simpson - boiler feed pump turbine case study

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Page 1 of 11 Boiler Feed Pump Turbine Subsynchronous Vibration Case Study Jeffrey Simpson, P.E. LG&E and KU Energy LLC [email protected] ABSTRACT This paper presents the case study of a boiler feed pump turbine subsynchronous vibration problem that resulted in numerous shutdowns, production limits and an outage of a large steam turbine generating unit. Diagnosing the problem proved to be challenging due to assumptions established from the machine history and other informational factors. The machine had been retrofitted with an advanced vibration monitoring and diagnostics system that provided detailed vibration data capture prior, during and after events. This paper describes the events, diagnostics tools, root cause process and pitfalls surrounding this unusual subsynchronous vibration problem. INTRODUCTION A single GE Type DRV631 19,000 HP turbine driven boiler feed pump (TDBFP), Figure 1, pumps water to the boiler to produce 2400 PSIG, 1005 F steam that drives a GE Type G2 525 MW steam turbine generating (T/G) unit commissioned for service in 1982. Loss of the TDBFP will result limiting the generating limit to 160 MW (365 MW loss) due to having operate with a motor driven start up pump. Both the TDBFP and T/G are instrumented with GE Bently 3500 vibration protection circuitry and GE Bently System 1 continuous data collection/diagnostics software. Each bearing is equipped with X and Y orthogonal proximity probes and bearing metal temperature thermocouples. On November 13, 2012 while operating at 4,768 RPM (79.5 Hz), the TDBFP turbine protection circuitry tripped the machine due to high inboard bearing vibration, followed by the main generating unit tripping from loss of feedwater. Before resolving the problem nine (9) days later, the TDBFP turbine had tripped a total of five (5) times on high inboard bearing vibration, was unavailable and resulted in nearly 61,000 MWH of lost generation. Logical root cause analysis efforts can sometimes lead down the wrong path requiring reevaluation and extra time to solve a problem. MACHINE HISTORY In 1996 this TDBFP turbine experienced a 1/2X operating speed vibration problem which caused a series of random trips and outages. At that time the unit did not have a continuous data collection and diagnostics system to analyze the vibration, only overall amplitude was available. Delaware Analysis Services (then CJ Analytical) was contracted to instrument, analyze and diagnose the cause of vibration trips. Upon discovering that the vibration was at 1/2X operating speed, Delaware recognized it to be a known problem with this type of TDBFP turbine inboard bearing caused by a subsynchronous resonance as a result of the rotor operating at 2X first critical and triggering the rotor first critical to excite the bearing pedestal natural frequency that happens to be at that same frequency 1 . The solution was a redesign of the elliptical sleeve bearing to a “pressure dam” type sleeve bearing by simply re-pouring and machining a recess in the upper half of the bearing to provide downward oil force on the journal,

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  • Page 1 of 11

    Boiler Feed Pump Turbine Subsynchronous Vibration Case Study

    Jeffrey Simpson, P.E. LG&E and KU Energy LLC

    [email protected]

    ABSTRACT

    This paper presents the case study of a boiler feed pump turbine subsynchronous vibration problem that

    resulted in numerous shutdowns, production limits and an outage of a large steam turbine generating

    unit. Diagnosing the problem proved to be challenging due to assumptions established from the

    machine history and other informational factors. The machine had been retrofitted with an advanced

    vibration monitoring and diagnostics system that provided detailed vibration data capture prior, during

    and after events. This paper describes the events, diagnostics tools, root cause process and pitfalls

    surrounding this unusual subsynchronous vibration problem.

    INTRODUCTION

    A single GE Type DRV631 19,000 HP turbine driven boiler feed pump (TDBFP), Figure 1, pumps water to

    the boiler to produce 2400 PSIG, 1005 F steam that drives a GE Type G2 525 MW steam turbine

    generating (T/G) unit commissioned for service in 1982. Loss of the TDBFP will result limiting the

    generating limit to 160 MW (365 MW loss) due to having operate with a motor driven start up pump.

    Both the TDBFP and T/G are instrumented with GE Bently 3500 vibration protection circuitry and GE

    Bently System 1 continuous data collection/diagnostics software. Each bearing is equipped with X and Y

    orthogonal proximity probes and bearing metal temperature thermocouples.

    On November 13, 2012 while operating at 4,768 RPM (79.5 Hz), the TDBFP turbine protection circuitry

    tripped the machine due to high inboard bearing vibration, followed by the main generating unit

    tripping from loss of feedwater. Before resolving the problem nine (9) days later, the TDBFP turbine had

    tripped a total of five (5) times on high inboard bearing vibration, was unavailable and resulted in nearly

    61,000 MWH of lost generation. Logical root cause analysis efforts can sometimes lead down the wrong

    path requiring reevaluation and extra time to solve a problem.

    MACHINE HISTORY

    In 1996 this TDBFP turbine experienced a 1/2X operating speed vibration problem which caused a series

    of random trips and outages. At that time the unit did not have a continuous data collection and

    diagnostics system to analyze the vibration, only overall amplitude was available. Delaware Analysis

    Services (then CJ Analytical) was contracted to instrument, analyze and diagnose the cause of vibration

    trips. Upon discovering that the vibration was at 1/2X operating speed, Delaware recognized it to be a

    known problem with this type of TDBFP turbine inboard bearing caused by a subsynchronous resonance

    as a result of the rotor operating at 2X first critical and triggering the rotor first critical to excite the

    bearing pedestal natural frequency that happens to be at that same frequency1. The solution was a

    redesign of the elliptical sleeve bearing to a pressure dam type sleeve bearing by simply re-pouring

    and machining a recess in the upper half of the bearing to provide downward oil force on the journal,

  • Page 2 of 11

    Figure 2. This increased the first critical above the pedestal natural frequency and eliminated the

    subsynchronous high vibration occurrences.

    Figure #1 GE Type DRV631 19,000 HP Turbine Driven Boiler Feed Pump

    The TDBFP turbine was last overhauled in 2006 where the pressure dam bearing was re-installed after

    being reconditioned to proper clearances. The 1/2X vibration phenomenon was also experienced on two

    other company TDBFP turbines, also corrected with pressure dam bearings. Any change to stiffness or

    bearing load such as might be caused by bearing profile, wiped bearing, looseness, clearance/fit, cracked

    pedestal, alignment, steam loading, etc. can lower the first critical frequency back down to where

    interaction with the pedestal is possible. Both the TDBFP and T/G are retrofitted with GE Bently 3500

    vibration protection circuitry and GE Bently System 1 continuous data collection/diagnostics software.

    DISCUSSION

    Analysis of the November 2012 TDBFP turbine vibration trip by LG&E KU Generation Engineering using

    the Bently System 1 discovered a sub-synchronous vibration of 7.67 mils P-P at near 1/2X of 4,768 RPM

    operating speed that had exceeded the trip limit of 5 mils, Figure 3. A trend plot of the inboard bearing X

    and Y proximity probes 1X operating speed and overall (direct) vibration demonstrated the 1/2X

    vibration went from normal to trip level in just a few seconds on both X and Y probes, lessening the

  • Page 3 of 11

    prospect of a probe or instrument related issue, Figure 4. A different view of the event in Figure 5 shows

    a waterfall plot of the 1/2X vibration disappearing within a couple seconds of the machine tripping. At

    the time of the trip the unit and pump were at approximately 90% load and slowly increasing to meet

    demand. There was no sign of oil whirl/whip as the orbit showed no signs of distress as can be seen by

    the large round subsynchronous orbit, Figure 6. Bearing lube oil supply temperature was within

    acceptable limits at 111F and no significant change in bearing metal temperature was discovered. The

    pump bearing vibration also increased but at much lower amplitude levels. A review of the control

    system data showed the BFP turbine bearing overall vibration amplitude and variability had step

    increased in June 2012, about one week after coming back on from a maintenance outage and five

    months before the November 1/2X trip, Figure 7.

    Figure #2 Pressure Dam Sleeve Bearing

  • Page 4 of 11

    Figure #3 BFPT Inboard Bearing 1/2X Vibration

    Figure #4 100 Sec Trend of Inboard Direct and 1X Vibration, 1st Trip

    1/2X

    1X

  • Page 5 of 11

    Figure #5 Inboard Bearing Waterfall Plot, 1st Trip

    Figure #6 Inboard Unfiltered Orbit, 1st Trip

  • Page 6 of 11

    Figure #7 Trend of Inboard Overall Vibration, March Aug 2012

    The TDBFP and main T/G unit were returned to service several hours after the first trip to meet load

    demand and determine if the vibration trip was a one-off event. Approximately 23 hours later the

    question was answered by a second trip of the BFP turbine and main T/G unit, again due to BFP turbine

    inboard bearing 1/2X high vibration at nearly the same operating speed. Based on the 1/2X vibration

    history of this machine, a problem with the inboard pressure dam bearing was suspected. Although the

    proximity probe gap voltages, Figure 8, did not indicate a wiped bearing an inspection was performed to

    check dimensions and fits, all of which were found acceptable. As a precaution the bearing was

    refurbished due to light scoring. During the period of the TDBFP outage the main generating unit was

    operated at reduced load using a motor driven start-up pump.

    Figure #8 Trend of Inboard Bearing Gap Voltages Prior to 1/2X Trip

    Mil lCreek.U4.4F3358.PV

    Mil lCreek.U4.4F3359.PV

    Mil lCreek.U4.4F3360.PV

    2.1633

    mils

    Mil lCreek.U4.4F3361.PV

    Mil lCreek.U4.4TPSM21AI.PV

    Mil lCreek.U4.SV.UNITLOAD.001H.avg.AvgValue

    BFPT BRG 2X VIBRATION

    8/6/2012 2:30:51 AM3/8/2012 1:01:48 AM 151.06 days

    MC4

    0

    1

    2

    3

    4

    5

    6

    7

    8

    9

    10

  • Page 7 of 11

    Shaft alignment of the grease lubricated double engagement gear spacer coupling, Figure 9, was

    checked using a LUDECA laser alignment system. The TDBFP was returned to service with a refurbished

    inboard pressure dam bearing. A live vibration spectrum was displayed in System 1 as the pump speed

    was increased with main unit load. After only three hours of service the 1/2X vibration appeared at an

    operating speed of 4,527 RPM so the pump was shut down before tripping. The TDBFP was rolled up

    one more time to verify if the problem repeated at the same speed. This time the 1/2X vibration began

    at a lower speed of 4,223 RPM indicating the speed at which the 1/2X occurred was decreasing, Figure

    10. This was different than the problem experienced in 1996 where the subsynchronous vibration

    repeated at relatively the same rotor operating speed.

    Figure #9 Double Engagement Gear Spacer Coupling

  • Page 8 of 11

    Figure #10 1/2X Occurring at Lower Speeds for Subsequent Events

    Refurbishing the bearing made no difference and the problem was potentially worsening. The bearing

    appeared to be unloaded as the orbit in Figure 6 is circular. Referencing back to the control system data

    in Figure 7, signs of a problem conceivably began five months earlier, about a week after the June 2012

    maintenance outage. Engineering began to evaluate what conditions could result in unloading a bearing

    and if there was work performed during the outage that could be related to the problem. Steam

    influences can lift turbine rotors but the inboard bearing is at the opposite end of the steam nozzle and

    the machine was not known to have low pressure nozzle issues. Steam supply control valve linkages

    were visually in good condition. A review of the June outage work revealed that the TDBFP turbine

    steam exhaust expansion joint located directly below the inboard bearing end was replaced. The rubber

    joint visually appeared to be stretched very tight so there was concern the new joint could be pulling

    down on the frame, lowering the inboard bearing support thus unloading the bearing. A review of the

    shaft alignment job performed after the refurbished bearing showed that the alignment data did not

    repeat and several vertical moves were made. Due to the lack of repeatable data the vertical position

    was restored to as-found by reinstalling the original shims. Laser alignment systems allow for alignment

    of flexible couplings without uncoupling the machine provided there is access to mount the laser

    brackets on the coupling hubs at each end. An observation was made that the turbine end coupling hub

    was not accessible due to the tight spacing between coupling gear housing and the turbine frame, Figure

    9. During alignment the turbine end laser bracket was incorrectly mounted on the coupling gear housing

  • Page 9 of 11

    instead of the hub resulting in erroneous and inconsistent alignment data. The coupling spacer would

    need to be removed to properly check alignment.

    During removal of the coupling spacer an unexpected finding was made. A small amount of water

    drained out from the coupling as the spacer was removed and the gear teeth were found to have no

    grease, corroded and heavily contaminated with debris, Figure 11. This could be the source of the 1/2X

    vibration if the coupling were locking up causing a change to the rotor dynamics and unloading the

    bearing. It was obvious the coupling had to be cleaned and re-greased but this unearthed yet another

    problem of not sufficient clearance to slide back the coupling covers to access the gear teeth, Figure 12.

    The only way to gain access to the gear teeth and the small 5/32 space on the backside of the teeth

    would be to provide enough clearance to slide the coupling covers out of the way which would require

    removing the entire turbine rotor and partial disassembly of the pump. There was no way that proper

    routine lubrication PMs had ever been performed or ever could be performed on the coupling other

    than during machine overhauls. The coupling was painstakingly cleaned out using wire and other small

    implements to fish out debris, followed by re-greasing through the ends of the gear teeth.

    Figure 11 Turbine End Coupling Half As-Found

  • Page 10 of 11

    The TDBFP was returned to service seven days after the first incident. Watching the live data as the

    speed increased there was no sign of the 1/2X until it suddenly appeared again at 5,015 RPM, but 15%

    higher than last observed and 5% higher than the first trip which was an explainable improvement

    because as load increases the friction between the coupling gear teeth also increases. The machine was

    taken out of service. This time a more aggressive effort was made to clean out the coupling, again using

    wire and other small implements to meticulously fish out debris but also repeatedly flushing a solvent

    through the gear teeth in hopes of removing as much debris as possible. Additionally the grease type

    previously used was found not to be for couplings, so Conoco-Phillips Coupling Grease was applied

    during the second attempt by forcing grease through the teeth. Not being able to slide the coupling

    housing back on the hub and the tight clearances between the hub and housing gear teeth made it

    difficult, if not impossible to ensure all friction surface areas were properly greased.

    Figure #12 No Access to the Gear Teeth

    The TDBFP was again put into service for the fifth and final time since the first vibration trip nine days

    prior. Full load was obtained without any signs of the 1/2X running speed vibration. Gear coupling

    manufactures recommend biannual greasing and periodic cleaning to ensure reliable coupling

    performance. Suspecting the problem would likely return from not being able to perform proper routine

  • Page 11 of 11

    maintenance, a Goodrich contoured diaphragm non-lubricated coupling will be installed as a permanent

    solution at the next planned outage opportunity, Figure 13.

    Figure #13 Goodrich Diaphragm Coupling

    CONCLUSIONS:

    A misapplied coupling design in service since 1982 resulted in a locked up gear coupling when under

    load due to lack of lubrication caused by the inability to perform proper routine cleaning and greasing.

    This resulted in unloading the bearing causing a fluid induced rotor instability manifested at 1/2X

    running speed vibration. Having an online vibration diagnostics system was a valuable asset for

    automatic capture of the data and post event analysis. To permanently mitigate the root cause, a non-

    lubricated diaphragm coupling will be installed. The past history of the inboard bearing subsynchronous

    resonance initially led engineering to assume a repeat of a previous problem. In retrospect, an

    inspection of the coupling in conjunction with the bearing refurbishment would have been prudent.

    REFERENCES:

    Eshleman, Ron; Guy, Kevin; Jackson, Charles. "Auxiliary Turbine Subsynchronous Vibration", Vibration

    Institute article, 1985. 1

    Bently, Donald. Fundamentals of Rotating Machinery Diagnostics, 2002.