update repo{[ced!!n1ylneitmtfont cofjtrol block: | |h · obse"ved by jeff chumley, georgia...

22
" , " Update Repo{[CEd!!n1YlNeitMtFont m 28-78 , COfJTROL BLOCK: | | | | | | |h !PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) i e lo li|-|C I A l c II In i 2 l@lo lo |- Io lo lo o 10 |- 1010 l@l4 11 11 Il 11 l@l | |@ 7 8 9 LICEt.SEE LODE 14 lb . LsL L rol Nuvut et 2a Jt, LICE %E T Y PE JO b7 LA1 bd C T b c 'l $$U dl 0 | 5 | 0 | 0 l Ol 3 | 6 | 6 hl 0 | 7 | 2 | 4 | 7 | 8 }@|0 | 2 |0 | 9 | 7 | 9 |@ " " CE P S 60 01 DOCsc ET NUMUER ed 63 EVENT DATE le 7b HEPOH T DATE 6J EVENT DESCRIPTION Af40 PROOAULE CONSEQUENCES h O 2 Durina tho heatun tilateau of Unit 2 Startun Testing the average drywell tenperature | o a i exceeded the limit of 135 F as set forth in Tech. Specs. Section 3.6.1.7. UpOn | o 4 | discovery of this condition, reactor heatup was terrainated in the ef fort to resolve | o 5 | the problem. l lO 161 I l O 7 I . O M | 7 8 9 80 SYSTEM C AUS E CAUSE C OY P. VALVE CODE CODE SUBCODE COMPONEN T CODE SuaCODE SUCCODE | A l A l@ La_J@ l ^ l @ I z I z I z I z I Iz I@ 6 @ 6 @ o 9 . 7 8 9 10 II 12 13 la 19 2J _, SEQUENTI AL OCCURRENCE REFORT REVISION LER RO t \ E NT Y E A R REPORT NO. CODE TYPE P O. @ gEg |217 j8 | |-| |0[0[6| y 0 |3 | ] g g 22 23 24 . ti 21 ?d 2"J 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATT ACHM E N T N P R D-4 PRIVE COP /P. COYPONENT 1AKEN ACTION ON PL ANT METHOD HOURS SUBVl1T E D FORM buis. SUPP LI E H MANUFACTURER W h!F|@ |Al@ |A|h |0 18|0|0) (Jjh |d@ |A |@ [7d7 Idh 1 7 3J s4 . Jo 3/ 40 41 4 43 44 47 _ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS ej LFo11owin9 reae t ar s''nt do'n on 7-] 7.- 73 _aD iTLo.?.Ltic h b v it e ch t al Pe*;qr _.Cnn,nm, %n,._ j 1 11 11| | and Georcia Power Comonnv perconnel revealed str,tifiention nf nie t r e,, o r , t o -n <- 4n I i y | tha drvvell. Analvsis of the nroblems resulted in an ournee from 8-?O-78 to 0 1;-78 l 13 | a | ] as detailed in the attachmont. The attach'.cnt was in,dsortently loft off Revisin" T| ]t |41 [ and is beine transnitted as Revision ? 7 8 9 80 FAC1LITY V E T54 DD OF STATUS % POWE R OTHER ST ATUS CE OVEHY DISCOVERY DESCRIPTION La_l@ lo lo lo l@L N/A | |C j@| Startup Testing | s s S JTiv,Tv cob 1 ' '2 " '' ** '' So AMOUNT 05 ACBVITY @ | nEtt AsEn c. HE LE CE LOC ATION OF HE LEASE li le | I z I @ Iz I@ N/A | N/A _j 7 8 9 10 11 44 4h 80 PE RSONNEL E xPCSuoES NUMB E R TYPE D E SCRI PTI ON 151711 o l o ol@lz @l N/A | 7 8 9 11 17 13 80 PEi1 SONNE L INJU AIES NU*tBER DESCRLPTDON |1 la | | 0 | 0 l 0 }@| N/A | " 790215o t OSS Or OR D * AGE TO F ACILITY 1 vPE DE SCRIF T TON E l 1 z Pl n/A 1 v 7 4 9 10 go c.. u[n tSCneTic . @ NRc tiSE ONLY , ?|' | Y D| Prens Delonso on Aur 91, ! o 7 9 , ,, ,, n , ., i ., . , j y|||||| ||||} n.,- ' . e, r,3 aso ; 7 a e w i N A?/.E OF PFtE P AR E R . . Creene, Supt, of Mr Fng. SNON E: (017) - - ,.

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Page 1: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

" , " Update Repo{[CEd!!n1YlNeitMtFont m 28-78,

COfJTROL BLOCK: | | | | | | |h !PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)i e

lo li|-|C I A l c II In i 2 l@lo lo |- Io lo lo o 10 |- 1010 l@l4 11 11 Il 11 l@l | |@7 8 9 LICEt.SEE LODE 14 lb . LsL L rol Nuvut et 2a Jt, LICE %E T Y PE JO b7 LA1 bd

C T

b c 'l $$U dl 0 | 5 | 0 | 0 l Ol 3 | 6 | 6 hl 0 | 7 | 2 | 4 | 7 | 8 }@|0 | 2 |0 | 9 | 7 | 9 |@" "

CEP S 60 01 DOCsc ET NUMUER ed 63 EVENT DATE le 7b HEPOH T DATE 6J

EVENT DESCRIPTION Af40 PROOAULE CONSEQUENCES hO 2 Durina tho heatun tilateau of Unit 2 Startun Testing the average drywell tenperature |

o a i exceeded the limit of 135 F as set forth in Tech. Specs. Section 3.6.1.7. UpOn |

o 4 | discovery of this condition, reactor heatup was terrainated in the ef fort to resolve |

o 5 | the problem. l

lO 161 I l

O 7 I.

O M |7 8 9 80

SYSTEM C AUS E CAUSE C OY P. VALVECODE CODE SUBCODE COMPONEN T CODE SuaCODE SUCCODE

| A l A l@ La_J@ l ^ l @ I z I z I z I z I Iz I@ 6 @ 6 @o 9 .

7 8 9 10 II 12 13 la 19 2J_, SEQUENTI AL OCCURRENCE REFORT REVISION

LER RO t \ E NT Y E A R REPORT NO. CODE TYPE P O.

@ gEg |217 j8 | |-| |0[0[6| y 0 |3 | ] g g22 23 24 . ti 21 ?d 2"J 30 31 32

ACTION FUTURE EFFECT SHUTDOWN ATT ACHM E N T N P R D-4 PRIVE COP /P. COYPONENT1AKEN ACTION ON PL ANT METHOD HOURS SUBVl1T E D FORM buis. SUPP LI E H MANUFACTURER

W h!F|@ |Al@ |A|h |0 18|0|0) (Jjh |d@ |A |@ [7d7 Idh1 73J s4 . Jo 3/ 40 41 4 43 44 47

_

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS

ej LFo11owin9 reae t ar s''nt do'n on 7-] 7.- 73 _aD iTLo.?.Ltic h b v it e ch t al Pe*;qr _.Cnn,nm, %n,._ j1

11 11| | and Georcia Power Comonnv perconnel revealed str,tifiention nf nie t r e,, o r , t o -n <- 4n I

i y | tha drvvell. Analvsis of the nroblems resulted in an ournee from 8-?O-78 to 0 1;-78 l

13 | a | ] as detailed in the attachmont. The attach'.cnt was in,dsortently loft off Revisin" T|

]t |41 [ and is beine transnitted as Revision ?7 8 9 80

FAC1LITY V E T54 DD OFSTATUS % POWE R OTHER ST ATUS CE OVEHY DISCOVERY DESCRIPTION

La_l@ lo lo lo l@L N/A | |C j@| Startup Testing |s s

S JTiv,Tv cob 1' '2 " '' ** '' So

AMOUNT 05 ACBVITY @ |nEtt AsEn c. HE LE CE LOC ATION OF HE LEASE

li le | I z I @ Iz I@ N/A | N/A _j7 8 9 10 11 44 4h 80

PE RSONNEL E xPCSuoESNUMB E R TYPE D E SCRI PTI ON

151711 o l o ol@lz @l N/A |7 8 9 11 17 13 80

PEi1 SONNE L INJU AIESNU*tBER DESCRLPTDON

|1 la | | 0 | 0 l 0 }@| N/A |"790215ot OSS Or OR D * AGE TO F ACILITY

1 vPE DE SCRIF T TON

E l 1 z Pl n/A 1v7 4 9 10 go

c.. u[n tSCneTic . @ NRc tiSE ONLY,

?|' | Y D| Prens Delonso on Aur 91, ! o 7 9 , ,, ,, n , ., i ., . , j y|||||| ||||}n.,-

' . e, r,3 aso ;7 a e w i

N A?/.E OF PFtE P AR E R . . Creene, Supt, of Mr Fng. SNON E: (017)- - ,.

Page 2: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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PLANT E. I. H ATCH UNIT IIPRIMARY CONTAINMENT C00 LINO MODICICATION

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During the heatup plateau of the Unit II Startuo Program it wasobserved that the average drywell air tencerature was exceeding the135 de g ree limit as specified in the Hatch Unit II TechnicalSpecifications. The Technical Specification violtion was firstobse"ved by Jeff Chumley, Georgia Power Test Engineer, while he wasperforming startup test HNP-2-10244, "Drywell Temperatures," on July20, 1978. The arithmetic average at th is time was dete" mined to he143 degrees F with the reactor at 160 psig and 370 degrees F.

To bring the drywell air te mp era tu re below the TechnicalSpecification limit, all of the standby Drywell Cooling Fans wereplaced in service. Within three hours the average drvwell temperaturehad been reduced to 132.5 degrees F, and in another 4 hours it haddropped to 124 degrees F.

The following morning, July 21, B ec h te l was notified of theproblem we were experiencing. Their mechanical design groun asked usto begin mon icoring d"vwell air temocratu"es on a regular basis whileexperimenting with various cooling and reutreulation fan alignnants.

Again, on July 23, the Technical Scoc i.'i en tion linit of 135degrees F was exceeded when reactor p"essu e was increased to 524psig. In an effo"t to derrease the drvwall temocrature, two of theReactor Building coolers were taken out of service to reduce the loadon the Reac tor Building chillers. This b"ought the te mo e"a tu re downto 131 degrees F. As reactor prersiae war ine" eared to 500 osig at480 '' .; rm .3 LL; d.c, _ te at e w. ; r *;d 3. .e g ees F.Standby Gas Treatment and the Dryuell Purge Fan were placed inservice, as reac tor pressure was lowered, t r. order to help reduce thedrywell temperatures.

Bill Papproth of Bechtel arrived on site July 24 to analyse theDrywell Cooling System.

On July 26, management decided to bring the reactor to coldshutdown to allow Bechtel to enter the drywell for an inspection ofthe Drywell Cooling System.

Bech te l re o re sen ta t ive s and Georgia Power Company engineers andmaintenance personnel entered the drywell of July 27 to begin theirinspection. They found the rupture discs missine, f"on the s a c r i f '. c i a lshield which allowed the a i r, designed to flow in the annulus betweensacrificial chield and the reac tor insulation, to escace. They alsodiscovered that the annulus was less than one inch wide where designhad specified 3 inches, thus cutting down on the area for air flowfron the Drvwell Cooling System. See Figure 1 for schematic of theD.' y we ll Cooling Syste m.

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Page 3: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Bechtel direc ted that several runs of temporary ducting heinstalled to redistribute the cool air at the bottom of the drywell tothe hotter upper regions and duct the hotter air from the top of thedrywell to the larger capacity coolers at the bottom.

Following the installation o r the rupture discs and the tanooraryduct work per temporary DCR 78-212 the reactor was again haoughtcritical on July 29. The reac tor was brought to 165 psig on July 10*

and eleven hours later the drvwell temperature exceeded 135 degrees F.

Reac tor shutdown began immediately to allow Bech te l to do further woakin the drywell.

From July 31 to August 3, under Bech te l 's d irec tion the following

changes were made:

(1) Reversed the d i re c,ti on of air flow of 2T47-C002 A and B to forcecore air up through the annulus area per temporary DCR 78-223

(2) Installed two thermocouples in the aia gap between the sacrificial. shield and reactor insulation, two thermocouples on reactoa

-insulation and relocated te mp era tu re elements 2T47-N002, 2T47-N010and 2T47-N001K per temporary DCR 78-232.

(3) In s t a ll e d te mp ora ry 24 inch du c two rk from fan 2T47-C001A to inletof fans 2T47-B008 A&B and replaced existing suction ductwork for2T47-C001 A with flexible du c twork per temporary DCR 78-?30.

(4) Scaled off CRD cavity a.ea by the instal't.' c.) of a docr at theCRD cavity entrance to allow cavity area to b e p re r~ aized to help

in the noving of air up through the a n nu lu s, area per temporary DCRS .

.

(5) Installed wedges between the sacrificial shield and reactorinsulation to increase the air gap of the annulus to increase air -

fl ow.

(6) Inspec ted reac tor insulation for oroper installation.

(7) Reduced chilled water flow to the lower drywell cooling units,2T47-8008 A &B and 2T47-B009 A&B, to increase ' low to uppea

cooling units, 2T47-B007 A&B.

(8) Carl Sox of Environmental Balance Corocration rebalanced drvwellcooling fans air flow per Bechtel's instructions.

Reac tor was. irought to 500 psig and 470 der-ces F on Augu st 4 to*

evaluate the Drywell Cooling System. Drvwall average airte mp era ture again exceeded 135 degreen F approx'natelv '? hours

after the reactor went critical. Reactor was again brought tocold shu tdown, on Augu s t 5, for additional changes.

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Page 4: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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'The following changes were made under Bechtel's instructions onAugust 5 and 6:

(1) Blade pitch on fans 2T47-B007 A&B were inc rea sed , to increase airflow through t'h e s e units by approximately 50%, per TER 78-6.

(?) The supply duc ts to the CRD cavity f rom 2T47-B008 A&B and2T47-B009 A& B were blanked off to direct more air up through theannulus and up to the hotter upper regions of the drywell per TER78-6.

(3) A sheet metal ring wa s intalled around the reac tor skirt toisolate the annulus from CRD cavity area per TER 78-6.

(4) Existing te mp ora ry fl e xib le duc t wa s removed from 2T47-C001A andreplaced with a temporary sheet metal suction bell. 2T47-C001Bwas also fitted wiqh suc tion bell per TER 78-6,

(5) The 2T23 instrumentation in drywell was put back in service toprovide add it iona l te mp era tu re readings.

On Augu s t 7, reactor was brought to 575 psig and 485 degrees F forevaluation of changes made in drvuell thus far. Drywell temperatureexceeded 135 degrees F about 30 hours after reaching 575 psig. Thereac tor pressure was then reduced to 400 psig on August 9 to maintaindryvell temperature at approximately 130 degrees F, while managementwas waiting word from URC for a Techincal Specification change which"ould allow use of a volumetricly weighted formula for computingaverage drywell air te=perature.

Due to a problem with tbc drywell tn toru: vacuum brefeers thecacto. .s 'roup , L, c. s i d snu do on ps- .1.o

While the reac tor was down the following additional changes weremade per TER 78-8:

(1) The bottom of the reac tor vessel insulation was flashed so thatair could not flow between reacto" vessel and insulation whichcould cause higher heat transfer from the reactoa vessel to thedrywell thus placing a greater load on the Drywell Cooling System.

(2) The reac tor st a b ili z er covers were removed in hopes of inc reasingair fl ow in the annulus area.

(3) The reac tor /dy rwe ll bellows wa s insulated to dec rea se the amountof heat flux from reacton vessel to drywell air.

(4 ) Temporary te mp era tu re elements were installed by request ofTransco, R?V insulation supplier, to evaluate insulation and toestimate heat load.

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Page 5: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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(5)'The annulus between the sacrificial shield wall and the RPVinsulation was checked for debris which might have blocked airfl ow . S ev e ra l i t e ms , including a welder's b rush and miscellaneoustrash, were found in the air space and removed.

(6) Aia fl ow read ings were taken to determine air flow being suopitedto annulus and amount leaving a n nu lu s at the top of thesacrificial shield. It was found that 13,500 c fm wa s beingsupplied to the annulus but only approximately 690 cfm exhaustingat the top, which showed a substantial amount of air leakage fromthe annulus through the sacrificial shield penetrations.

Following the completion of the items above, the reac to r wasbroght critical on August 14, after being down for three days. Alsoon August 14, Max Manary, Plant Manager, received wond from'the NRCthat the volumetric weighting for drywell temperature averaging wasa c c e p ta b.l e .

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on Augu s t 16, 32 hours after going critical and at 1005 psig, thedrywell temperature reached 134.7 degrees F and all the standbycooling fans had to be started to reduce drvwell te mpera te e . Reactorpressure was reduced to 940 psig and drywell cooling r e tu rn e d tonormal c on fi gu ra ti on . At this lower p re ssu re the d rywe ll wasmaintained at 132 degrees F.

Plant management decided on August 19, to bring the reac tor tocold shu tdown to allow construction to enter the drywell and makepermanent mod ifi ca tions to the "rywell Cooling S ystem. The reactorwas in cold shetdown on Augus t 20, and all startap test i _or HatchUn it II was discontinued until the c omp le ti on of the Drywell CoolingModifinrtion Outage.

DRYMELL COOLING OUTAGyAugust 20 to September 15

To best describe the outage and what was done, a before and afterlook at the Drywell Cooling System design will be presented here,which will encompass all work done to the system per DCR 78-270.

ORIGIMAL DRYUELL COOLING DESIGN_

Fi gu re 1 shows the original Drywell Cooling System designs chem a t ic a ll y . The original fan line up was to have the followingfans running: 2T 47-2007 A, 2T47-9003A, 2T47-B009A, 2T47-C001A,2T47-C002A and 2T4 7-C00 2B with the other four fans in standby. Withthis line up, 4000 cfm was bein6 supplied to the CRD cavity area by2T47-B00SA and 2T47-B009A, 4000 cfm was being exhaust the CRD cavityarea by rec ircu la t i on fans 2T47-C002A and 2T47-C0023. Fans 2T47-B008Aand 2T47-B009A were also to supply a total of 8000 cfm to the annularspace between the cacrificial shield and the reactor vesselinsulation. Th i s 8000 cfm was to travel up the annulus picking up

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.amassme es. O C__-we I

Page 6: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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heat lost from the RPV insulation, thus reducing sacrificial shieldtemperature, until it reached the top of the sacrificial shield whereit would exit into the uoper drywell region at elevation 185'. Theremaining 38,000 era supplied by 2T4 7-B008 A an d 2T47-B009A wasd irec ted at other loations o f drywell between the 130' and 158'elevations. Air movement between elevations 158' and 185' was to beby natural circulation. In the upoer elevation of the drywell,2T47-B007 A supplied 5000 cfm through a ring header in the drywell domeand 1000 c fm into the d rywe ll below the bellows at elevation 200'.Recirculation fan - C001A removed 5000 cfm from the drywell domethrough a single inlet and 1000 cfm from below the bellows atelevation 200' and d is charged the total 6000 cfm down the drywell atelevation 182' just below the - B007A intake. The four standby fanswere only to come on i t' an operating fan failed or if the air

area exceed 148 degrees F.temperature in the CRD c a v i,t y

Chilled water flows to the fans were as follows:.

B007A - 53 gpaB008A - 213 gpaB009A - 211 gomTotal - 479 gpm

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The chilled water is s up p li e d by the Rea c tor Building chillerswhich also supplies the Reactor Building and Radwaste Building areacoolers. The duc twor k in the drywell was fabricated from ASTM A 167,stainless steel sheet, Type 304, No. 2D finish.

.REVi3ED DRYWELL COOLING DESI.GN----- - - - _

As a ro s -' t * t"e ' n'rimen in and d a '- a'r ly - : *s' en "'v'

20, 19/b anc August 20, a final cesign was formulated by Becatel unacwould optimise the Dr v we ll Cooling System with the least amount ofdown time for the reactor. A reactor outage was necessary due to highte mp eaa tu re and radiation levels in the drvuell and the length of timeneeded to do the work. Also the northeast drywell hatch plug had tobe removed to allow the transfer of eculoment and materials in and outof the drywell. A 28 day outage was aporoved by Georgia Power Companymanagement to implement design change 78-270.

Fiqure 2 shows the resulting Drywell Cooling System design. Thepresent fan line un is : 2T47-B007A, 2Tu7-B007B, 2T47-8008 A ,2T47-B009A, 2Th7-C001A, 2T 4 7- C 0 01 B , 2T47-C002A, and 2T4 7-C00 2B runningwith 2T47-B0083 and 2T47-B009B in standbv. The only logic change-

needed to accomplish this was to remove the interlock between2T 47- B007 A and 2T47-B007B which p rev en ted both fans from runningsimultaneously.

All of the te mp ora ry duc twork , installed during the previous shortoutages, was removed from the drywell before the actual installationof the mod ifi ed ductwork began.

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Page 7: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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A ring header extending 90 de g ree s around the devuell. from east tosouth was tied into the existing d is cha rge duct of B007A as seen inFigure 3 This ring header delivers 6500 cfm to the upper drywellthrough two outlets as seen in Figure 4.

Fan 2T47-B007 A also delivers 1500 cfm to the ring header in thedrywell done. (The resister which previously d e live re d 1000 cfm, justbelow the bellows, wa s closed). The rated ca p ac it y of "ans 2T47-3007A&B is now 8000 cfm due to the change in pitch of the blades madeAugust 5 and 6, per TER 78-6. Fan 2T47-B007B wa s modified in asimilar manner as 2T47-B007 A with the same air flows.

The most extensively changed po" tion of the D"ywell Cooling Systemwas t! e upper recirculation fans 2T4 7-C 001 A an d B . The existing 7.5hp fans were removed and reBlaced with 30 hp 12,000 cfm capacity-

fans. The two Joy Fans. pu rcha sed were r e c e iv e d with 480 volt motorsand 4 blade rotors. The motors were removed and sent to Reliance (themanufacturer) to be rewound f or 600 volt duty. The 4 blade rotor wasnot sufficient to produce the desi"ed pe"formance cu"ve, so the twelve

~blades were removed from the o"iginal 2T47-C001 A& B fans and installedon th'e new rotors. 'Jh e n the rewound motors were back on site, thefans were reassembled and mounted on test stands in the maintenanceshop to be balanced under the direc tion of a Jov Manu f ac turins Companyrepresentative. After the success ful completion of fan t alancing, thetwo new fans were installed where the original fans had been removedat elevation 185. New cable and conduit was also recuired due to thelarger motors. The duc twork for 2Th7-C001 A&B was completelvredesigned. The new design included two 2 4" discharge ducts, seeFi gu re 5 one each from the ran ou tle ts at elevation 185' down toelevation 128' sea F"-urn 6 (ty''ca' of bot' "ams'. The Fuct'ond u c . .t e r . was a eo moc..ted tr._ sactio.i j.-- selow the sulknead at;

elevation 203' r2ther than from the drywell done area. The intent of.these changea was to move as much of the hot air from the top of thedrywell down to the lower levels where the higher capacity coolingunits were.

.

Two additional 24" supcly ducts were addeo, one each from2T47-B003A and 2T47-B009A, see Figure 7 an d 8, to supply 6000 cfn eachto the middle elevations of the d rywe ll , see Figure 9. The supplyducts to the CRD cavity were left blanked of f per TER 78-6.

The lower recirculation fans 2T47-C002 A&B were le f t with theirflow direc ted into the CRD area per DCR 78-223.

Following the completion o f duc twork and fan installation, CarlSox of Env i ron m en tal Balance Corporation rebalanced the DrywellCooling System per the new PPD issued by B ech te l.

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Page 8: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Other changes made included the ins t a ll a t ion o f re flec tor shieldson RTD's that were in areas of high heat radiation so that a moreS accura te air te mp era ture could be recorded. The RTD's which had thereflec tor shields 1nstalled where 2T 4 7-N 002, 2T4 7-N 0 0 3, 2T4 7-N 0 09,2T47-N010, 2T47-N014 and 2 T 47- N015 . In addition to the shields,temperature elenents 2 T 4 7-N 0 0 2, 2T4 7-N010, 2T 4 7- N014 and 2T4 7-N015were relocated approximately one foot farthen away from the vesselinto the air stream. From the data recorded by TER 78-8 concerningthe annulus air gao air flow, it was found that most of the coolingair being supplied to the annulus was being lost around thepene tra tion s th-ough the in service inspec tion doors. To alleviatethis problem, neoprene gasket material and flashing was installed onthe following doons: '2B11-N2A through 2B11-N2H, 2 B 11 -N 2J , 2B11-N2K,2B11-NB A an d 2B11-NSB. The CRD cavity door added by DCR 78-231 wasfi t t e d with hinnes so that entrance into the area would be lessdifficult. The stabilizer covers removed by TER 78-8 were reinstalledper original design. The wedges b etween the sacrificial shield andreactor insulation were left in place to maintain the needed air g'ap.The increased chilled water flow to 2T47-B007 A&B was left as balancedon August 3 The flashing around the reactor skirt and at the bottono f the reac tor insulation as we ll as the bellows insulation was leftas installed per TER 78-6 and 8. Two additional fans, designated as2T47-C0u A&B, were to be added into the new 23" supply ducts f"on2T47-B008 A and 2T47-B009A, however d e l i v e ry was such that installationdu ring the 28 day ou tage wa s not poscible. New cables were pulled outside the drywell in anticipation- of their arrival and need. Bechtelhas determined f"om data taken during o 1. a n t operation, since theou tag e , that these fans will not bc 2 svined.

The ou tag e lasted 26 days, two da? s less than scheduled. The.gt w'a' v y acor' Sly c. ,5 c ; u- to tb , serat' a '34e'

Generation Departnent Outage Coordinators and. Maintenance Deoartment,Construction Department and their contractors, and the on s w e Bechtelrepresentatives.

At p re sen t , the mod ified Drywell Cooling System is maintaining theaverage temperature between 128 degrees F and 130 degrees F at ratedte mp era t u re and p re ss u re .

See Attachment I for c or. lusions d ra wn by B ech tel regardingexisting system performance a .i d future changes required.

.

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Page 9: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Page 10: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Page 11: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Page 12: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Page 13: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

. . . . , . . .. , .. ... ,s, mm.., .. . . r- - -

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Beci tel Power Corporation-.

.-15740 Shyfy Grove Road *

-r.I::.

Gaithersburg, f.laryland 20700 --.

W, j'

301-D.sB 27Co- ' ' *

_

.

October 6,1978 --.,

~' .

Mr. M. Manry '?-.

. -.

Ccorgia Power Company,

. .*

Production Department - -

* 'P.O. Box 442 *- *

. Bax1cy, Georgia 31513 '-

.

--. sy, , . ., . ,

-.

, _

Dear Mr. Manry: *-:- - . ~-. -

. . , ~ .. -

~ -

E. I. Hatch : uclear Plant Unit 2 # - ''

Bechtel Job 6511-020 ~ - ~

Dryuell Coolin; Systen Modifications' '

'-

,-

and Post-Xcdificctica Testing,

File: A-29. 3/ S S -2102 -160/ S S -2115 -2/ B -GP -5899._

.

As you are aware, subsequent to accenpliching the drywell cooling systenductuork modifications, the air handlin:; equip = cat was balanced by.-

-Envircer.catal Salance Corporation. We have reviewed the data supplied.

" ~by Environ =catal 3 lance, and find the syste a balance reported, to beacceptchla. -

Also, we have reviewed the dry rell temperature data acquired during-.

the post-codificatica testing period and we draw the follcuing~

.

. - conclusions;.

*

- . .

. ' -.

.

'Addition:1 codification will be required, during the first -

A.refueling cutage, fer the ductuerk above the reactor well, ,

bulkhecd, to enh:nce air distribution in the volume over ,',,

. the RPV head (see attached sketch) and,i B. In order to regain ccolcr redundancy, the RP7 insulation syste:n

probicas cust be corrected, at 1 cast for the insulation above the- top of the sacrificial shield s.all. (i.e. - above el. 183'0")

Refer to probicas report ettcched, fer more informat ion.Enclosed is a su=ary report of the Dryucil Cooling System Prob 1c=s.-

'

If 90 tn'ay, be of service in the future, picace advisc., -

;.

Very truly yours

U bM~AAf |-

< ...

' ' ' 'T. J. Mcdonald- MSD:WJP: din Project Engineer, .

Enclosure *'

,' cc: V. C. Valekis, w/cncl. '

W. A. Widner , w/ ene L. . . . . . . . . . . - . . . . - . - . . . . - - . - . - - - -

(.. J. R. Jordan, w/cncl.,

H. H. Gregory, III, w/cncl. ',.

.

.

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g . e. .m-

_,_ , _,pe e.e , *Wo. W - F**'W -8 - "'

Page 14: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Page 15: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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ED*JI: I. H.iTCHS:t CTI.in p Li!.--[

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CEO2CI.i P& #1 CO""A:!' ,'

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DRY'..?.LL COOLI::C SYST" pROBLE''S.

> -

Back?round:.

....

, I.}.,l - On July 19 and 20,197S, Georgia Power Co pany informed Bechtel-Gaithersburgthat they were experiencing difficulty with the drywell cooling systca, asystca.which Zechtcl-Gaithersburg had designed and provided. Specifically,the system could not be operated in a fashica which would maintain anaverage contai=ent dryuell air tenperature of 1350F or less, as recuiredby the plant technical specifications. On Sunday, July 23, 197S, a teamof engineers was dispatched to the plant site to evaluate system per-formance.

.

Descrintien o f the S es ter - ~

The drywell cooling system for $'!P-2 is a chill water-to ai.r.. coolingsystem with a design of approximately 415 tons (~ 5 x 10 */F.r) of heat-

.

'. removal capacity. The systen (shown sche =ctically on Bechtel Drawin; ~'

11-26074) utilizes three (3) no=21 operating air-to-chill water coolersand three (3) nor=al operating air circulating fans.

As provided, the system represents a co=prc=ise with consideratiens ~,

given to equipment space availability n'nd optinun system perfor=ance...

In order to provide proper air roverent and cooling, the system relics i

on the principle that hot, or heated air rises and cold, or cooler airdescends. Design paraccters for the sacrificial shield inside diancterend the RPV insulatica outside dic .eter were specified to provide a 3 :.nchairjap for ventilatica cooling air flow frc= botte= to top. Based on an80 tU/lir. heat loss frca the insulation surface, and with 8000 Cfm cooling

, air at 75 F entering the base of the sacrificial shield, it van esti.atedt. hat the air exit temperature to the upper drywell area would have beenapproxi :ely 1100F (plus or minus 100F).

-

Itcated air uithin the upper drywell was at icipated to cix with the exitingair frem the sacrificial shield annulus, and be cooled and exhausted by theair handling equipment provided. The vole- c above the reacter well floor, '

confined by the drywell head, was to be cooled by rupplying 75 F supply-

air to the region, and then exhausted to the annulus created by the con-centric configuration of the sacrificial shield and the cylindrical portionof the drywell.

.

9

. '

E

.

.

.

%

''''.2 .. . . :. . .- .. .

- . . . - : ~ ~ ~~- n -_ _ _ _ _ _ _ . _ . _

.

Page 16: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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s -

Drywell Cooling Systc= Proble=sPage Two

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The large volu=c vithin the spherical section of the drywell, as well as.the CRD cavity uithin the RPV pedestal are served by two chill water

cooling units which provide cooled air at a design tc=perature of75 F to the base of the sacrificial shicid, the upper CRD cavity andthe elevation 127' and 150' (MSL) vole =es.

Disetission of the Problers Encountered:.

Upon arrival at the jobsite, and for a period of approximately 60 hours,an evaluation of syste= performance was conducted with the followingfindings:--

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Cooling Units 2T47-E007A and 2T47-E0073, located in the drywell- n.

upper volene (elevation 185' 0") were operating si=ultaneously,with a heat removal duty of approximately 1.1 nillica ETU/HR(almost twice the design sp2cified capacity) per unit.

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Cooling Units 2T47-3003A and 2T47-3009A, located in the drywellspherical vole =c (elevatien 127') were operating at a he2t

. rc= oval duty of approxi=arely 660 thousand 3TU/ER lonly about*

30 percent of the design specified capacity) per unit.I.

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Peak dryvell te=perarures were recorded as high as 250 F (near Ic.

the reacter well bellows, el. 200') and sinultaneously as low- as 80 F (in the CED Cavity). ,

On July 26, 1978, the unit was placed in a shutdown and cooled down.

condition, uith the follouing course of action:. .

,' 1. Provide a supply air header for . cooling. unit 2T47-3007A, to belocated atn- clevaticn 193', i==ediately below the reactor wellbulkhead.

2. Provide discharge duct for circulating fan 2T47-C0013, to allowfan discharge to cooler suctions for cooling units 2T47-3009Aand/or 2T47-LC093. (1-24" Elephant Trunk)

3. Elininate exhaust air ductin; for fan 2T47-CC013 above elevation190', to allow evacuation of the volu=e i==ediately below the'

reactor well bulkhead.

4. Pr' ovide 4000 c f= of supply air to drywell elevation 175', 'tcprovide cooling air injection at the main stea= line chase vole =c.(2-16" Elephant Trunks)'

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Page 17: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Dryvell Cooling System Problems'Page Three

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During the period of plant downtine to effect the above codificaticas, an Iinspectica of the drywell revealed thattwo closure devices at the baseof the sacrificial shield had been c=itted during plant construction.The caission of the closure devices (Rupture Discs 2TL7-D001 A and 3)

resulted in the annulus ecoling air bypassing the annulus and "short g

circuited" a cooling air flow of 8000 cf=, intended to be provided to .

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the upper drywell voluna. Additionally, the inspectica revealed that j

the specified cooling air gas of 3", between the RPV insulatica and thesacrificini shield had not been u.aintained, and the actual gap thickr.ess ',was found to be non-unifera and varying frca 0" in sc e locations to %"in others._ (This is due to the sacrificial shield not being plumb and,

.-_ also due to insulation not being installed as shown on engineering dwgs.) .in an effort '

to assess the ramifications of the lack of cooling air for the,

sacrificial shield, Civil and Nuclear Engineers at Gaithersburg were con-suited.It was de crnined that the concrete within the sacrificial shie'dvall does not contribute te the stability of the structure, but is pro-

vided to shield che dryvell cc ponents frca the nucicar radiation emittedfrom the reactor core during picnt operation.-

' The temperature of the-

outer surface of the sacrificial shield will be monitored and theresulting data will be used to calculate concrete te=peratures withinthe shield. Then the adecuacy of the concrete with respect to neutrcashielding can be evaluated.

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k It was also noted that the RPV flange be110ws was uninsulated and as-

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such conservatively trcnsnits core than 100,0C0 STU/Hr..

to ambient. GPCagreed to insulate this shicid.

During the evalttatica of the shield, it was also determined tFat nerercusholes had been provided in the RFV pedestal by the ccatainment

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These holes, or porta were provided to allcw access to the vessel skirtcrector.

hold-down bolting during vessel seating and torquing. These ports previdea path for air ficw to and frem the annulus and CRD Cavity.,

A review ofthe drywell cooling systen design has revealed that these ports were notconsidered during the design phase, and nay have centributed to poor-

sys te_t performance had th7 previously centioned deficiencies not occurred.

In addition to the =cdifications above, Cecrgia Power Cenpany ConstructicaManagement effected the installation of rupture discs. 2T47-DOOl A and B.

To11owing the above repairs and modifications,.the unit rest cd startup -

testing, and the Ecchtel engineering team proceeded to evaluate the ,effectiveness of the system modifications.

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On July 30, 1973, with reactor ccolant temperature at 4cS F, the averagedrywell temperature was ec=puted to be 135.2 F, and plant managementdecided to terminate the test program for additional modificatien.

The following additional modifications were effected:1. Reverse the flow direction for fans 2T47-C002A and B, so that

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cooled air may be exhausted fres elevation 118' 0" and pumped.

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Page 18: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

' D 11 L 1 6 oy a .m P.oble=, '' ' ' ' ' ' ' 6 d - Pu l J. (> . k- o\ luPage Four-

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to the CRD Cavity, to provide pressurizaticn of the RPV pedestaland, via the hand-holes, the sacrificial shield annulus.

n. _ . - ..---2. Provide a closure for the louer CRD Cavity access, to allow

pressur-ication of the ce=partment via fans 2T47-CC02 A and 3, ias mentioned above. '

i!3. Provide discharge ducting and codify the suction duct network i

for fan 2T47-C001A, as previously described for fan 2T47-CC013. !

i4. Evaluate volume flow rates for cooling systes units 2T47-CC01A,

C0013, 3007A, 20033, and 30093. j

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*With the advice of North Erothers, Inc. and Georgia Power Cc=pany iConstruction, open the RPV insulation-to-shield wall gap I

to the maxi =ca possibic vidth.

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6. Measure air gap flous.

Prior to resu=ing plant testing, the total volume flow rates for thevarious paths era cuantified as follows:

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a. Frcm 2T47-3003A/3 to clevation 179' (MSL) ,1600 cubic feetper minute. (Through a 16" elephant trunk)

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b. From 2T47-3003A/3 to the R?V insulation-to +ield wall airgap, 7,500 cubic feat per ninute.

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c. Frca 2T47-3009A/3 to elevatica 179' (MSL) ,1300 cubic f:ct.

per ninute (Throu;h a 16" elephant trunk)

'd. From 2T47-3009A/B to the RFV.insulatien-to-shield wall air "

gap, 6,000 cubic feet per minute.,

c. Froa 2T47-C001A to Coolin; Unit 2T47-30033, 3,400 cubic fcerper minute. (Thrcugh a 24" elephant trunk)

f. From 2T47-C0013 to Ccoling Unit 2T47-30093, 3,000 cubic feet_ per minute. (Through a 24" elephant trunk)

g. RPV insulation-to-shield wall gap discharge, 1,200 cubic feetper ninute.

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Resuming' plant heatup cn August 3, 1973, we found dryvell averagetemperature.again cr.cceding 135 ?, and in an atte=pt to corrcet the -apparent heating probica Bechtc1 suggested reducing air flow to the RPVinsuistion-to-shield wall pap by closing first two volume dampers and

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then isolating the air gap completely. The intent was to reduce airIcakage to annulus between RPV and insulation. The effcet was not noticcabic.-

Stopping circulating fans 2T47-C002A and B proved to have no effect onreducing the average drywell te=perature; however, the reduction of CR3Cavity pressurizing air also had no effect on CRD Cavity temperature.* ~

. On August 4, 1973, the plant was again shutdown for further ventilation,

modifi. cations..

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Page 19: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Drywell cooling System ProblemsPage Ftvc

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i:.....-.. . . Through the period August 5 through August 7, 1973, the followingmodifications were e f fected:

1. Supply air ducts to the CRD Cavity were closed with in-ductblanking gaskets.

2. Construction debrid was removed frem the RPV insulatien-to-.

shield wall air gap, to the extent possible.

3. Discharge ducting fre circulating fan 2T47-C001A was re-connected to the fan discharge flange.

4. Suction ducting for fans 2T47-C001 A and B, including suctionbells, were fabricEted and installed, to allow exhausting airfrca the refueling bellous.

5. RPV pedestal bolting rin; holes were covered to providepressurication of the RPV insulation-to-shield wall air sap.

- -~ 6. Insulatica was installed en the RPV refueling bellows.

7. Obvious openings in the RPV insulation can were closed wi asheet metal plates.

''' '8. Tc=perature cic enes 2T47-TI-N002, N014 and UO15 were relocated

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away frc= the shield wall.-

9. Temperature cle=2nts 2T47-TE-5014, 3015, N003 and n009 wereshielded frc= the unpainted shield t'11. *

. 10. Ther=occuples were installed to monitor the following locations:.

RPV insulation-to-shield wall air gap temperature ata.. cicvations 145 and 190 -

b. Shield trail interior temperature at clevation 190 and 145

Insulation surface tc=perature at elevation 190 and 145,c.

interior and exterior.

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d. Inservice Incpection gap tc=perature at elevation 190 and 145s. -

c. 1 Shield wall exterior temperatures at elevations 160, 170,and 180, and ,

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f. RPV refueling bellows surface temperature..

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Page 20: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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Dryvell Cooling Systen Probicas ..

Page Six '

Resening plant testing cperations on August 7, 197S, in lieu of utilizingan arithmetic averanc temperature, a chan;c to plant technical specifications""~~~ ~~'-

allowed volumetric weighting of the dryuell air temperatures. Althoughthe peak tenperatures within the containment were greater than desired,the average drvrall temper 2ture uns calculated to be less than 135 ? .

(i.e.,133 F) with a reactor coolant temperature of 545 F (rated) .

On August 21, 1973, plant operations were curtailed to allowinstallation of pern:nent duct.rar% and modifications or nsulationand instrumentation. The follouing work was acec=pli . u:

1. Sixteca (16) gau;c, 24 inch nc=inal dia=eter stainicss steel,,

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ductwork was installed to provide;

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Air distribution-to elevation 175'0" (MSL) frca coolinga.units 2T47-B005 A (3) and 2T47-3009 A (3) and,

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b. Heated air transport frca clevation 200'0" (MSL) toclevatica 120'0" (MSL) via circulating f ans 2T47-C001 A & 3.

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2. Twenty-two (22) irch nominal dia=cter ductwork was also addedto cooling units 2T47-3007 A and 3 to provide coolcl air

distributica at elevatica 190'0" (MSL).

3. Circulating fans 2T47-C001 A and 3, cri;inally specified asJoy Manufacturin,Co. Medcl 23-17.5-1750, were replaced -

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vith Model 23-17.5-3500, accuired frca Philadelphia Electric-

Company's Linarick station. This "as accc=plished to providean increase in enhaust air ficw rate, frea c,000 cfa to 12,000

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4. Fan blades in cooling units 2T47-3C07A And 3 were adjusted toprovide a ncainal air volume flow late of 5,000 cf= per unit.

5. In un effort to reduce the convecticn heat transfer uithin theinservice inspection volume bounded by the EFV insulation and

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the RTV shell, North Erethers, Inc. applied stainicss steelflashings at insulation penet:::icas fer no les NSA and 3,UllA and 3, N12A and B, and F.6A and 3.

6. To reduce the chic 1d wall to RPV insulatica annulus coolin;

'nir bypass flo , inservice inspection door penetrations sealf1' ashing was installed at doors USA and 3 and 32A,B,C,D,E F',

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C,ll,.1, and K. .

7. To enhance air ter.perature samplina, RTD's 2T47-TE-3002,-

N010, 5014, and NOIS were relccated and reficctive shicidcans were installed on RTD's 2T47-TE-3003, M009, and thea fo rc=ent ioned , to reduce and/or clininate radiant heat gainof the sensor probe.

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Page 21: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

[~ A T T AC_ M bA \- N ~I _ p.| o I,

. Drywell Cooling System problems *

Page Seven:

Following the post-modification balancin; of the drywell cooling systca,, , ,

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the plant was returned to start-up testing operation. As of this date,(October 2, 1973)., the unit has achieved 207 thermal power and averagedrywell tc peratures have t/pically not exceeded 1270F. Peak contain-

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ment temperaturas below the reacter uell bulkhcad is as 167'F, in thevicinity of elevation 203'0" (MSL). The containment te=peraturesarc distributed as falluss: :

Elevation ("SL) Avera?e Tencerature (OF)

190'0" 143 (average of 3 RTD's).. 175'0" 126.5 (average of 2 RID's)

158'0" -152.3 (average of 3 RTD's)130'0" 126 (average of 8 RTD's)

Pre-modification contain=ent te=perateres were distributed as follows:

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Elevatien (MSL) Averare Tercerature (o~.

190' 175.7 (average of a RTD's)175' 152.5 (average of 2 RTD's)158' 146.3 (average of 3 RTD's)130' I 106.75 (average of 8 RTD's)

- And, containment peak tempercture prior to the nodifications wasrecorded as high as 2550s.

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Due to the difficulties associated with accurately esti=ating the,

interior surface tcuperature of the shield uall and thus deterningsacrificial shield ccacrete te=peratures, Georgia Power Co:pany has

- agreed to install (ca both the cuter & inner surface of the sacrificialchicid) te porary ther:occuplas in the vicinity of the "16A and E dcors.Data provided by thase ther=occuples will allow an accurate deterninationof shield wall ccncrete tc peratures. Esti=ates to date indicate

4 concrete to ben 200 F, below c1cvation 175'0".

To regain redundancy in the upper drywell volume cooling units (2T47-E007 A and B) the cenvection currents within the inservice inspecticaannulus rust be cli=inated/ reduced. As previously stated, thase {convection currents result in failure of the RFV insulation to perform i

its intended function, thus causing excessive heat transfer to theupper drywell. Transco, Inc., the insulatica supplier, has stated thatit is possibic to do at 1 cast two things, in the interest of reducit.g '

vessel heat loss. These are: -

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1. Add a convection air break (i.e. , baffic) at, or near the,

top of the sacrificial shield wall within the inservice.

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Page 22: Update Repo{[CEd!!n1YlNeitMtFont COfJTROL BLOCK: | |h · obse"ved by Jeff Chumley, Georgia Power Test Engineer, while he was performing startup test HNP-2-10244, "Drywell Temperatures,"

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,Dryucil Coolin; System P. - .,

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inspection annulus, or

2. Eli.inate the intervice inspection annulus above the sacrificial* shield wall cud apply the vessel insulation directly to the

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