an ojt report on 3 month internship at surya nepal
DESCRIPTION
Review of project carried out at Surya Nepal Pvt. ltd during three month On The Job Training.TRANSCRIPT
Bikram DahalThapathali Campus
PMD
OJT AT SURYA NEPAL
SupervisorAyush Raj Aryal
I/C PMD
Projects
• Admoist protocol
• Increase filling value of Surya
Main projects
• Spillage reduction in CTS bin
• GFP feed maintenance at CRS Cutter
• Cp & Cpk of CRS Dryer
• Optimization of blend change time (CRS line)
Side Project
• Design of pan for Sampling at HT and stand for Serrico TrapDesign
ObjectiveIncrease productivity, quality and profitability through keen data analysis and process design; significantly improve operations and provide efficient resolution of process issues.
OJT at Surya Nepal
Methodology
Asking question (understanding problem)
Labeling patterns in data
Modeling conceptually
Decomposing
Experimenting
implementation
Continual monitoring and communicating
1
2
4
5
6
7
3
OJT at Surya Nepal
Moisture Content
variation in cutter above
0.5
Raw material Method Mother Nature
Size distribution
Intrinsic Property
Moisture Content
Type
(cold or Hot)
Bulking time
Temperature
Power failure
Humidity
Hand feel
Moisture
Measuring Instrument Least count Setting of machine
Uniformity of filling
Uniformity of water, raw material
and steam flow
MachineMan
Finding
Fig 1: Fish bone Diagram of causes for moisture variation
Admoist protocol and Data Analysis
Result and Discussion
35.50
36.00
36.50
37.00
37.50
38.00
38.50
39.00
39.50
40.00
0 5 10 15 20 25 30 35
Moisture Mean Ex-cutter
0.00
0.10
0.20
0.30
0.40
0.50
0.60
0 5 10 15 20 25 30 35
S.D Chart
Admoist protocol and Data Analysis
Result and Discussion
• Weight deviation
for HVM/VSN5
stem is high
because stem of
this Grade are
longer and have
non-uniform
thickness
Admoist protocol and Data Analysis
0.00%
1.00%
2.00%
3.00%
4.00%
5.00%
6.00%
0 5 10 15 20 25 30
Coefficient of Variation of weight
• Failure of PRV to maintain set pressure of 0.3-0.4 bar. Line pressure was changing as per main pressure variation.
• Main line pressure was decrease to 5bar from maximum pressure of boiler i.e. 7- 8 bar.
Cause Solution Result• Temperature of 3 samples
of 3 operation was tracked average value was found 71 C
Due to low filling value of CRS from regular interval in QUAS daily report after 17 aswin.
Temperature of product at 1 meter distance from outlet of admoist was checked. It was
found that temperature was above SOP i.e. 76.
Further Step
Admoist protocol and Data Analysis
Finding (Research)
• Virginia Tobacco have less filling Value due to high sugar Content
• Lamina Cutter is optimum at 32CPI other argue its best at 25 CPI
• F.V varies among different part of same leaf, between different year crops
• FV is very sensitive to moisture
• Main control able factor effecting filling value
• HT steam pressure
• CPI of cutter
• Storage time and temperature
• Cheese pressure of cutter
• Type of dryer
Increasing filling Value of Surya
Finding(Data analysis)
• F.V after Ex-cutter was below average
• Expansion from cutter to H.T of both
lamina and CRS was with in speciation limit
• CPI of Cutter was below average and
not uniform
• Steam pressure of CRS H.T could be increase
• Order of operation had no effect on
filling value
Increasing filling Value of Surya
13.62
8.11
0%
2%
4%
6%
8%
10%
12%
14%
16%
Ex-cutter to Ex-bin Ex-cutter to Ex-Dryer
CRS Lamina
• Filling value jump from ex-
cutter and ex-dryer
Step taken to improve F.V
• Maintenance and Calibration of Cutter was carried out
• Steam pressure of CRS H.T was increased from 4bar to 5bar
• Cheese pressure of lamina cutter was reduce for NG to 15KN
• Temperature of lamina dryer was reduced from 66 C to 62 C
Increasing filling Value of Surya
Increasing filling Value of Surya
CPI of Cutter Result
139
166
0
20
40
60
80
100
120
140
160
180
Before After
CP
I0.00
0.05
0.10
0.15
0.20
0.25
0.30
0.35
0 10 20 30 40 50
Wax Thickness (before)
0
0.05
0.1
0.15
0.2
0.25
0 10 20 30 40 50
Wax Thickness (after)
Result
Increasing filling Value of Surya
47.78
49.15
47.00
47.50
48.00
48.50
49.00
49.50
Before After
Filling Value Cut Tobacco
* FV value for before batch (NG1-42) and after (NG-43-78) was taken form QUAS daily report
After Before
Mean 49.16 47.78Observations 32 36p-value 2.91E-06
• Continuous
monitoring was
carried till end of
project
Scope of Further Improvement
• Increase tobacco and steam ratio to find optimum ratio in H.T
• Changing rate and temperature of airflow in dryer
• Experimenting with CPI of both cutter under control environment
Increasing filling Value of Surya
Result
0
0.5
1
1.5
2
2.5
3
3.5
1 2 3 4 5 6 7 8 9 10
Old Boiler | | New boiler
Cp and Cpk of CRS dryer
Cpk
Cp
0
0.1
0.2
0.3
0.4
0.5
0.6
0.7
0 1 2 3 4 5 6 7 8 9 10Old Boiler | | New Boiler
SD chart of Steam pressure at HT
Cp and Cpk of CRS Dryer
• Large tart time difference between VOV(2) and bin belt conveyer(1) i.e. 5 sec
• High speed of Belt conveyer(6)
• Start time difference between 2 and 1 was reduce to 1 sec
• Speed of 6 was reduce to 12+0.5 all other blend except VSY from which it was reduce to 15+ 0.5
Cause Solution Result• No single gap between
stem in conveyer from bin to cutter
• Product at GFP was visible most of the time
In order to maintain uniform flow of product at CRS cutter, product level at GFP should always
be visible. But some of the time, product at GFP of CRS cutter is empty.
Introduction
Feed maintenance at CRS cutter GFP
Feed maintenance at CRS cutter GFP
• Inter-
operational
time 8 minutes
• 90sec gap
• 390sec time
difference
between start
and finish
Stem Conditioning
WEIGHCON
SC
ADMOIST
AIR LIFT
Optimization of Blend Change Time
40 sec 65 sec 165sec
45 sec 510 sec
sec
60 sec
30 sec
35 sec
OP 1 390 sec 90 Sec OP 2
Inter-operational time
Start:
Finish:
GapDiff. start to finish
HT• Speed cylinder
rpm at tail out was increase from 16 to 18
• Decrease In 1 minutes tail out time
• Inter-operation time is 360sec after sensor in GFP Detects no Tobacco
CRS Dryer
VC
WEYCON
KLS
Optimization of Blend Change Time
55 sec 70 sec 390 sec 45 sec
705 sec90 secVariable 40 -240 sec 50 sec
Start:
Finish:
secOP 1 280 sec 80 Sec OP 2
Inter-operational time
GapDiff. start to finish
Design
Design of Pan for Sampling at HT
Summary
• Admoist protocol was passed
• Filling value of NG was increased by 3% on average
• Cp and Cpk of CRS dryer were calculated
• Spillage of CTS was reduce by 5-8 kg/day
• Uniform feed at CRS cutter was maintained
• Pan and stand were designed
• Standard blend change time was established for CRS conditioning and CRS
Dryer line. Along with decrease in tail out time of CRS dryer.
OJT at Surya Nepal