmaterial should be
used ahead of all wate r-se ns~t ive hem~ cals
Straddle packers may be con s~dered n some cases
Each job w ~ l l epend upon tools, mat er ~a ls , nd hole
cond ~tio ns o be designed fo r speed and effic~entopera-
t ~ o n
CASE HISTORIES
The follow~ngcase htstones a re representatwe of
some of th e d~ ff er en t roblenls encountered These jobs
all used the s111con tetr aflu onde ga s However, the tech-
nique used In a water-shutoff op er at ~o n s In general the
same for other water-shutoff agents.
Well A-Peeos County. Texas
In t h ~ s ell ( see
ig
2) , 9.56-111. cast ng was se t a t
6.088 f t Gas drt ll ~ngwas used unt~la fishing job
occurred and was unsuccessful A wlnclow wa s cut In
the ca s~ ng t ap prox ~mat ely ,600 f t and the old hole
was s~detracked nd dr ~lled o about 5,900 f t w ~ t h ud
The hole was the n unloaded and ga s-d r~l led o 5,970 ft
where approximately 5 bbl of water per hour were
encountered. The hole was then blown and ~mst-dr~lled
to 6,466 f t in an att empt to dr y up the zone As the
wate r ~n fl us ersisted, a water-shutoff was planned
The well was cleaned with a f oa ln ~n g gent and wa ter
p rior to pul llng the b ~ t
traddle packers of the inflat-
able type were then placed a t 5,950 f t and 6,088 f t to
include any possible water zone. Then 6 gal of diesel
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Fig. 2 - A Straddle-packer Squeeze Job
After squeeze, gas drilling continued to below
12 000 ft without a water problem.)
were pumped into the drill pipe to be used as a sweep-
ing agent and to inflate the packers, after which 252
Ib of silicon tetrafluoride were injected as a shutoff
material. This amount was less than 2 lb per f t of hole
exposed; however, the water zone was only a few feet
thick.
Natura l ga s was used to bring th e pressure up to 725
psi maximum line pressure. A pump-down was released
and followed with a 4-bbl diesel blanket which, in turn,
was followed by water. When the drill pipe contained
18
bbl of water, the bottom-hole pressure approached
1,500 psi. A s th e annulus wa s unloaded t he packers were
set with this differential pressure.
Wa te r mjection continued until the bottom-hole pres-
sure of 3,540 psi was reached and maintained. During
this period the formation apparently took the diesel a t
3 180
psi bottom-hole pressure and
a
slight pressure
dro p occurred when th e silicon tetrafl uoride wa s injected.
The pressure then increased rather rapidly, indicating
the plugging action taking place in the permeable zone.
After the zone was apparently shut off, the drill-pipe
pressure was released, unloading almost all the water,
and the packers were unseated and pulled. A bit was
run back in and the hole was cleaned with a foaming
agent. Some silicon tetrafluoride was noticed, indicating
the zone had plugged before all the gas had been
displaced.
The hole was dry-drilled with ga s for over two weeks
without any fur th er indication of water.
In this particular area the formation that was gas-
drilled is principally a shale that is water-sensitive.
Therefore, mis t drilling with chemicals presently avail-
able is almos t impossible. More tha n 50 day s were saved
by the continued use of gas drilling.
This job used the bottom-hole pressure to determine
when the plugging action was complete. The pressure
gradient of 0.74
psi per f t of depth will generally frac-
ture formations with fluid. However, gas has been
found to fractur e a t considerably lower pressures. Fo r
this particular well a gradient of 0.6 psi per f t of depth
was used; and when the formation supported the 3,540
psi bottom-hole pressure the job was complete.
Well B-Logan County, Ark ans as
This well had 10 -in. casing set a t 733 ft. A 9 -in.
hole was drilled out with air, and water was hit about
1,520 ft. Another 29 f t were drilled, using a foa ming
agent and water injected a t a constant rat e into the a ir
line. Then when all geological data indicated that the
permeable zones had been penetrated, a water shutoff
with silicon tetrafluoride was planned to stop t he 4 bbl
of water influx.
The hole was cleaned with a foaming agent and an
inflatable packer wa s run t o 1,503 f t and set with wate r
pressure. The packer was then opened
t
circulating
position and the hole was unloaded.
The packer was opened below and 155 gal of diesel
were injected, followed by
320
lb of silicon tetrafluoride.
Nitrogen w as used t o complete the squeeze with a maxi-
mum bottom-hole pressure of 975 psi. Upon unloading
the hole after the packer w as pulled a small amount of
water was still being produced by the permeable zone
and, therefore, the use of mist drilling was necessary.
The job wa s classed a s a pa rtial wate r shutoff. However,
logs run on the completion of the well indicated a zone
of pe rmeabi lity a t 1,549 f t which could have accounted
for the small influx of water.
Well C--Haskell County, Oklahoma
This well was making about 2 bbl of water an hour
from two zones in the Hartsharn sand. The 9-in. hole
was drilled with gas as a circulating medium and pene-
tration rates were fast enough
t
generate sufficient
dust to keep the hole dehydrated. However, slow drill-
ing below 3,500 f t allowed the moisture to form mud
rings that eventually formed a severe annular restric-
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tlon. Logs Indicated that the permeable zones were
between 960 f t and 1,050 f t and between 1,160 f t and
1,250 ft.
Slhcon tetrafluoride mas used to shut off both zones.
Inflatable-type straddle packers were set a t 1,145 f t and
1,273 f t to trea t th e lower zone. Afte r th e packers were
111 pos~tlon, 40 gal of dlesel and 400 lb of slllcon tetra-
fluoride were used. Natural gas was used to set the
packers, and was also used a s a flush A bottom-hole
pressure of 630 psi wa s used to sh ut off t he lower zone.
The packers were then released and pulled up to treat
the upper zone.
Natural ga s was used to set the packers a t 953 ft and
1,081 ft Then 340 gal of dlesel and 200 lb of slllcon
tetrafluorlde were injected, followed by natural gas for
a flushlng agent. The inaxlnluin bottom-hole pressure
used for the upper zone was 525 psl.
Subsequent logs indicated t ha t a considerable zone of
permeability
exlsted a t a d epth of 3,500 ft . Thls zone
had not been anticipated and was, therefore, not con-
sldered for wa ter shutoff This zone a t 3,500 f t was prob-
ably producing most of the water.
Well E--Andrews County. Tex as
.
The format1011 frac ture d d uri ng th e squeeze of thi s
job and st111 a high percentage of wat er shutoff w as
attained
The 8%-in. hole was air-drllled f rom t he casing point
a t 4,100 f t to 4,364 f t, where damp cutti ngs were noted.
At 4,912 f t th e voluine 0 water enterlng the hole
approached 60 bbl per hour. At this point the hole was
cleaned and an inflatable packer was iun and set at
4,514 f t, th en 300 gal of dlesel wei e used a s a sweeplng
age nt The silicon tetrafluorlde was diluted with nitro-
gen In consideration of the long sect~onof hole to be
squeezed. A nltrogen buffer followed the silicon tetra-
fluorlde and the buffer was, in turn, followed by air
pressure Nitrogen was again used to the maximum
pres sure limlts of the equipme nt and th e pump-down
plug was released. Water was used to complete the
treatment
At slightly over 2,500 psi bottom-hole pressure, a
pressure drop of 500 psi was noted. This pressure drop
probably Indicates the breaking down of the formation.
Aft er t h ~ she maxiinurn bottom-hole pressure attained
wlth further displacement was 2,135 psl
The packers were pulled and the hole unloaded The
water production was now measured a t 6 bbl per hour
T h ~ s as a pleasant surpnse,
considering
a fractured
formation.
Well D-Alberta Canada
Large-diameter holes can present an unusual problem
of gre at forces with small dlfferentlal pressures. In t his
well, 13%-in casi ng was set a t 3,720 ft. A 12%-ln. hole
was drilled out to 3,808 f t with a small influx of wa ter
apparently entering the hole a t or near the casing shoe
Thls meant that the ~a c k e r eat would have to be lnslde
the caslng. As an inflatable packer was the only type
rea d~l y vailable,
lt
was seated In the float collar to
att aln a s much frictlon a s posslble The hole had been
cleaned
Nitrogen was used as a sweeping fluid and as a buffer
behind the silicon tetrafluorlde Air pre ssur e was used
as a squeezing medium Annulus pressure was inain-
tained to keep the dlfferentlal pressure a cross the packer
froin becoming too great. Water and air pressure were
used for this.
A bottom-hole pressure of 2,315 psi was attained and
the shutoff was colnpleted without any d~fficulty.
I t IS interesting to note that a force of a quarter of
a m~lllon ounds was acting beneath the packer.
These case his tone s ar e Intended t o illustr ate some of
the different problems and hole conditions that arise
They are not meant a s any stand ard, for each job should
be planned according to the hole conditions and tools
and materials
avallable
CONCLUSIONS
Water-shutoff techniques have advanced froin ,a tn al -
and-error method to an accepted procedure for alr and
ga s drilllng Varlous research organizations and service
companies hav e contributed greatly to modern nlaterlals
and techniques and are now strlving towards a inore
efficient method of water shutoff. Although water-shut-
off methods ar e st111 in the p rinl ary stag es, several
iinportant factors can now be concluded.
The less fractured or open the perineabillty, the bet-
te r th e chance fo r complete wate r shutoff. Therefore, a
stronger type of shutoff material 1s still needed.
Squeeze pressures must be maintained a s low a s pos-
sible to avold fracturing the water-bearing forn~atioli
Inltlal results of wat er shutoff ~nd lca te hat better
shutoffs are attained from
materials
that gel or set after
enterlng the permeable sectlon.
Flnally, and most important, the economics of shut-
tlng off water zones can be held to a surprising mini-
inuin by plannlng ahead This involves a st udy of t he
characteristics of t he fo rm at ~o n o be penetrated, a
knowledge of the tools and
materials
avallable, and
being ready to cope with the s~tuationwhen t arises.
The major cost of a water-shutoff treatment
IS
directly
related to the t i ine consumed, and planning is the
remedy.
REFERENCES
IRandall, B V; Lunlmus,
J
L; and Vincent, R
Combatting Wet Formation While Drllling wlth Alr or
Gas, D?-il l~n{/ ont,rnctor, Oct. (1958).
ZHower, Wayne F , McLaughlln, Charles, Ramos, Joe;
and Land, John: Water Can Be Controlled In Alr or Gas
Drllling, IVorltl 0~1 ~ n parts) Par t
I;
Feb. (1959),
P ar t 11, March (1959).
sGoodwin, Robert J and Teplitz, A. J : A Water-
shutoff Method for Sand-type Porosity in Air Drilling,
T,rcrlls Ant I ns t. i l f ~ ) ~ z n ge t. E T L Q ~ S .Petroleltm Devel-
op)~lemt
ind
T e c h n o lo q y ) .
2 1 6 , G3 Oct (1958).
4Sufal1, C. I . and McGhee, Ed: Water-shutoff Treat-
ments for Air and Gas Drlllii~g,011 Gus
J.
57 [5 1 Dec.
7 (1959)
sBecker, Frederick L and Goodwln, Robert
J:
Private
colnnlunlcation.
Wrabb, H. H. Pnvate communication.