unexpected rotordynamic instability in a ...unexpected rotordynamic instability in a...

10
UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Sf Engineer Conoco, Inc. Wesake, Louisiana Ed Wilcox is a Senior Staff gineer with Conoco, Inc., in Westla, Louisiana, where he is the Reliability Engineer for cel- Paralubes, a joint venture beeen Conoco and Pennzoil. He also provides technical support for the adjacent Conoco Refine. His responsibilities include maintenance, troubleshooting, and specification of rotating equipment. Mr. lcox received his B.S.M.E. degree fm the University of Missouri-Rolla and M.S.M.E. degree from Oklahoma State Universi He is also doing post graduate work at the Georgia Institute of Technology in the areas of machine vibration, lubrication, and rotordynamics. He is a bration stitute certed Level I btion ecialist and a registered Pfessional Engineer in the Ste of Oklahoma. ABSTRACT The cause and ects of a large subsynchronous vibration (3.5 mils at 3490 cpm) in an FCC wet gas compressor are examined. The compressor is driven at 7850 rpm by a 6000 hp electric motor, through a speed-increasing geox, and compresses hydrocbon gases om 20 psig to 235 psig. A rotordync analysis of the compressor determined that even though the compressor had a long histo (approximately 25 yes) of smooth operation (overall amplitudes less than 0.5 mils), it had a ve low margin of stability. This lack of stability was caused by a high being to shaſt stiess ratio as well as destabilizing rces in the balance piston and shaſt seals. The pressure dam bearing design is not destabilizing to the rotor system because the joual is very heavily loaded; however, the high direct stiess that is produced reduces the ective damping of the system. Labyrinth and oil seals are usually not considered to have large effects on a compressor with such low pressures. However, the atmospheric side of the oil seal was determined to contribute the largest destabilizing effect. The effective length to diameter (L) ratio of the oil seal was reduced by 50 percent to lower the amount of cross-coupled stiess e seal produces. This modification reduced the subsynchronous vibration from 3.5 mils to 0.1 mils. The rotordynarni c analysis also identified other modifications to the being and balance piston design that should be made to increase the rotor's mgin of stability. Both steady-state and transient spectral vibration data e provided before and aſter the oil seal modification to validate the rotordync model of the compressor. INTRODUCTION The compressor was first commissioned in 1971 and had a history of very low vibration levels ( < 1.0 mil). It is a straight through, horizontal split machine that operates at 7850 rpm. It has two sections, wi three impellers in the first section and four in the second (Figure 1). It was rerated ree times between 1973 and 1992, but none of the rerates involved astic design changes (i.e., 4 1 smaller impellers were installed, speed decreased 200 m, three impellers were redesigned). The compressor operates at relatively low pressures with suction and dischge equal to 20 psia and 235 psia, respectively. The molecul weight of the gas varies om approximately 35 to 45. 6000 hp 1750m 4.49 Ratio ' gu 1. FCC t Gas Coressor 2 Section Strght through 7850rpm The compressor was originally installed with pressure dam bengs. The bearing ective L was decreased during the second rerate because the rotor weight decreased slightly and it was believed that the OEM wanted to maintain the same bearing loading/eccentcity to prevent instability. The OEM recommended changing to spherically seated tilt-pad beings dung the last rerate; however, the user decided not to make the change due to historically low vibration levels. The unbalance response analysis conducted before the last rerate did not include any oil seal effects (only aerodynamic). did show a ve high amplification factor, approximately 18. On September 26, 1997, over five yes aſter the last rerate, the compressor shut down due to an electcal power outage. A few days aſter the compressor was restted, the compressor outboard bearing vibration increased to 2.5 mils. The largest amplitude was at approximately 0.4x to 0.45x. The vibration levels were very eatic, but seemed to be affected by horsepower, molecular weight, oil pressure, and oil temperare. Several attempts were made to reduce the vibration online by vying the oil temperature and pressure, but they only achieved limited success. Aſter each change, the overall magnitude of the subsynchronous vibration would increase. It was decided that a detailed rotordync analysis of the compressor needed to be perfoed to determine the cause of the subsynchronous instability. High Subsynchronous bration The compressor is equipped with two radial proximity probes mounted at 45 degrees om the vertical at each being. The vibration monitoring system was upgraded in 1995 to include an online real time/spectrum analyzer that allowed monitong of all the spectra online. The high overall vibration levels were caused by a subsynchronous component at approximately 0.45x (3400 cpm), with the highest levels on the compressor outboard being (Figure 2). As can be seen, the subsynchronous component was approximately six times the synchronous vibration levels. In the

Upload: others

Post on 04-Mar-2021

14 views

Category:

Documents


0 download

TRANSCRIPT

Page 1: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR

by Ed Wilcox

Senior Staff Engineer Conoco, Inc.

Westlake, Louisiana

Ed Wilcox is a Senior Staff Engineer with Conoco, Inc. , in Westlake, Louisiana, where he is the Reliability Engineer for Excel­Paralubes, a joint venture between Conoco and Pennzoil. He also provides technical support for the adjacent Conoco Refinery. His responsibilities include maintenance, troubleshooting, and specification of rotating equipment.

Mr. Wilcox received his B.S.M.E. degree from the University of Missouri-Rolla and

M.S.M.E. degree from Oklahoma State University. He is also doing post graduate work at the Georgia Institute of Technology in the areas of machinery vibration, lubrication, and rotordynamics. He is a Vibration Institute certified Level III Vibration Specialist and a registered Professional Engineer in the State of Oklahoma.

ABSTRACT The cause and effects of a large subsynchronous vibration (3.5

mils at 3490 cpm) in an FCC wet gas compressor are examined. The compressor is driven at 7850 rpm by a 6000 hp electric motor, through a speed-increasing gearbox, and compresses hydrocarbon gases from 20 psig to 235 psig. A rotordynarnic analysis of the compressor determined that even though the compressor had a long history (approximately 25 years) of smooth operation (overall amplitudes less than 0.5 mils), it had a very low margin of stability. This lack of stability was caused by a high bearing to shaft stiffness ratio as well as destabilizing forces in the balance piston and shaft seals. The pressure dam bearing design is not destabilizing to the rotor system because the journal is very heavily loaded; however, the high direct stiffness that is produced reduces the effective damping of the system. Labyrinth and oil seals are usually not considered to have large effects on a compressor with such low pressures. However, the atmospheric side of the oil seal was determined to contribute the largest destabilizing effect. The effective length to diameter (LID) ratio of the oil seal was reduced by 50 percent to lower the amount of cross-coupled stiffness the seal produces. This modification reduced the subsynchronous vibration from 3.5 mils to 0.1 mils. The rotordynarnic analysis also identified other modifications to the bearing and balance piston design that should be made to increase the rotor's margin of stability. Both steady-state and transient spectral vibration data are provided before and after the oil seal modification to validate the rotordynarnic model of the compressor.

INTRODUCTION The compressor was first commissioned in 1971 and had a

history of very low vibration levels ( < 1.0 mil). It is a straight through, horizontal split machine that operates at 7850 rpm. It has two sections, with three impellers in the first section and four in the second (Figure 1). It was rerated three times between 1973 and 1992, but none of the rerates involved drastic design changes (i.e.,

41

smaller impellers were installed, speed decreased 200 rpm, three impellers were redesigned). The compressor operates at relatively low pressures with suction and discharge equal to 20 psia and 235 psia, respectively. The molecular weight of the gas varies from approximately 35 to 45.

6000 hp 1750rpm

4.49 Ratio

' Figure 1. F CC Wet Gas Compressor.

2 Section

Straight through

7850rpm

The compressor was originally installed with pressure dam bearings. The bearing effective LID was decreased during the second rerate because the rotor weight decreased slightly and it was believed that the OEM wanted to maintain the same bearing loading/eccentricity to prevent instability. The OEM recommended changing to spherically seated tilt-pad bearings during the last rerate; however, the user decided not to make the change due to historically low vibration levels. The unbalance response analysis conducted before the last rerate did not include any oil seal effects (only aerodynamic). It did show a very high amplification factor, approximately 18.

On September 26, 1997, over five years after the last rerate, the compressor shut down due to an electrical power outage. A few days after the compressor was restarted, the compressor outboard bearing vibration increased to 2.5 mils. The largest amplitude was at approximately 0.4x to 0.45x. The vibration levels were very erratic, but seemed to be affected by horsepower, molecular weight, oil pressure, and oil temperature. Several attempts were made to reduce the vibration online by varying the oil temperature and pressure, but they only achieved limited success. After each change, the overall magnitude of the subsynchronous vibration would increase. It was decided that a detailed rotordynarnic analysis of the compressor needed to be performed to determine the cause of the subsynchronous instability.

High Subsynchronous Vibration

The compressor is equipped with two radial proximity probes mounted at 45 degrees from the vertical at each bearing. The vibration monitoring system was upgraded in 1995 to include an online real time/spectrum analyzer that allowed monitoring of all the spectra online. The high overall vibration levels were caused by a subsynchronous component at approximately 0.45x (3400 cpm), with the highest levels on the compressor outboard bearing (Figure 2). As can be seen, the subsynchronous component was approximately six times the synchronous vibration levels. In the

Page 2: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

42 PROCEEDINGS OF THE 28TH TURBOMACHINERY SYMPOSIUM

cascade plot (Figure 3), the subsynchronous component appears at 6850 rpm, then disappears. Also, the vibration levels were very erratic, but continued to grow with time after the September 26, 1998 shutdown (Figure 4). Because the vibration represented a significant increase in past vibration levels, it was considered to be a serious problem. The vibration levels were affected by the following:

• Horsepower

• Process gas molecular weight

• Oil pressure

• Oil temperature

B -C-103FCC GASCOMP

c-103 -8V COMP OUTBOAR D B R G -VE RT 4.5

I 4.0

3.5 .. iii .5 3.0

i E 2.5 !! .. 'li. ;!! 2.0 "' rL

1.5

1.0

0.5

0 ] II 6000

I

12000 19000

Frequency In CPM

24000

Figure 2. Compressor Outboard Vibration.

Route Spectrum

0 1-DEC-97 15:40

OV RAL L= 3.69 D-O G

p.p = 3.67

30000

LOAD= 100.0

RPM = 7850.

RP S = 130.83

Froq: 3496.9 Ordr: .445 Spec: 3.159

Subsynchronous peak I l popsup at6850rpm�.,. �l- .... � _.. __ -� ----.-.��-.,_ ..... ����---r�t�L"P then goes away

l ------------� j j _ _ .... _ ... - - - ------ --- - - - - - -�---

1 I ---��

Figure 3. Compressor Outboard Radial Vibration on Startup.

Figure 5 shows the overall levels of vibration on the compressor outboard vertical probe immediately before the compressor was shutdown on January 6, 1998. As can be seen in the plot, the levels dropped from approximately 3.0 mils to 0.5 mils when the power was reduced from 4500 hp to 2500 hp. Likewise, the vibration dropped when the oil temperature was lowered, but would not stay low for an extended period of time (Figure 6). Raising the oil pressure also lowered the vibration (Figure 7), but the vibration levels increased later even though the oil pressure was not changed.

The vibration appeared to be very consistent with oil whirl in the journal bearings because:

• The largest component was at 0.45x.

• The vibration was affected by oil temperature and pressure.

• The problem started after an electrical power outage that might have caused the bearings to wipe.

COY Vibration

5

n�r IIJII

�4 '-'av 0

29-Jul-97 7-Sep-97 17-0ct-97 26-Nov-97 5-Jan-98 14-Feb-98

Figure 4. Increase of Vibration Amplitude Over Time.

4

,;�·· \ .. ,·--. : ........ ,.. ..

COY VIbration and Horsepower During Unit Shutdown

� !' ..... I • : .

:II' .

Vibration drops / when power is decreased

/ /

v·· .. ··-"",

I · • ·COY Overall Amplitude -%Max Load

Figure 5. Effects of Load on Vibration.

COY VIbration and 011 Temperature

5.-----------------------------------------,

4 _., ___ .......... ----................ .. ..

1 ! 3 -··

. :

. '-..... --.......... __

_§ 1 2+------..---------------------------------+

>

OL-------------------------------------�

COY Overall Amplitude • • Supply Oil Temperature I

Figure 6. Effects of Lube Oil Temperature.

100

80

60 1 j 40 '1-

20

0

150

120

90 g: I! "

60 l E �

30

0

• The bearings were fixed geometry pressure dam instead of tilting-pad.

However, several facts were not consistent with oil whirl:

• The high vibration did not start until a few days after the compressor was restarted. A wiped bearing would have normally caused a problem immediately.

• The main lube oil pump is turbine driven, so lube oil pressure was available during the shutdown.

• No high bearing temperatures were noted during the shutdown or subsequent startup.

Page 3: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR 43

I .!! !

Raised lube oil pressure

COY VIBRATION

No change in lube oil pressure

�3�----�h-------------�--------------------� �

j2t-�t-�----------------\-�����-A� .. --�

I

Figure 7. Effect of Lube Oil Pressure.

ROTORDYNAMIC STABILITY ANALYSIS A rotordynamic stability analysis was conducted to determine the

source of the subsynchronous vibration and recommend a solution to eliminate or reduce the vibration to an acceptable amplitude. The rotor model developed for this machine included the shaft model (Figure 8) as well as the following shaft support component models:

• Bearings

• Oil seals

• Balance piston seals

• Impeller eye seals

• Interstage shaft seals

• Aerodynamic effects on impellers

7stagew/balplstonanclollsaaleffects

20

..i!l " 60 ll! II II I I I I Ill T lUI

�IHJ uu d l I Ill lUI

�< � <""

20

Figure 8. Shaft Model.

Bearings

4 0

... < ��<

• 0

> <

Axial Location, Inches

70 •o ..

"'"" < '<""

• 0

The bearings are 120-degree arc pressure dam journal bearings. As can be seen in Figure 9, there are two relief tracks in the bottom half of the bearing, one on each side. These relief tracks reduce the effective LID of this bearing to be 0.25! The diametrical clearance is 0.006 inch to 0.008 inch. This design results in a very heavily loaded (180 psi) bearing with a high eccentricity ( E = 0.85 to 0.9), confirmed by shaft centerline plot, in Figure 10, and very axisymmetric principal stiff­ness (Kyy = 5 x Kxx• Figure 11). Of course this also makes the bearing have a stabilizing effect on the rotor as well, since Kxy < 0. A simpli­fied stability map for this bearing with a point mass rotor is shown in Figure 12. As can be seen, the bearing operating point is in the stable region, but it does not have an infinite onset speed of instability (i.e., it can be driven unstable). This stability map does not indicate the stability of the compressor, but does show that the bearing has no

destabilizing effects. The only possible way for this bearing to be destabilizing at its original design point was for it to be mechani­cally damaged or have the radial load on the journal decreased.

T I

-

-

-

-Lower Half

Ht.ooo L _J

Upper Half

Figure 9. Pressure Dam Bearing.

Seal bushing "locks up" then floats

"'''

Rotation · · · · - �- -

·--·---..... ; ...... : ....... ; . . . . . . • . . . . . . :. .. �.' ... ·:- . • . . • ·> . • . . • ! . • . . . ·:- ...

-o!lli.{l� • . • •

Startup with journal at bottom of bearing Operating position at

7899 rpm, e =0.87

u-u. �3.u.G� t11-U•H•$ll)t!i)

Figure 10. Compressor Nondrive End Shaft Centerline Plot.

However, this bearing design does not come without a cost to the total system stability. The high bearing to shaft stiffness ratio (K):

2KB K= Kg =24 (1)

reduces the effective damping in the system, because the rotor is like a pined connection at each end. A simple method to predict stability based on K was developed by Barrett, et al. (1978). Based on this method, the amplification factor (Q) is approximated by:

Q = 2(1 + K)=50! (2)

Likewise, the cross-coupled stiffness required in the middle of the rotor to drive the system unstable is:

1 Kxy = Mwtr [ 1 +2K ]z =3725 lbf I in (3)

2(1 + K) 2(1 + K)

and the optimum direct damping in the bearing is:

(KBc (cro&\\ w ·

CoPT= W + \

2g }} roc =7800 lbf - s I m (4)

Page 4: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

44 PROCEEDINGS OF THE 28TH TURBOMACHINERY SYMPOSIUM

Stiffness Coefficients 3.0E+06 ,.----------------------,

2.0E+06 t----------------------1 "2" "" ! 1.�+06 +----------------------1

� O.OE+OO r-------:&==e==:e==iiii=:::S:=::e=:::::e!i=:::S---j Iii G B B B 8 B El 0

·1.0E+06 t----------------------1 ... • • • • • • ...

·2.0E+06 t---�--�---�--.,---�-----1 2000

8.0E+03 7.0E+03 6.0E+03

"2" l 5.0E+03 @. "' 4.0E+03 ·i E 3.0E+03 2l 2.0E+03

1.0E+03 O.OE+OO

0 2000

4000 6000 8000 Journal Speed (rpm)

J-+-Kxx -iil-Kxy -.t.-Kyx 411-Kyyj

Damping Coefficients

II!

\ '

"' ..._____

,...___,_

4000 6000 8000 Journal Speed (rpm)

1-+-Cxx -iii- Cxy -.t.-Cyx -11- Cyy I

10000 12000

-....-........

10000 12000

Figure 11. Stiffness and Damping Coefficients for Pressure Dam Bearing.

L/D •1.5

�10.0 ::r

PRESSURE DAM BEARING STABILITY­

EFFECT Of L/0 RATIO

K'• 3.0 . .. 3 Ld•O. 75 i:1• 0.25

B. • 125• Re2·2; STABLE 1.0 l-..--L--L...J....t...l..J.l.J.l__J.......JL..-.J-.L.J..A...u..I..-....._,.Yf-1-L ............ .01 0.1 1.0 10.0

Current operating point

Figure 12. Stability Map for Pressure Dam Bearing.

which is twice the actual value. This is only an approximate method for a simple model (i.e., the rotor's mass has been lumped together into one modal mass, gyroscopics are not included, and the bearings are considered to be identical). Obviously, this method over-predicts the synchronous amplification factor because it does not include the direct damping provided by the oil seals. However, it provides an easy way to estimate the sensitivity of the rotor system and the optimum bearing damping required. This will be confirmed later by the system stability analysis using the transfer matrix method.

Oil Seals

The shaft end oil seals are the mechanical face type, with rotating and stationary faces, as well as a carbon face in between the two. The process seal itself has very little effect on the rotor, other than to add a little damping. It is the floating bushing seal that is the big concern (Figure 13). The bushing seal floats in the seal housing and allows the seal oil that does not leak past the process seal to return to the lube oil reservoir, through the lube oil return line. If the friction force generated by the differential pressure across the seal is greater than the hydrodynamic forces generated by the oil between the seal and the shaft, the seal ring will no longer float in the radial direction . Floating seals at these low pressures are usually not considered to be a problem, since the low differential pressures do not allow for a potential "lock up." The bushing seal can float 0.030 inch diametrically in the housing, but only has 0.003 inch axial clearance. It was originally designed with a relatively low diametrical clearance of 0.005 inch to 0.007 inch between it and the shaft. Note: this clearance is less than the bearing's, which is 0.006 inch to 0.008 inch.

Figure 13. Shaft End Seal.

The 70 psid oil pressure exerts approximately 600 lbf of axial force, which presses the bushing into the outer ring of the seal housing. High pressure seal faces are normally lapped together to produce a very smooth finish and/or spray coated with a hard material such as tungsten carbide to reduce the amount of friction between the two. However, because it is such a low pressure application, the bushing seal in this seal is just machined. This increases the coefficient of friction between the floating bushing and seal housing, resulting in a radial force of approximately 120 to 150 lbf that can "lock up" the bushing seal in an eccentric position (Figure 14). The emergence of the subsynchronous vibration at 6850 rpm, in Figure 3, is evidence that the floating bushing "locked up" momentarily on startup, but then started floating again by the time the compressor reached full speed. The radial load carrying capability of these seals is not enough to lift the rotor off the bearings (the rotor weighs 1450 lbf). However, these bushings can affect the rotor stability in two ways:

• Decrease the radial load on the bearings-Decreasing the radial load on the bearings would reduce the eccentricity of the journal in the bearings and potentially cause the journal to "whirl" in the bearing. However, the downward force of the pressure dam is approximately 400 lbf. This force along with the rotor half weight of 725 lbf is more than enough to keep the bearing in a stabilizing mode at this speed.

Page 5: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ''PROVEN" FCC WET GAS COMPRESSOR 45

Friction load =

120lbf No.alload = 600 lbf

t .... � �·� Cd = 0.005 inch Axial float= 0.003 inch Radial float = 0.030 inch

Figure 14. Floating Seal Oil Breakdown Bushing.

• Act as an additional support with a high cross-coupled stiffness-In addition to affecting the radial load on the bearing, the bushing seal acts as a bearing as well. The bushing seal is similar to a straight journal bearing with no pressure dam, an LID =

0.1875, and an axial pressure drop of 70 psid. The floating bushing develops stiffness and damping in a similar manner to a journal bearing, except that the flow is obviously more turbulent and the oil does not normally cavitate until it reaches the low pressure side of the seal.

Because of the balance line, the floating bushings on each end of the compressor see the same seal oil differential pressure, but not the same oil temperature. Because of limited buffer gas on the seals, the discharge temperature of the compressor causes the seal oil temperature on the drive end to be approximately 175"F (52 SSU); whereas, on the nondrive end, the oil enters the sleeve at approximately l lO"F (100 SSU). Because the flow through the seal is nearly laminar, the viscous effects are much more important than inertial forces. This lower viscosity on the drive end makes a large difference in the stiffness coefficients between the two seals of the compressor. As can be seen in Figures 15 and 16, the nondrive end seal has a much higher cross-coupled stiffness value.

Oil Seal - Non-drive end 140000

120000

100000 // /�

80000 c: "" 60000 ,g

� 40000 c:

� 20000

/ -� / v �-�A

A v·--·-· ------..

_______. -------

-20000

-40000 . .....____, -60000

2000 4000 6000 6000 10000 12000 Rotor Speed, rpm

Figure 15. Stiffness Coefficients for Nondrive End Oil Seal.

Note: the computer model for the bushing seal requires the seal eccentricity as input. Since the eccentricity is unknown, it is entered iteratively until the calculated radial load capacity matches the frictional load in Figure 14.

Balance Piston Seal

The balance piston seal has a teeth-on-rotor (TOR) labyrinth (Figure 17). This type of labyrinth is very common on wet gas services because of its excellent resistance to fouling (i.e., it centrifuges out any buildup in the labyrinth). However, TOR labyrinths have been shown to be more unstable than teeth-on­stator (TOS) seals (Childs, 1993). The location of the balance

Oil Seal - Drive End 140000

120000

100000

60000 c: "" 60000 ,g .,; -------"' 40000 " � 20000 en

L---------- ----::--- f-----

-20000 .. -'""--·40000

·60000 2000 4000 6000 6000 10000 12000

Rotor Speed, rpm

Figure 16. Stiffness Coefficients for Drive End Oil Seal.

piston seal relative to the antinode of the first bending mode (i.e., larger displacement means larger force produced) is the reason this balance piston has a large affect on the stability of the compressor, not the magnitude of the stiffness coefficients (Figure 18). Obviously, the balance piston seal is much closer to the center of the rotor than the bearings or oil seals. Because of the shape of the first bending mode, this causes the effect of the balance piston to be magnified.

Rotating labyrinth 21 teeth, 0.19 in equal spacing, 0.18 in tall Diametrical clearance- 0.010- 0.020 inch External diameter - 12.993 P1=235 psia P2= 35 psia Mw=35-45

Figure 17. Balance Piston Seal.

Balance Piston 70000

60000

60000

40000 c:

£! 30000

!3 20000 " c:

� 10000 / ___, .--------

-10000

-20000

---. ..._____ r----

·30000 0 2000 4000 6000

I /

/

6000 Rotor Speed, rpm

I I

/ /

10000

Figure 18. Balance Piston Seal Stiffness Coefficients.

12000

The cross-coupled stiffness of a labyrinth seal is a function of many parameters including surface speed, differential pressure, and gas molecular weight. Neither the speed nor differential pressure changed in Figure 5 (i.e., low load case); however, the molecular weight of the gas drops as the FCC unit is being shut down. This indicates that the balance piston seal (likewise the other internal labyrinth seals) may be causing the sensitivity to load. The stiffness coefficients for the balance piston seal with half the

Page 6: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

46 PROCEEDINGS OF THE 28TH TURBOMACHINERY SYMPOSIUM

normal molecular weight is shown in Figure 19. They are approximately 75 percent lower than those in Figure 18. The effect of the balance piston seal, with the two different molecular weights, on the stability of the compressor will be discussed below.

c: "' ,g .;

20000

15000

10000

5000

� ·5000 � -10000

-15000

-20000

·25000

-30000 2000

Balance Piston w/ Mw=20

/ /

...--,.____, ...____

"' ""'

"" ""

4000 6000 6000 10000 12000

Rotor Speed, rpm

Figure 19. Balance Piston Seal Stiffness Coefficients with Mole Weight= 20.

Impeller Eye Sealsllnterstage Shaft Seals

Obviously, the stiffness and damping coefficients for the small impeller eye and interstage shaft seals are quite low in comparison with the balance piston seal listed above. This is due to:

• Much lower differential pressure.

• TOS construction.

• Reduced LID.

• Reduced number of teeth.

In fact, the impeller eye seals have such a small effect for a compressor of this type, with such low pressures, that their effect in the rotordynarnic model is negligible.

Aerodynamic Effects on Impellers

Because of the relatively low pressures and horsepower, the cross-coupled stiffness values obtained from the Wachel equation were all less than 500 lbf/in per impeller, at full load with the high molecular weight. These values certainly add to the instability of the system just because they increase the amount of cross-coupled stiffness at the center of the rotor (where it has the most effect on the first bending mode), but overall they have a very minor effect on the stability of the compressor.

SUMMARY OF STABILITY ANALYSIS The first step in any stability analysis is to verify the

rotordynarnic model of the machine. The calculated unbalanced response at the outboard bearing, Figure 20, shows the fust damped mode to be in close agreement with the one shown in the measured Bode plot (Figure 21).

Table 1 shows the calculated logarithmic decrement (log dec) and frequency of the first forward mode of the compressor for various models. The rotor with the bearings alone is not very stable, with a log dec of only 0.035 (model 1). Normally, a minimum log dec of 0.1 to 0.2 is required to ensure stability of the system. The stability improves slightly with the addition of the centered oil seals to the model because of the damping they add (model 2). Adding the balance piston seal lowers the calculated log dec to 0.022 (model 3), though it is still considered marginally stable. If the seals are assumed to be locked with the low molecular weight gas, the calculated log dec increases slightly to 0.035 (model 4), which explains the low vibration when the compressor was pumping lighter gas. As can be seen, it is only the

0 ..

0.70

I 0.80

.!! 0.50

! 11 OAO 'g =8. 0.30

E Cl; 0.20

0.10

0.00

Compressor Outboard Vertical

II

I I I

I \ I �

__..., ----

1000 2000 I1JOO

Speed (rpm)

Figure 20. Predicted Unbalanced Response of Compressor Outboard Bearing.

Bodat Histori.cal: 02-27 09:43:00 - 02-27 09 ,4.9' 00

1%1.il.• �-------------------------------------, o .•

0.4

o .•

l.OOO 2000 4000 7000 8000

Figure 21. C-103 Measured Response, Compressor Outboard Bearing Vertical.

combination of locked seals and high molecular weight that drive the compressor unstable (model 5). The frequency of the high subsynchronous vibration is within 200 cpm of the predicted first forward mode at 3240 cpm for this model (Figure 22). The calculated log dec of the first mode equals -0.055, which means that the vibration will not die out if it is perturbed (i.e., the system is unstable).

Table 1. Variations in Stability of Calculated First Forward Mode.

# Model Log Dec Frequency 1 Rotor/bearings 0.035 3336 2 Rotor/bearings/floating oil seals 0.044 3305 3 Floating oil seals/balance piston/high MW -load 0.022 3247 4 Locked oil seals/balance pistonllow MW-load O.D35 3280 5 Locked oil seals/balance piston/high MW -load -0.055 3240

The following conclusions can be drawn from the stability analysis:

• The high bearing to shaft stiffness ratio causes the rotor to be very sensitive to even small amounts of cross-coupled stiffness.

• The instability of the compressor is caused mainly by the destabilizing forces in the shaft oil seals and balance piston labyrinth seals.

• The increase in vibration after the September 26, 1997 shutdown was probably caused by lockup of the oil seals, during the shutdown under load or subsequent startup.

• The subsynchronous vibration is not caused by destabilizing forces (oil whirl) in the journal bearings. The bearings are loaded heavily enough at this speed.

Page 7: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ''PROVEN" FCC WET GAS COMPRESSOR 47

Damped Eigenvalue Mode Shape Plot C-103 FCC Wet Gas Compressor

7 stage w 1 bal piston and oil seal effects

forward _backward

Figure 22. First Forward Mode Shape, Before Modifications.

• The oil seal floating bushing is very similar to a lightly loaded journal bearing, which has large amounts of cross-coupled stiffness.

• The lack of vibration during the low load condition probably comes from reduction of the cross-coupling in the balance piston labyrinth seal and the aerodynamic cross-coupling in the impellers, when the molecular weight of the gas and the horsepower of the compressor are both lower.

• Nondrive end seal effects are greatest because of higher seal oil viscosity.

PROPOSED MODIFICATIONS The root cause of the subsynchronous vibration is the high

bearing to shaft stiffness ratio, which decreases the effect of the system damping. The obvious answer to this problem is to replace the existing bearing design with a new design that is stabilizing but does not produce such high direct stiffness values. This can be accomplished with an optimized tilting-pad bearing. However, changing to a tilt-pad bearing design required modifications to the bearing housing and a considerable amount of downtime. Because of the compressor's long history of low vibration and the fact that the problem occurred after the electrical shutdown, the plant maintenance department still believed that the compressor bearings had been damaged. Also, only a short time period (approximately 24 hours' mechanical time) was available in January 1998 to work on the compressor without impacting plant throughput.

Since the oil seals could be modified easily, they were examined. It was decided to increase the diametral clearance of the bushing seal by 0.001 inch, and decrease the effective LID of the seal by cutting a 1/16 inch square groove in the middle of the land of the seal (Figure 23). Increasing the clearance and cutting the groove in the bushing seal breaks up the hydrodynamic effect in the seal, which produces the high cross-coupled stiffness (Semanate and San Andres, 1993). It also reduces the radial load capacity of the seal, which causes the modified seal to operate with a higher eccentricity. Reduction of the hydrodynamic effect in the seal could have been accomplished by just increasing the seal clearance. However, this would have resulted in too much seal leakage, since the leakage rate is proportional to the cube of the clearance.

The predicted stiffness coefficients of the modified bushing seal are shown in Figure 24. As can be seen the cross-coupled stiffness, Kxy• is approximately 30 percent to 40 percent of the previous value in Figure 15. Its effect on the first mode is to raise the log dec to 0.022 (identical to the value predicted for floating seals, Figure 25). This value indicates a very slight margin of stability.

RESULTS OF MODIFICATIONS On January 6, 1998, the compressor was shut down to inspect

the bearings and make the necessary modifications to the floating

0.375 in

Co=0.006

1 ...

1/16 inch square groove

Figure 23. Modifications to Floating Seal Bushing.

Oil Seal- Non-drive end (After Modifications) 140000

120000

100000

80000

c:: � 60000

ui 40000 "'

IJ)

� 20000

0 t::=:.. l---: ,_....-- ---f---

--.. --<1

.__

·20000

-40000

-60000

0 2000 4000 6000 8000 10000 12000

Rotor Speed, rpm

Figure 24. Seal Bushing Stiffness Coefficients After Modifications (One-Half of Seal).

Damped Eigenvalue Mode Shape Plot C-103 FCC Wet Gas Compressor

After modification of non-drive end oU seal

forward -backward

Figure 25. Mode Shape of Compressor After Nondrive Seal Bushing Modification.

bushing. The bearings were found to be well within the OEM clearance tolerance and showed no signs of wear. The modifications were made to the nondrive end seal bushing. After the compressor was started again, the overall levels of vibration were below 1.0 mil on all compressor probes. The spectrum from the compressor outboard vertical probe at full load shows that the subsynchronous component has been reduced from 3.5 mils to 0.1 mil (Figure 26).

Page 8: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

48 PROCEEDINGS OF THE 28TH TURBOMACHINERY SYMPOSIUM

c - 103 -BV COMP OUTBOAR D BRG ·VERT 1•0 ,--,--1-,----,---......---�---. Route Spectrum

1!hiAN-98 09:47

0.8

0.6

0.4

0.2

6000 12000 18000

Frequency In CPM

I. 24000

OVRAL L= .7954 D - DG

P·P= .7924

LOAD= 100.0

30000

RPM= 7850.

RPS= 130.83

Freq: 358 1.3

Ordr; .456

Spec: . 106

Figure 26. C-103 Compressor Outboard Vertical Spectrum After Seal Bushing Modification.

ADDITIONAL RECOMMENDATIONS Even though the compressor vibration was acceptable after the

modifications to the oil seal, the margin of stability needs to be increased. This can be accomplished by modifying the bearing and/or the balance piston seal design.

The bearing design should be changed to lower the bearing to shaft stiffness ratio (K). As mentioned above, this is the root cause of the stability problem. The bearing selected is a five pad, load­on-pad (LOP) bearing, with a preload of 0.2 and LID = 0.4. Stiffness and damping coefficients for the proposed bearing are shown in Figure 27. This will improve the stability of the first forward mode (the calculated log dec is 0.5), as well as reduce the amplification factor of the rotor to 5.6 (Table 2).

5 Pad, LOP, IJD=0.4, 0.2 Preload

1.2000E+06 ,---------------------r2500.0

500.0 a�� r-------------------1

O.ODOOE+00-1----�-----�--�-------i- O.O 0 2000 4000 6000 8000 10000 12000

- ( .... )

Figure 27. Optimized Tilting-Pad Bearing Stiffness and Damping Characteristics.

Table 2. Comparison of Pressure Dam and Tilt-Pad Bearings.

Modification Log Dec Amplification Factor

Pressure dam Bearing w/ seal mods 0.022 18.1

4 pad, LBP bearing w/ seal mods 0.51 5.6

The stability of the compressor can be increased further by replacing the existing TOR design balance piston seal with various designs that are less destabilizing, such as TOS

labyrinth, honeycomb, or TAMSEAL™. All three of these options would undoubtedly improve the stability of the compressor, but they would all be very costly in comparison to the proposed bearing design modification and would require a much longer timeframe to install. Besides, the calculated stability with the tilt-pad bearing design does not warrant any further modifications, and the rotordynamic model has already been proven to be accurate.

CONCLUSIONS Many machines operating today may have only a small margin

of stability. Regardless of the number of years of smooth operation, even the most reliable machine may have hidden stability problems. The fixed geometry bearings in many older compressors may have been "optimized" so that the fixed geometry bearings themselves are stable; however, this may limit the overall stability of the compressor itself. The bearing to shaft stiffness ratio (K) is an important parameter in accessing the long term stability of a machine. Normally, the value of K should be maintained below 10 to 12 to guarantee a stable machine. Obviously, this limitation is dependent upon the amount of direct damping available in the bearings, seals, and/or bearing supports.

Just because a compressor operates at low pressures, does not mean that it cannot be susceptible to destabilizing forces from oil seals and labyrinth seals. The oil seals can easily lock up if the seal is not well balanced and/or the seal faces do not have a very smooth finish. Likewise, even a low differential pressure labyrinth can be a problem if the compressor is only marginally stable and the seal design is somewhat destabilizing.

NOMENCLATURE c = Bearing radial clearance Copt = Optimum bearing damping K = Shaft to bearing stiffness ratio

� = Bearing stiffness tensor = Rotor modal mass

Q = Synchronous amplification factor w = Rotor modal weight

fficr = Rotor rigid bearing critical speed

Subscripts

B = Bearing S = Shaft

REFERENCES Barrett, L. E., Gunter, E. J., and Allaire, P. E., 1978, "Optimum

Bearing Support Damping for Unbalance Response and Stability of Rotating Machinery," Journal of Engineering for Power, 100, pp. 89-94.

Childs, D. W., 1993, Turbomachinery Rotordynamics, New York, New York, J. C. Wiley.

Semanate, J. E. and San Andres, L. A., 1993, "Analysis of Multi­Land High Pressure Oil Seals," Tribology Transactions, 36, pp. 661-669.

BIBLIOGRAPHY Atkins, K. E. and Perez, R. X., 1988, "Influence of Gas Seals on

Rotor Stability of a High Speed Hydrogen Recycle Compressor," Proceedings of the Seventeenth Turbomachinery Symposium, Turbomachinery Laboratory, Texas A&M University, College Station, Texas, pp. 9-18.

Atkins, K. E. and Perez, R. X., 1992, "Assessing Rotor Stability Using Practical Test Procedures," Proceedings of the Twenty-First Turbomachinery Symposium, Turbomachinery Laboratory, Texas A&M University, College Station, Texas, pp. 151-159.

Page 9: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN'' FCC WET GAS COMPRESSOR 49

Allaire, P. E. and Nicholas, J. C., 1978, "Analysis of Step Journal Bearings-Finite Length, Stability," ASLE Transactions, 22, pp. 197-207.

Allaire, P. E., Kocur, J. A., and Stroh, C. G., 1986, "Oil Seal Effects and Subsynchronous Vibrations in High Speed Compressors," NASA Report, CP 2409, pp. 205-223.

Childs, D. W. and Scharrer, J. K., 1986, "Experimental Rotordynamic Coefficient Results for Teeth-on-Rotor and Teeth-on-Stator Labyrinth Gas Seals," Journal of Engineering for Gas Turbines and Power, 108, pp. 599-604.

Cerwinske, T. J, Nelson, W. E., and Salamone, D. J., 1986, "Effects of High Pressure Oil Seals on the Rotordynamic Response of a Centrifugal Compressor," Proceedings of the Fifteenth Turbomachinery Symposium, Turbomachinery Laboratory, Texas A&M University, College Station, Texas, pp. 35-52.

Emerick, M. F., 1982, "Vibration and Destabilizing Effects of Floating Ring Seals in Compressors," Proc. of the Workshop on Rotordynamic Instability Problems in High Performance Turbo-Machinery, Texas A&M University, College Station, Texas, pp. 187-204.

Kirk, R. G., 1986, "Oil Seal Dynamics: Considerations for Analysis of Centrifugal Compressors," Proceedings of the Fifteenth Turbomachinery Symposium, Turbomachinery Laboratory, Texas A&M University, College Station, Texas, pp. 25-34.

Semanate, J. E. and San Andres, L. A., 1994, "Thermal Analysis of Locked Multi-Ring Oil Seals," Tribology International.

Vance, J., 1988, Rotordynamics of Turbomachinery, New York, New York: J. C. Wiley.

Wilkes, K. W., Kirk, R. G., and Elrod, D. A., 1993, "Rotordynamic Analysis of Circumferentially-Grooved Turbulent Seals: Theory and Comparison to Published Results," Tribology Transactions, 36, pp. 183-192.

Zeidan, F. Y. and Carlson, T. D., Nov/Dec 1991, "Sub-Synchronous Vibrations: Temporary Fix and Permanent Solution," Turbomachinery International, pp. 38-45.

Zeidan, F. Y., Perez, R. X., and Stephenson, E. M., 1993, "The Use of Honeycomb Seals in Stabilizing Two Centrifugal Compressors," Proceedings of the Twenty-Second Turbomachinery Symposium, Turbomachinery Laboratory, Texas A&M University, College Station, Texas, pp. 3-15.

ACKNOWLEDGEMENT

This paper would not have been possible without the help from Daryl Taylor of Conoco, Jerry Rodriguez and Ted Gresh of Elliott Co., Robert Perez of Koch, Inc., Dr. Fouad Zeidan of Bearings, Inc., and Dr. Luis San Andres and Dr. John Vance both of Texas A&M University.

Page 10: UNEXPECTED ROTORDYNAMIC INSTABILITY IN A ...UNEXPECTED ROTORDYNAMIC INSTABILITY IN A "PROVEN" FCC WET GAS COMPRESSOR by Ed Wilcox Senior Staff Engineer Conoco, Inc. Westlake, Louisiana

50 PROCEEDINGS OF THE 28TH TURBO MACHINERY SYMPOSIUM