improved vacuum pan performance using jigger … · improved vacuum pan performance using jigger...
TRANSCRIPT
Presentation to SIMTEC 2008
Improved Vacuum Pan performanceusing Jigger Tubes
by Professor Ross BroadfootQueensland University of Technology
Supported by:
BIG Tecnologia www.bigtecnologia.com.brActionLaser www.actionlaser.com.au
The use of a novel jigger system to improve vacuum pan performance
ByR. Broadfoot,
D.W. Rackemann andS. Morris
Queensland University of Technology, AustraliaActionLaser Pty Ltd,
Australia
Introduction
• Jigger system uses incondensiblegases/vapour injected into base of pan under the calandria to improve circulation and heat transfer
• Designed to uniformly distribute injected gases through very fine perforations. Install jigger tubes as- Ring for batch pans- Axial pipe/s for horizontal continuous pans
SRI jigger tubes• Laser drilled stainless steel tube• Holes of 0.2 mm diameter at intensity of
100,000 holes per metre
Effect of noxious gas jigger on circulation
Jigger system design
• Simple installation
• Controlled by manual valves and set to achieve required pressure differential (typically 15 to 20 kPa)
NOXIOUS GAS / STEAM LINE
JIGGER RING INLET/S
CALANDRIA
MAX. BOILING LEVEL
SOCKET FOR PRESSURE MEASUREMENT
VALVE FOR CONTROLLING NOXIOUS GAS FLOW
VALVE FOR EACH INLET
TO CONDENSER / ATMOSPHERE
Factory applications, testing and experience
• First installation in continuous C pan at Tully Mill, Australia in 2003 season
• Comprehensive testing in 2004 and 2005 seasons- 200 t batch A massecuite pan (Kalamia)- Continuous A massecuite pan (Tully)
• Installed in 6 batch pans and 7 continuous pans for the 2007 season
Continuous pan installation
SRI jigger pipe
Bottom of calandria tube plate
Previous HP steam jigger system
Results – 200 t batch pan
• Improvements in average circulation rates (up to 20%)
• Reduction in calandria pressure of20 – 40 kPa
• Improvements in HTC’s (5 to 30%)• Reduced average steam flows• Shorter cycle times
Results – 200 t batch panCirculation velocity
0
0.1
0.2
0.3
0.4
0.5
90 120 150 180 210
Operating quantity in pan, t
Circ
ulat
ion
velo
city
, m/s
40
45
50
55
60
65
Res
ista
nce
Run 1 - Velocity (Jigger on)Run A - Velocity (Jigger off)Run 1 - Resistance (Jigger on)Run A - Resistance (Jigger off)
Heavy up period
Results – 200 t batch panSteam flow rate and calandria pressure
0
5
10
15
20
25
90 110 130 150 170 190 210
Operating quantity in pan, t
Stea
m fl
ow ra
te, t
/h
0
20
40
60
80
100
120
Cal
andr
ia p
ress
ure,
kPa
Run A (Jigger off) steam rateRun 1 (Jigger on) steam rateRun A (Jigger off) calandria pressureRun 1 (Jigger on) calandria pressure
Heavy up period
Results – 200 t batch panHeat transfer coefficient
0
100
200
300
400
500
90 120 150 180 210
Operating quantity in pan, t
Hea
t tra
nsfe
r coe
ffici
ent,
W/m
2 /K
Run A (Jigger off)
Run B (Jigger off)
Run 1 (Jigger on)
Run 2 (Jigger on)
Heavy up period
Results – Continuous A pan
• Improvements in circulation (up to 15% increase in measured velocity)
• Quantity of slow moving massecuite on the pan base reduced
• Slight reduction in calandria pressure
Feedback on improvements to batch pan performance
v B pan operates on 12 minute shorter cycle time→ benefit to other pans in the schedule
v Eliminate use of defoamer in magma pan
v Reduced calandria pressure, allowing higher steam rates at high massecuite levels
v Much improved circulation at pan full, better control and heavy up
v Eliminated problems of jigger steam pipes becoming blocked
with massecuite
Feedback on improvements to continuous pan performance
v Higher dropping brix (increase by 0.6 unit for a C pan); plus more consistent brix
v Increased circulation → tighter control on conductivity
v Longer operating time between cleans (High grade seed pan previously cleaned every 10 days now cleaned after 14 days)
v Tubes and base of pans are faster to clean during a boilout (less sugar to remove)
v More rapid restart after stopping pans with massecuite at the operating level (e.g.during factory breakdown)
Check on operation of the jigger tube after 15,000 hours
Air test into jigger in Tully C pan after operation for 15000 hours (during 4.5 seasons).
Pressure drop 20 kPa
Check on operation of the jigger tube after 15,000 hours
Air test into jigger in Tully C pan after operation for 15000 hours (during 4.5 seasons).
Pressure drop 50 kPa
Other features of the new system
• Low installation cost (installed by mill tradesmen)• Minimal operator intervention• No special cleaning requirements• Pipes do not block with massecuite• Non return valves not needed• No additional gas load on the condenser or vacuum
pump
Able to retrofit to batch or continuous pans
New installations for the 2008 season
v Batch and continuous pans
v Four pans in Australia
v Pans in Argentina, India and South Africa
Acknowledgements
• Tully Mill staff • Kalamia Mill staff • Queensland Sustainable Energy
Innovation Fund• Board of Sugar Research Institute,
Australia. SRI owns the intellectual property for the jigger tube system.