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NASA Technical Memorandum 85900 'NASA-TM-85900 19840021810 Effect of Control Logic Modifications on Airstart Performance of F100 Engine Model Derivative Engines in an F-15 Airplane David B. Crawford and Frank W. Burcham, Jr. , August 1984 l .. NI\S/\ National Aeronautics and Space Administration II DRARY COpy {\i IG 2 8 1984 LANGLEY RESEARCH CENTER LIBRARY, NASA HAMPTON, VIRGINIA https://ntrs.nasa.gov/search.jsp?R=19840021810 2020-04-14T09:18:48+00:00Z

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Page 1: Effect of Control Logic Modifications on Airstart Performance of … · 2013-08-31 · NASA Technical Memorandum 85900 Effect of Control Logic Modifications on Airstart Performance

NASA Technical Memorandum 85900 'NASA-TM-85900 19840021810

Effect of Control Logic Modificationson Airstart Performance of F100 EngineModel Derivative Engines in anF-15 Airplane

David B. Crawford and Frank W. Burcham, Jr.

, August 1984

l~..

NI\S/\National Aeronautics andSpace Administration

II DRARY COpy{\i IG 2 8 1984

LANGLEY RESEARCH CENTERLIBRARY, NASA

HAMPTON, VIRGINIA

https://ntrs.nasa.gov/search.jsp?R=19840021810 2020-04-14T09:18:48+00:00Z

Page 2: Effect of Control Logic Modifications on Airstart Performance of … · 2013-08-31 · NASA Technical Memorandum 85900 Effect of Control Logic Modifications on Airstart Performance
Page 3: Effect of Control Logic Modifications on Airstart Performance of … · 2013-08-31 · NASA Technical Memorandum 85900 Effect of Control Logic Modifications on Airstart Performance

NASA Technical Memorandum 85900

Effect of Control Logic Modificationson Airstart Performance of F100 EngineModel Derivative Engines in anF-15 AirplaneDavid B. Crawford and Frank W. Burcham, Jr.Ames Research Center, Dryden Flight Research Facility, Edwards, California 93523

1984

NI\S/\National Aeronautics andSpace AdministrationA'mes Research CenterDryden Flight Research FacilityEdwards, California 93523

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Page 5: Effect of Control Logic Modifications on Airstart Performance of … · 2013-08-31 · NASA Technical Memorandum 85900 Effect of Control Logic Modifications on Airstart Performance

INTRODUCTION

The ability to achieve rapid and reliable airstarts is crucial to the safeoperation of modern Jet aircraft. The NASA Ames Research Center's Dryden FlightResearch Facility is currently testing prototype Pratt and Whitney FlOO Engine ModelDerivative (EMD) engines in an F-15 aircraft. The FlOO EMD has a thrust increase ofapproximately 15 percent over the standard FlOO engine. It incorporates a redes­igned fan, improved materials in the hot section, and a redesigned augmentor fueldistribution system. The FlOO EMD also incorporates the digital electronic enginecontrol (DEEC) system. The DEEC, described in ref. 1, incorporates closed loopairstart logic which was evaluated on a standard FlOO engine (ref. 2), and resultedin a significant improvement in airstart envelope. For the first flight tests_ ofthe FlOO EMD in March-June, 1983, similar airstart logic was used and similarairstart results were obtained (ref. 3). In the FlOO EMD flight evaluation flown inJuly-September, 1983, modifications to the airstart logic were evaluated. Thisreport describes the FlOO EMD engine, the DEEC, the modifications to the airstartlogic, and the airstart results before and after the logic modifications.

NOMENCLATURE

CIVV

DEEC

EMD

FTIT

HP

JFS

M

Nl

N2

PB

PLA

PS2

PT6M

compressor inlet variable vanes

digital electronic engine control

engine model derivative

fan turbine inlet temperature, °c

pressure altitude, m

jet fuel starter

Mach number

engine fan speed, rpm

engine core speed, percent (100 percent is 14,000 rpm)

main burner pressure, N/cm2

power lever angle, deg.

engine inlet static pressure, N/cm2

2mixed turbine discharge pressure, N/cm

------_. -~---------~----

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RCVV

SEC

T

TT2

t

WF

WF/PB

rear compressor variable vanes

secondary engine control

airstart time, time from pressurization to idle N2, sec

engine inlet temperature

time, sec

engine fuel flow, kg/hr

fuel flow-burner pressure ratio

DESCRIPTION OF APPARATUS

The F-15 aircraft (fig. 1) is a single seat, high performance, all weather airsuperiority fighter capable of Mach 2.5. It is a twin engine airplane with a high­mounted sweptback wing, twin vertical stabilizers, and large horizontal stabilizers.The F-15 has been modified to be a general test bed aircraft. During the firstphase of the flight test program, an F100 EMD engine was installed in the left sideof the F-15. During the second phase, the EMD engine used in Phase I was installedin the right side, and another F100 EMD was installed in the left side.

The F100 EMD engine (figs. 2 & 3) is a twin spool, low bypass ratio, augmentedturbofan. It has a three stage fan driven by a two stage low pressure turbine. Thefan has five percent greater airflow capability and seven percent more pressure risethan the standard F100 fan. The ten-stage high pressure COmpressor is driven by atwo-stage high pressure turbine. The turbines incorporate single crystal blades andvanes, allowing a higher operating temperature than the standard F100 engine.Compressor bleed is used only during starting. The variable camber inlet guidevanes and rear compressor variable vanes allow for higher performance over theoperating envelope. Variable augmented thrust is provided by a mixed flow, sixteen­segment afterburner. The mixed flow is exhausted through a variable areaconvergent-divergent nozzle. During Phase I, F100 EMD engine serial number P680350was used, and for Phase II, F100 EMD engine serial number P680585 was added. Bothengines are pre-production test models. Airstarts were conducted with both P680350and P680585.

An important feature of the EMD engines is the DEEC unit. The DEEC is afull-authority digital electronic control system with a simple integral hydro­mechanical secondary engine control. TheDEEC replaces the functions of thesupervisory electronic engine control and the hydromechanical unified fuel controlon the F100 engine. The DEEC system, shown in figure 4, receives inputs from:a) the airframe through throttle position (PLA) and Mach number (M); b) the enginethrough pressure sensors PB, P6TM, PS2, temperature sensors TT2 and FTIT, and rotorspeed sensors Nl and N2; and c) the control system through feedback resolvers thatindicate variable vane (RCVV, CIVV) positions, metering valve positions (fuel flowfor primary and augmented thrust modes), and exhaust nozzle positions. This infor­mation is used by the DEEC controllor to a) schedule the compressor bleeds andposition the variable vanes through actuators in open-loop system; b) control the

2

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primary and augmented fuel flows in a closed-loop system; and c) control the nozzlein a closed-loop system.

The DEEC computer is a 16 bit, 1.2 microsecond cycle time micro-computer with10.5k available memory. The entire electronic unit is fuel cooled, and is enginemounted.

The DEEC secondary engine control (SEC) is a hydromechanical engine fuelcontrol. It is mechanically integrated within the gas generator fuel meteringhardware of the DEEC. In the event of a critic~l DEEC failure, or at the pilot'soption, the SEC system can be engaged. The SEC inputs are PLA, TT2, PS2, and RCVVposition. Based on these parameters, the SEC system controls the engine fuel flow,the RCVV position, and the compressor start bleed.

The Jet Fuel Starter (JFS) is a small auxiliary gas turbine power unit whichcan be coupled to the F100 engine. The JFS is used to accelerate the highcompressor for engine starting on the ground. It may also be used in flight ataltitudes below 7000 m. The JFS disengages automatically when 50-percent N2 isachieved.

Pressures, temperatures, rotor speeds, fuel flow, and positions of variablegeometry are measured at various positions in the F100 EMD engine. Engine para­meters important to this report are PLA, N2, PB, FTIT, and WF. All parameters areinput into a pulse code modulation (PCM) system during the test flights. Thedigital PCM data are recorded on an onboard tape recorder and also telemetered tothe ground for real time display in the control room.

DEEC Airstart Logic

In the event of an engine shutdown or flameout, the DEEC monitors severalparameters to insure a successful airstart. An open-loop lightoff fuel flow ismetered into the combustor until lightoff is detected. Once lightoff has beendetected by the DEEC by an increase in FTIT, fuel flow and compressor bleeds arecontrolled by the closed-loop logic shown in figure 5. This logic attempts tomaintain a desired N2 rate by varying fuel flow. The desired N2 rate is a functionof PT2, TT2, and M. If the fuel flow is too high, the compressor may stall,resulting in a "hot start" or the combustor may blowout from an overrich fuel-airratio. If the fuel flow is too low, the energy available will not be sufficient toovercome the losses in the engine and the accessory power drain, resulting in a"hung start". The DEEC airstart logic maintains the scheduled N2 rate subject to abias if FTIT exceeds a temperature limit. The minimum fuel flow, set by a stop inthe fuel metering valve, is approximately 115 kg/hr. The compressor bleeds are heldopen until a scheduled value of N2 is achieved.

DEEC logic 4.2.2, which is an updated version of logic 4.2.1, incorporates lllanychanges, including several to the airstart logic. These are shown in Table 1.Logic 4.2.2 increased the N2 rate schedule, biased lightoff fuel flow and trim rateslew out by PT2, raised the percentage N2 before the start bleeds closed, andreduced the FTIT limit during airstarts. These changes help to prevent hot startsand significantly reduce airstart times.

3

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TEST PROCEDURE

Tests were performed to compare the airstart capability of the FI00 EMD enginewith logic 4.2.2 to the capability of the former logic, 4.2.1. The three types ofairstarts examined are 40-percent spooldown, 25-percent spooldown, and JFS assisted.For all airstarts the normal F-15 power requirements for the engine and accesorieswere present.

The spooldown airstart is achieved in a four step procedure: 1) engineshutdown, 2) pressurization, 3) light, and 4) acceleration of the engine to idlespeed. The engine shutdowns were mostly performed from the intermediate powersetting. The compressor rotor was then allowed to wind down (spooldown) to apredetermined percentage of maximum core speed. For the evaluation of EMD airstartcapability, values of 40-percent N2 and 25-percent N2 were used. The pressurizationstep was accomplished when the pilot returned the throttle to the idle power settingto begin the start cycle. This pressurized the fuel system and fuel began to flowto the combustor. Approximately 8 seconds later, the fuel reached the combustornozzles and was ignited (light). The fuel flow was modulated by the DEEC tomaintain the desired N2 rate until the scheduled idle speed was reached and theairstart sequence was completed. Airstart time, T, is calculated from the time ofpressurization to the time when idle N2 is reached in the above procedure.

The JFS assisted airstart is accomplished by coupling the jet fuel starter tothe high compressor rotor through a gearbox. The JFS may be engaged at any N2 speedfrom 0 to 30-percent. The pressurization step may be initiated at a core speed of12-percent or greater. The JFS disengages automatically at 50-percent N2.

Of the 35 primary DEEC airstarts attempted during the test flights, 18 were40-percent spooldown, 12 were 25-percent spooldown, and 5 were JFS-assisted.

During the airstart tests the pilot used one engine for the test and maintainedthe desired altitude and airspeed with the other engine. Airspeed was held within 4knots and altitude within 30 m of the desired test condition. Test day temperatureovaried as much as + 10 C from standard day temperatures. More details of the testprocedure can be fOUnd in reference 1.

RESULTS AND DISCUSSION

Spooldown Airstarts

Figure 6 is a time history of an EMD DEEC logic 4.2.2 airstart at 250 knotscalibrated airspeed and an altitude of 10,700 m. The pilot initiated the airstartprocedure by shutting down the engine at t = 11 sec. The core speed, N2, immedia­tely began to spool down with a rapid drop in fan turbine inlet temperature (FTIT).The core reached 40-percent rpm at t = 34 sec,at which time the pilot moved thethrottle to idle, which pressurized the fuel system and initiated the airstartsequence. The fuel began to flow through the fuel manifold, however FTIT and N2continued to drop until t = 42 sec when the fuel reached the combustor and wasignited as indicated by the rise in FTIT. The DEEC closed-loop logic then modulatedthe fuel flow to achieve the desired rate of acceleration of the engine core. N2increased uniformly until t = 60 sec, then increased its acceleration. FTIT

4

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increased along with the increased N2 rate while fuel flow, WF, was decreasing,indicating a sudden increase in the efficiency of the main combustor. This increasein burner efficiency has been noted previously at high altitude conditions. Idlerpm was reached at t = 79 sec. The airstart time, T, defined as the time frompressurization to idle, was 45 sec.

Figure 7 shows a 40-percent spooldown airstart at the same flight conditions of250 knots and 10,700 m, but with DEEC logic 4.2.1. The pilot shutdown the engine att = 11 sec. Fuel flow quickly went to zero, while core speed and FTIT droppedrapidly for the first few seconds, then more slowly. The engine reached 40-percentN2 at t = 31 sec, at which time pressurization occurred. Engine rpm and FTIT

ocontinued to drop, reaching 30-percent and 412 C respectively at t = 42 sec, whenthe fuel mixture ignited. The compressor rpm increased uniformly until t = 63 sec,when N2 rate increased due to the increase in combustor efficiency, as previouslynoted in figure 6. Idle rpm was reached at t = 93 sec. The airstart took 62 seccompared to 45 sec for DEEC logic 4.2.2, shown in the previous figure.

Spooldown to a lower percentage N2 increased the airs tart time considerably.Figure 8 shows an airstart with DEEC logic 4.2.2 at the same flight conditions asfigure 6, 250 knots and 10,700 m. The difference is a 25-percent spooldown insteadof a 40-percent spooldown. The pilot shutdown the engine at t = 13 sec and pressur-oized at t = 66 sec. The engine spooled down to 23-percent N2 and FTIT was 325 Cwhen the fuel ignited at t = 75 sec. The engine reached idle speed at t = 123 sec.The total airstart time was 57 sec compared to 45 sec for the same logic at the sameflight conditions but for a 40-percent spooldown airstart.

Figure 9 is another comparison between logic 4.2.2 and 4.2.1. It shows thesame spooldown percentage and flight conditions as figure 8 but this time with logic4.2.1. The pilot shutdown the engine at t = 10 sec and pressurized at t = 59 sec.oEngine rpm and FTIT dropped to 21 percent and 285 C respectively at t = 70 sec whenthe burner light occurred. The engine reached idle at 130 sec. The airstart timewas 71 sec compared to the time of 57 sec for the same airstart with DEEC logic4.2.2.

Airstarts at lower airspeeds took longer because of the reduced energy of theinlet flow, lower burner pressure, and lower stall margin. Figure 10 shows a40-percent spooldown airstart at an airspeed of 200 knots and an altitude of10,700 m. Shutdown occurred at t = 9 sec and the system was pressurized att = 26 sec. The fuel ignited at t = 35 sec when rpm was 31 percent and FTIT was

o400 C. The engine reached idle at t = 84 sec for an airstart time of 58 sec. Thismay be compared to the 250 knot airstart in figure 6 which had an airs tart time of45 seconds. Also this may be compared to the same airstart performed with DEEClogic 4.2.1 which had an airstart time of 92 sec, indicating a reduced time forlogic 4.2.2 by 37 percent.

Airstarts were performed at different altitudes to test the effect of altitudeon airstart times. Figure 11 is a 40-percent spooldown airstart at 250 knots and analtitude of 7,600 m. The pilot shutdown the engine at t = 7 sec and pressurized att = 22 sec. The engine spooled down to 31 percent and FTIT reached 500 °c beforethe light occurred at t = 30 sec. The engine reached idle speed at t = 55 sec foran airstart time of 33 sec. This may be compared to the airstart at 10,700 m whichtook 45 sec. The same airstart as figure 11 but for DEEC logic 4.2.1 had a time of48 sec. The modifications in DEEC logic 4.2.2 reduced the airstart time by 31percent.

5

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JFS-Assisted Airstarts

The JFS was utilized to test for faster airstart times at conditions within theJFS envelope. Figure 12 shows a time history of a JFS-assisted airstart at anairspeed of 170 knots and an altitude of 7,000m. The pilot shutdown the engine att = 3 sec and engaged the JFS at t = 41 sec, when N2 was at 13 percent. The JFSaccelerated the compressor, and the pilot advanced the throttle to idle att = 46 sec. The JFS continued to accelerate the compressor and the light occurredat t = 56 sec. The compressor quickly accelerated to 50 percent. When the JFSdisengaged, the N2 rate dropped off for a few seconds, then increased again, andidle was reached at t = 83 sec. The airs tart time was 37 sec, compared to a25-percent spooldown at similar conditions of 175 knots and 7,600 m, which took76 sec.

The same JFS-assisted airs tart at an altitude of 7000 m and an airspeed of170 knots was performed with DEEC logic 4.2.1. The airstart time was 60 sec.DEEClogic 4.2.2 improved this airstart time to 37 sec, a decrease in time of 38 percent.

Summary of Airstart Times

Comparisons of the airstart times for DEEC logic 4.2.1 and 4.2.2 are shown infigures 13 and 14 for 40-percent spooldown airstarts and 25-percent spooldown air­starts respectively. The results show a large improvement in DEEC logic 4.2.2 over4.2.1. In figure 13, the 40-percent spooldownairstart times for the DEEC logic4.2.1 range from 52 sec at 250 knots and 7,600 m to 133 sec at 7,600 m and175 knots. These times were taken from reference 3. For DEEC logic 4.2.2,however, airstart times range from 33 sec to 62 sec for the same conditions. Thusthe modified logic reduced the airstart times 37 percent to 53 percent. The largestdecrease in times came at the lower airspeeds. This is not surprising since themodified logic calculates fuel flow rate as a function of airspeed. This results inthe large improvements in the airstarts at low airspeeds.

The 25-percent spooldown airstart results shown in figure 14 are similar.Times for DEEC logic 4.2.1 ranged from 56 sec at 3050 m and 250 knots to 170 sec at7600 m and 175 knots. Times for DEEC logic 4.2.2 ranged from 39 sec to 83 sec atthe same conditions. This was a reduction in time of 30 percent to 51 percent.Again, the greatest reduction in times was for the slower airspeeds.

Unsuccessful Airstarts

The FI00 EMD experienced four unsuccessful airstarts during the flightevaluation of the 4.2.2 logic. TwO of these were hot starts, in which the enginelit normally, but the FTIT exceeded the engine starting temperature limit. Theother two were "blowouts" in which the combustor flame blew out and did notreignite.

Figure 15 shows the time history of an airstart in which a combustor blowoutoccurred. This happened on a 2S-percent spooldown airstart at an altitude of10,700 m and an airspeed of 200 knots. The shutdown occurred at t = 10 sec and thesystem was pressurh:ed at t = 47 sec. N2 and FTIT increased normally untilt = 81 sec when the blowout occurred. The pilot waited 12 sec to see if the burnerwould relight, after which he shutdown the engine, terminating the airstart test,

6

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and increased airspeed. He pressurized again at. t = 101 sec and N2 accelerated veryrapidly to idle. Figure 16 is a plot ot N2 versus fuel-flow to burner pressureratio, WF/PB, which closely resembles fuel-air ratio. It shows that when theblowout occured at N2 = 31.5 percent, WF/PB was 44. This mixture appears to be toorich for the low pressure and temperature present in the combustor causing a richblowout. The DEEC logi~ does not recognize blowouts and continued to increase fuelflow until the pilot terminated the airstart. Thus, in figure 16, WF/PB continuedto increase during the spoo1down after blowout, preventing a relight. One otherblowout occurred at 225 knots and an altitude of 12,200 m for the same reasons asabove.

Figure 17 shows the time history of a hot start at an altitude of 10,700 m andan airspeed of 175 knots. At t = 2 sec the pilot shutdown the engine and thenpressurized at t = 18 sec. The light occurred at t = 29 sec. N2 did not increaseand even with the fuel flow at its minimum value, the FTIT continued to increase,

oindicating a compressor stall on the lightoff. When the FTIT reached 750 C att = 44 sec, the pilot discontinued the test by shutting down the engine andincreasing airspeed, eventually reaching 300 knots. FTIT and N2 quickly droppeduntil the pilot repressurized at t = 51 sec. Then N2 quickly accelerated. to idle.

The fourth unsuccessful airstart, a 40-percent spoo1down at 200 knots and10,700 m, also resulted in a hot start. The test was repeated since the new logicwas designed to prevent hot starts. It was successful. A plot showing an overlayof the successful and unsuccessful airstarts at this condition is shown infigure 18. It shows that spoo1down rate and initial fuel flow are very similar butthere is some difference in FTIT. Prior to the hot start, the engine had been atintermediate power for a longer time, significantly increasing FTIT, and resultingin a hotter compressor. When the airstart was initiated, the light was normal, butafter about 5 sec, the N2 rate dropped off to zero while the FTIT continued to

oclimb, indicating a stall. As FTIT exceeds 700 C the fuel flow was reduced but withthe stalled compressor, recovery was not possible. The pilot shutdown the engine,increased airspeed, and successfully completed the airstart.

Summary of Spoo1down Airstart Success

Figure 19 summarizes the successful and unsuccessful airstarts for EMD DEEClogic 4.2.2 and logic 4.2.1. Airstarts below 10,700 m were all successful withlogic 4.2.2. At 10,700 m, three were unsuccessful; one a blowout at 200 knots and25-percent, one a hot start at 175 knots, and the third, a 40-percent spoo1downairstart at 200 knots that was successfully repeated. The blowout at 12,200 m and225 knots was not unexpected since the airstart was conducted at the upper limit ofthe airstart envelope.

Comparing the unsuccessful airstarts of logic 4.2.2 to those of logic 4.2.1,two significant differences appear. One is the now successful airstart at 3050 mand 175 knots which failed with logic 4.2.1. The success is due to the revised N2schedule and the other improvements in Table 1. The second difference is theblowouts which occurred at high altitude. Flight testing of airstarts with logic4.2.1 were never conducted at 12,200 m, thus rendering it impossible to make acomparison. Blowouts occurring with logic 4.2.2 were probably due to the higher N2rate schedules that resulted in a higher fuel-air ratio.

7

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CONCLUDING REMARKS,

A series of airstarts were conducted in an F-15 airplane with two prototypePratt and Whitney F100 Engine Model Derivitive engines equipped with DigitalElectronic Engine Control systems utilizing logic 4.2.2. The airstart envelope andthe time required for airstartswere defined. Comparisons were made between theoriginal logic, 4.2.1, and the modified 4.2.2 logic.

Spooldown airstarts with the 4.2.2 logic were more successful at lower alti­tudes than were those with logic 4.2.1. Spooldown airstart times ranged from33 sec at 250 knots to 83 sec at 175 knots. 4.2.2 logic improved the airstart timeby 31 percent to 53 percent, with the most improved times at slower airspeeds.JFS-assisted airstarts were conducted at 7000 m and airstart times were signifi­cantly faster than unassisted airstarts. The effect of altitude on airstart timeswas small.

The 4.2.2 logic, having higher N2 rate schedules, did result in more unsuccess­ful airstartsat the upper part of the airstart envelope at very low airspeeds.Combustor blowouts and hot starts occurred at test conditions where the 4.2.1 logicwould have been able to make a very slow but successful airstart.

NASA Ames Research CenterDryden Flight Research Facilty

P. O. Box 273Edwards, California, May 10, 1984

REFERENCES

1. Myers, L.P., : Flight Test of a Full Authority Digital Electronic EngineControl in an F-15 Airplane. AIAA Paper 81-1501,'July, 1981.

2. Licata, S.J., and Burcham, F.W. : Airstart Performance of a Digital ElectronicEngine Control System in an F-15 Airplane. NASA TM 84908, April, 1983.

3. Cho, T.K., and Burcham, F.W. : Preliminary Flight Evaluation of FI00 EngineModel Derivative Airstart Capabilities in an F-15 Airplane. NASA TM 86031,July, 1984.

8

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N2 RATE SCHEDULE

LIGHTOFF FUEL FLOW

TRIM RATE SLEW OUT

START BLEED CLOSURE

FTIT LIMIT DURING STARTS

TABLE 1.

DEEC SOFTWARE RELEASE

4.2.1 4.2.2

(MAR-JUNE 1983) (JULY-SEPT 1983)

BASE INCREASED

f(FTIT) f(FTIT, PT2)

f(M) f(M, PT2)

56-percent N2 61-percent N2

760°C 704°C

Significant differences in airstart logic

between software release 4.2.1 and 4.2.2.

9

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Figure 1. Photograph of the F-15 airplane.

Figure 2. Photograph of the FI00 EMD test engine.

10

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~~ ~"'-Ducted;:WOld:r---- __-r

Augmentor fuel spray ringsCompressor

start bleed

Rear compressor variablevanes (RCVV)

High-pressurecompressor

High-pressureturbine

Compressor inletvariable vanes(CIVV)

Fan turbineAugmentor ignitors

(dual)

{Mixed flow (Variable area

augmentor nozzle (AJ)

.,= .g!p?ffi"te~

~~~~~j~ "---------- --- --- --_ ..

Figure 3. Cutaway view of the FIOO EMD engine

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---- SEC

~ N2(DUAL) • N1 • TT2 • FTIT • PS2 • PB • PT6M

ELECTRIC N1 TT2 HIT PS2 P8 PT6MALTERNATOR SENSOR SENSOR SENSOR SENSOR SENSOR SENSOR

ELECTRIC (DUAL) (DUAL) (DUAL)POWER

•TT2DEEC PLA-.., I r--PS2,. __l __I __1__,

AUGMENTOR FUEL FLOW NOZZLEPLA OUTI'UT ~__ ~ HYDRO MECHANICAL ~ ______ L • CONTROL--. INPUT

VARiillE CONTROL DIGITAL TO I BACKUP CONTROL I 1

M TO DIGITAL COMPUTER ACTUATION r -i---r--------J CORE FUEL DUCT FUEL-- CONVERSION VAlUABLE: WF.G METERING METERING ....

CONYEIlSION I I VALVE VALVEI I :

I I ENGINE FUEL r FUEL DISTRIBUTIONSTAIIT I METERING AND REGULATION

I CIVV I BLEED I I RCVV I VALVEI

• ~ I ~ T SEGMENTI

ACTUATOR I -; ACTUATOR I ,.I ACTUATOIl f4J ~ ACTUATOR I SEQUENCEACTUATOR I ACTUATOR I.. ACTUATOR ~ ACTUATOR .. ..

POSITION • POSITION POSITION POSITION POSITION ~SITION POSITIONTRANSDUCER TRANSDUCER TRANSDUCER TRANSDUCER TRANSDUCER TRANSDUCEIl TRANSDUCER

STARTBLEED (DUAL) (DUAL)

SOLENOID

4

Figure 4. Block diagram of the FIOO EMD/DEEC control system

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.....w

COMPRESSORSTART BLEED

N2 i

FTITJFS N2 .

ENGAGED JL. N2 WF~

? dt ~ 1"'\

PS2~If ~

TT2 -;:I~• , D.N°2N2 WF WF

" \-PLA req

M .. °N2 D.N2 FTIT

SCHEDULES TO FUEL FLOH BIAS

Figure 5. FIOO EMD/DEEC airstart logic

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WF,kg/ht

FTrT,

deg. C

500

o

1000

500

-

---

I ,I I I

PLA,deg 50

oo 20 40 60 80 100

14

t,secFigure 6. F100 EMD 40-percent spooldown airstart.

DEEC logic 4.2.2, VC = 250 knots, HP = 10,700 m.

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IDLEr.SHUTDOWN PRESSURIZATION

LIGHT

50:[J~O_~JI .

.500

1000

FTIT,deg. C

WF,kg/hr

o

100

N2,percent

80

60.

40

20

o

100

PLA, 50deg

oo 20 40 60 80 100

t, sec

Figure 7. FlOO EMD 40~percent spooldown' airstart.DEEC logic 4.2.1, VC '= 250 knots, HP = 10,700 m.

15

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WF,kg/hr

FTIT,deg. C

O'-----L----I----.L.-...:.....-...;~---~----'-:---'

100

80

N2, 60percent

40

20

16

PLA,deg

OJ...-_~_.L.._ .L.._ L._ '__ L._ .L..______'

100,.....

50~

ol...----'---L'__....L-I__.L.-.J.I_'--JII-_-J.I__...J.-I..;....I_--IIo 20 40 60 80 100 120 140

t, sec

Figure 8. FlOO EMD 25-percent spooldown airstart.DEEC logic 4.2.2, VC • 250 knots, HP = 10,700 m.

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500

SHUTDOWNPRESSURIZATION

LIGHT r!DI.'

WF,kg/hr

0L....~.L-.....L -.J- .u.- ..:.-.-1..--.;.--.:..--L_-_....L.-~-.I

1000

FTIT,deg. C 500

0

100

80

60N2,percent

49

20

0

100

PLA,deg 50

00!.-._....I-_-'-- I--....;...._...u..--.:..-:.._...I- l-..__--I._---..:~...J

20 40 60 80 100 120 140

t, sec

Figure 9. F100 EMD 25-uercent spooldown airstart.DEEC logic 4.2.1, VC = 250 knots, HP = 10,700 m.

17

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WF,kg/hr

SHUTDOWN

o [I ~""';'~_"'----J1000

n

FTIT,deg. C

500

0

100

80

60N2,percent

40

20

0

100

18

PLA,deg 50

t, secFigure 10. FlOO EMD 40-percent spooldown airstart.

DEEC logic 4.2.2, VC = 200 knots, HP = 10,700 m.

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0

100

80

N2,percent 60

40

20

0

100

50

500

SHUTDOWN,. IDLE

5000.o .,[,d,

I1000

PLA,deg

FTIT,deg. C

WF,kg!hr

~i

t, secFigure 11. F100 EMD 40-percent spooldown airstart.

DEEC logic 4.2.2, VC= 250 knots, HP = 7,600 m.

19

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OL.,..;..__--L ...L...__-:....L...-_-..:.--I. ~

JFI) ENGAGEPRESSURIZATION

rSHUTDOWN rLICHT [JFS[D~;::GAGE

50:~~~!1-----L:J1...:...--..a-:

1000 I

FTIT,deg. C 500

WF,kg/hr

N2,percent

100

80

60

40

20

0"-----"'-------''----.........------''-----'

100

PLA,deg 50

Ol~'-----'----~.....I'--~----:-~--~

ot,sec

Figure 12. FIOO EMD JFS assisted airstart.DEEC logic 4.2.2, VC = 170 knots, HP 6,100 ID.

20

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140

HP, m

1300

0 30500 7600

0 10,700

120OPEN SYMBOL DENOTES

0 DEEC LOGIC 4.2.1

110 SOLID SYMBOL DENOTESto' DEEC LOGIC 4.2.2

100

90

T,

sec80

070

60 • 0

•50 • §

• •40 •30 I

275250225200175

20 '-- .!.-. ...I- -&-. .....J- --'

150

vc, knots

Figure 13. Cpmparison pf .DEEq logic 4.2.1 to 4.2.2and effect of air$peed on airstart timefor 40-percent spooldown airstart.

21

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0

160 HP, m

0 3050

150 0 76000 10,700

140OPEN SYMBOL DENOTES

DEEC LOGIC 4.2.1

SOLID SYMBOL DENOTES130 DEEC LOGIC 4.2.2 <'\

,

120

0110

0

100T,

sec90 <)

•80

070

I •60

•275250225200175

30~-----"L.--. .---I~ .---IL-- .---IL-- --J

150

VC, knots

Figure 14. Comparison of DEEC logic 4.2.1 to 4.2.2and effect of airspeed on airstart timefor 25-percent spooldown airstart.

22

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WF.kg/hr

I ..~ INCREASING ..r- AIRSPEEDBLOWOUT

PRESSUR'IZATIO HUTDOWN (TEST TERMINATED)rSHUTDOliN LIOIf! rPRErS~~~ZATION rIDLE

5°:D~_---.L.--I..;"'_~'_': ~'~':lJD dFTIT.des. C

O........;_-"" ~-+_...:...I. ...L:.__~,I,;.....:.._..... ""'-__---I

0.--

f-

o~

11" I I II d I I I I I I

5

10

PLA.deg

N2.percent

o 20 40 60 . So 100 120 140 160

t. sec

Figure 15. FlOO EMD 25-percent spooldown "blowout".DEEC logic 4.2.2. VC = 200 knots HP = 10.700 m.

23

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70 "--.... "SPOOLDOWN

WF/PB

60

50

tBLOWOUT PO f.NT

2'-- -..l. J...- ...I- --L ~ ~

20 22 24 26 28 30 32

4

N2. percent

Figure 16. FIOO EMD 25-percent spooldown airstart.Fuel-Air Ratio vs. N2, Combustor Blowout.DEEC logic 4.2.2, VC = 200 knots HP = 10,700 m

24

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0

100

80

N2, 60

percent

40

20

0

100

.;,

WF,kg/hr

FTIT, ,deg. C

PLA,deg

SHUTDOWNPRESSURIZATION

LIGHT SHUTDOWN

J II U"dC1000 I

500

50

o"""""""__...u.. ...-.I-...I--1 ..L.__--..l

o 20 40 60 80 100

t, sec

Figure 17. FWO EMD 40-percent spooldown "hot"start.DEEC logic 4.2.2, VC = 175 knots HP = 10,700 m.

25

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SUCCESSFUL

UNSUCCESSFUL

.... ;

,. _..- ...... ,..... -

SHUTDOWN (UNSUCCESSFUL)SHUTDOWN IDLE (SUCCESSFUL)

oD [,~L I

I

500

1000

FTIT,deg. C

WF,kg/hr

0

100

80

60N2,percent

40

20

OL-......:...._-L--:.._~L-__-L--:-.....,.J'--_......

100

PLA,deg 50

t, sec

Figure 18. Comparison of successful to unsuccessful airstartsF100 EMD 40-percent spooldown airstart.DEEC logic 4.2.2, VC = 200 knots HP = 10,700 m.

26

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4

2

4

2

~ 25-percent spooldown no flags - hung start~ 40-percent spooldown 1 flag - blowout

2 flags - hot startopen symbol - successful - standard F100 enginesolid symbol - unsuccessful 777 77

handbook limit

200300 7);/250 300175 / }25 250

12 xl03 Il// 12 x103

'*'-"ee ~e e e10

II10

I/h8 8eeee

HP, m HP, m

6 6

.2 .4 .6 .8 1.0 .2 .4 .6 .8 1.0M

DEEC logic 4.2.2

Figure 19.

M

DEEC logic 4.2.1

Summary of EMD spooldown test success.

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For sale by the Nat~ona1 Techn~ca1 Informat~on Serv~ce, Spr~ngf~e1d, Virginia 22161.

1. Report No. 2. Government Accession No. 3. Recipient's Catalog No.

NASA TM-859004. Title and Subtitle 5. Report Date

Effect of Control Logic Modifications on Airstart PerformanceAugust 1984

of Fl00 Engine Model Derivative Engines in an F-15 Airplane 6. Performing Organization Code

7. Author(s) 8. Performing Organization Report No.

David B. Crawford and Frank W. Burcham, Jr. H-1243

10. Work Unit No.9. Performing Organization Name and Address

NASA Ames Research Center 11. Contract or Grant No.Dryden Flight Research FacilityP.O. Box 273Edwards, California 93523 13. Type of Report and Period Covered

12. Sponsoring Agency Name and Address Technical Memorandum

National Aeronautics and Space Administration 14. Sponsoring Agency CodeWashington, D.C. 20546

RTDP 533-02-21

15. Supplementary Notes

16. Abstract

A series of airstarts were conducted in an F-15 airplane with two proto-type Pratt and Whitney Fl00 Engine Model Derivative engines equipped withDigital Electronic Engine Control (DEEC) systems. The airstart envelope andthe time required for airstarts were defined. Comparisons were made betweenthe original airstart logic, and modified logic which was designed to improvethe airstart capability. Spooldown airstarts with the modified logic weremore successful at lower altitudes than were those with the original logic.Spooldown airstart times ranged from 33 seconds at 250 knots to 83 secondsat 175 knots. The modified logic improved the airs tart time from 31 percentto 53 percent, with the most improved times at slower airspeeds. Jet fuelstarter (JFS)-assisted airs tarts were conducted at 7000 m and airstart timeswere significantly faster than unassisted airstarts. The effect of altitudeon airstart times was small.

17. Key Words (Suggested by Author(s)) 18. Distribution Statement

Airstart Unclassified-UnlimitedDigital controlF100 engineF-15 airplane STAR category 07

19. Security Classif. (of this report) 20. Security Classif. (of this page) 21. No. of Pages 22. Price'

Unclassified Unclassified 27 AD3It

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.;