root cause analysis of incidents during l ts catalyst ......l ts catalyst beds to reach temperatures...

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Root Cause Analysis of Incidents during LTS Catalyst Reduction and Primary Reformer Coking Event During a recent turnaround at Mosaic's St. James Ammonia Plant, a plant incident during lire LTS reduction caused the pressure drop across the primary reformer to triple. Mosaic and Clariont Technical Services worked together to determine the calise of the primary reform er pressure drop increase and implement procedures to attempt salvaging the charge of reforming catalyst. This paper will discuss the troubleS/lOoting that was completed, remedial action attempted, safety precautions taken following lite sltutdown to make Slife the primary reformer and LTS were started back lip safely, and lessons learned. Euge ne Britton, P.E. Mosaic Fertilizer, LLC Kateryna Gliebova Mosaic Fertilizer, LLC Tim Rembold Clariant Introduction M osaic Fertilizer, LLC operates an ammonia plant at it s Faustina facility in St. James, Louisiana. The ammo- nia plant was built by M. W. Kellogg and com- mi ssioned in 1968 with a nameplate capacity of 1,000 STPD (907 MTPD). The ammonia plant has been modified in several stages to its current 2015 239 capacity of over 1,500 STPD (1 ,361 MTPD). The Faustina facility also manufactures ammo- niated phosphate fertilizers, including DAP, GMAP, and Mosaic's proprietary MicroEssen- tials® products. AMMONIA TECHNICAL MANUAL

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Root Cause Analysis of Incidents during L TS Catalyst Reduction and

Primary Reformer Coking Event

During a recent turnaround at Mosaic's St. James Ammonia Plant, a plant incident during lire LTS reduction caused the pressure drop across the primary reformer to triple.

Mosaic and Clariont Technical Services worked together to determine the calise of the primary reformer pressure drop increase and implement procedures to attempt salvaging the charge of

reforming catalyst.

This paper will discuss the troubleS/lOoting that was completed, remedial action attempted, safety precautions taken following lite sltutdown to make Slife the primary reformer and LTS were started

back lip safely, and lessons learned.

Eugene Britton, P.E. Mosaic Fertilizer, LLC

Kateryna Gliebova Mosaic Fertilizer, LLC

Tim Rembold Clariant

Introduction

Mosaic Fertilizer, LLC operates an ammonia plant at its Faustina facility in St. James, Louisiana. The ammo­

nia plant was built by M. W. Kellogg and com­missioned in 1968 with a nameplate capacity of 1,000 STPD (907 MTPD). The ammonia plant has been modified in several stages to its current

2015 239

capacity of over 1,500 STPD (1 ,361 MTPD). The Faustina facility also manufactures ammo­niated phosphate fertilizers, including DAP, GMAP, and Mosaic' s proprietary MicroEssen­tials® products.

AMMONIA TECHNICAL MANUAL

2014 Turnaround

The Mosaic Faustina Facility had a routine turn­around planned for the summer/fall of 2014 to perform scheduled maintenance, conduct re­quired inspections, and replace catalysts. Dur­ing this shutdown, the plant replaced catalysts in the desulfurization system, high temperature sh ift (HTS) reactor and low temperature shift (LTS) main reactor. The L TS catalyst required a reduction step before being placed into service. The plant did not replace the catalyst in the pri­mary reformer, which had been in service for three years.

L TS Reduction Safety Considerations

L TS catalyst is installed in the oxide form and requires a reduction at elevated temperatures and in the presence of a controlled amount of hydrogen to provide active copper crystals.

There have been numerous incidents in the past where hydrogen leaks in the system have caused L TS catalyst beds to reach temperatures above 1600°F (87 1°C), which is greater than the tem­perature ratings for most L TS catalyst vessels. If the catalyst bed temperature is allowed to ex­ceed 450°F (232°C), natural gas present during the reduction can crack, causing more hydrogen formation and a runaway temperature event[ I].

To prevent overheating due to hydrogen leaks good operating practices would include the fol­lowing:

• Blind off known hydrogen sources from the carrier gas loop

• Calibrate the hydrogen control valve at low temperatures to confirm the hydro­gen concentration going to the LTS reac­tor

• Monitor the inlet and outlet hydrogen content for the LTS reactor frequently

AMMONIA TECHNICAL MANUAL 240

• Monitor the thermocouples present to

the L TS bed continuously

Closely monitoring these data points will reduce the ri sk of damaging the LTS catalyst (which accounts for 36% of a typical ammonia plant's total catalyst cost) and prevent having to replace the catalyst vesse l [2].

Plant Startup and L TS Reduction

Mosaic began restarting the ammonia plant on August 30, 20 14 . Due to the configuration of LTS guard beds and the LTS main bed, the plant was able to begin ammonia production before the reduction process began for the L TS main reactor catalyst.

The LTS main bed reduction began on Septem­ber 4, 20 14. The reduction process was inter­rupted multiple times and was not completed until September 29, 2014.

The reduction was initially interrupted by a pro­cess upset and trip, which triggered a mechani­ca l fai lure in the process air compressor train. The process air compressor repairs led to a full shutdown of the ammonia plant, which stopped the L TS reduction.

After the process air compressor was repaired and while trying to finish the reduction, Mosaic and Clariant engineers determined that synthesis gas was leaking into the reduction loop, and t.hat the source was not inadequately isolated from the LTS guard beds, which were in service. Clariant's gas chromatograph indicated 0.5 mol% hydrogen flow leaking into the beds. Mosaic and Clariant discussed how to remove the hydrogen or control the hydrogen leak. Since this hydrogen ingress could not be con­trolled, Clariant recommended that Mosaic in­stall a blind to prevent hydrogen from the guard beds entering the reduction loop. Mosaic was removing the reduction carrier gas when a pro­cess trip occurred due to high air to gas ratio, leading to a full plant shutdown. When the

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plant tried to restart, the pressure drop across the reformer had more than tripled.

Mosaic and Clariant engineers quickly switched from supervising the LTS reduction to trouble­shooting and determining the root cause of the primary reformer pressure drop issue.

Troubleshooting

After the plant trip on September 15, 2014, Mo­saic was in the process of restarting the ammo­nia plant, but experienced difficulties introduc­ing process steam to the Primary Reformer. The steam flow into the catalyst tubes was severely restricted, with a very high pressure drop indi­cated across the primary reforming catalyst tubes. After several unsuccessful attempts to in­troduce the steam to the Reformer, Mosaic and Clariant suspected that coke may have been formed on the reforming catalyst during the shutdown event. Observation of the radiant sec­tion showed that over 50% of the tubes were bright red indicating low or no flow through them. As the pressure drop increases in some of the tubes of the reformer, a flow imbalance oc­curs in the reformer causing some tubes with low flow to be operated at higher than design temperatures, which could lead to a reduction of tube life. Conversely, the tubes with high flow rate have lower temperatures. The pressure dif­ferential on the Primary reformer was 130 psi (896 kPa), while the normal pressure drop was 35-40 psi (240-280 kPa). At this point, the deci­sion was made to start a catalyst decoking pro­cedure.

Primary reformer pressure drop increases are normally caused by physical degradation of the catalyst andlor coking of the catalyst. During unplanned plant shutdowns, there is a rapid con­traction of the reformer tubes causing a signifi­cant amount of physical stress on the primary reformer catalyst. If the stress is too large, the catalyst will physically crack leading to dust and catalyst chips obstructing the process gas flow through the catalyst. The pressure drop across

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the reformer increases due to the physical im­pediments in the tubes. For this reason, high crush strength is a key parameter for catalyst se­lection. At low steam to carbon ratios, coke will fonn on the catalyst. This will occur both on the surface and in the pores of the catalyst. The carbon wi ll expand at high temperatures which can also cause a loss of physical integrity of the catalyst (See Figure I). Depending on the se­verity of the coking event, coked up catalyst can potentially be reactivated through decoking pro­cedures.

Slight Coking Severe Coking with Physical

Damage

Figure 1. Reforming Catalyst Coking and Phys­ka/lntegrity

Clariant's catalyst decoking procedure with steam was implemented. The first step was to ens ure natural gas flow to the reformer was shut off. The steam flow was then introduced at 50% of design rate at atmospheric pressure. The re­fonner firing was adjusted to maintain an exit temperature of 1300-1400°F (704-760°C), while maintaining the tube wall temperatures below the maximum design limit. The steam decoking process was allowed to continue for 24 hours.

After steaming the reformer for 24 hours, there was no significant change in the primary re­former pressure drop. After consulting with Clariant and other catalyst suppliers, the deci­sion was made to attempt to remove the coke fonnation by using an air-steam decoking pro­cedure.

The air-steam decoking process is a last resort for trying to salvage severely coked catalyst pri-

AMMONIA TECHNICAL MANUAL

or to replacement. This procedure is similar to the steam decoking method mentioned earlier, but air is added to the process steam to intro­duce a maximum of 1 % oxygen in the reformer steam feed. The tube wall temperature and exit temperatures should be monitored to keep them within normal ranges. This procedure can be at­tempted for 12-36 hours.

The key control point for the air-steam decoking process is controlling the total amount of air go­ing to the reformer to avoid further damage to the catalyst or tubes due to overheating. Clariant recommended venting the air-steam mixture di­rectly after the Primary Reformer, but with the M. W. Kellogg reformer configuration it is im­possible to isolate the Secondary Reformer from the decoking process. A blind was installed at the HTS inlet and air-steam flow was routed to the vent upstream of the HTS vessel. The Sec­ondary Reformer temperatures were monitored very closely to prevent extreme exotherms.

The air-steam decoking began with the steam introduction; then air was slowly added at 0. 1 %. Throughout the process. air was increased up to 5% (- 1% 0 2). Hourly steam condensate sam­ples were collected from the inlet and outlet of the Reformer and the pH was measured to check the decoking progress. Carbon dioxide forms when carbon is reacted with oxygen during the decoking process. The carbon dioxide will be adsorbed in the steam condensate in the reform­er causing the pH of the steam condensate to drop. Monitoring the pH of the inlet and outlet steam condensate is a simplified way to monitor the amount of carbon removed from the catalyst during the decoking process.

AMMONIA TECHNICAL MANUAL 242

The air-steam decoking was continued for 12 hours, but there was only slight reduction in the pressure drop, making the operation of the unit impossible. At this point, Mosaic decided to end the decoking process and replace the catalyst.

The primary reformer catalyst was replaced with Clariant's ReforMax® 210 LDP and 330 LDP catalysts. Clariant provided two engineers to supervise the unloading and loading of the cata­lyst. The unloading process was longer than nonnal due to the physical degradation of the coked catalyst. The catalyst tubes also had to be cleaned out before loading the new catalyst charge. The primary reformer loading was suc­cessfu lly completed with all but three of the tubes within ±5% pressure drop variance.

Incident Investigation

After the high pressure drop in the Primary Re­former was discovered, an investigation was ini­tiated to determine the cause of the catalyst fail­ure . This process began with developing a time line and reviewing the process conditions leading up to the p lant trip and shutdown.

When carrier gas flow was removed from the LTS reduction loop the ammonia plant' s high air/gas ratio trip activated. (This trip activates at a ratio process air to process gas drops to 1.65 .) The process gas flow meter orifice and control valves are located upstream of the gas heating coils and desulfurizer. Because of this, the op­erators must adjust the indicated process gas flow to account for the carrier gas used for heat­ing or reducing L TS catalyst. (See Figure 2)

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Mosaic Faustina's Current Process Gas Configuration Process

Steam -

r Heating Coils and

FIC-l Orifice

Natural _ 0 _ I Gas -----1f---..~ l Desulfur izer

"- Primary Reformer

Feed FIC-la/lb

Hydrogen for

LTS Reduction

FI-57 Orifice

---II 8""8

~

0 FI-5S

F Orifice

LT5 Heat-up/ Carrier Gas

~L ____ , LTS and LTS

Guard Vessels

Figure 2. Current Configuration of Mosaic Natural Gas Flow to Primary Reformer and LTS Reactors.

After the initial trip, the operators twice reset the process air compressor and tried to reintro­duce air to the Secondary Reformer. Both at­tempts were unsuccessful as the plant tripped on high air/gas ratio each time. The loss of process air flow reduced the amount of steam generation in the waste heat boiler system. The decrease in steam flow caused the superheated steam tem­perature to rise, which led to a trip of the fuel gas to the superheat burners. Less than one mi­nute later. the Auxi liary Boiler shutdown when its low draft trip activated, which further re­duced steam production. At this point, the 550 psig (3,800 kPa) steam header pressure de­creased which reduced the flow of process steam to the reformer. When the ratio of pro­cess steam to process gas dropped below 2.8 the process gas trip activated, closing the process gas flow control valves.

After these events, the steam production was greatly reduced since the Auxiliary Boiler was down, no waste heat was being generated, and operators could not start the Startup Package Boiler due to Boiler Feed Water pump issues.

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A review of the process data indicated that the process gas flow control valves (FIC- l a/FIC- l b) were fully closed, but the process gas flow me­ter (FTC-I) continued to show a flow of 215 MSCFH for the next 2.5 minutes, suggesting that the valves were leaking through. During this time, sufficient steam was flowing to the re­fonner to maintain the steam/gas ratio above critical values; therefore, the catalyst should not have been damaged at this time. After 2.5 minutes, the process gas flow decreased from 215 MSCFH to approximately 9 MSCFH.

During this time, the 550 psig (3,800 kPa) steam header pressure fell below the process pressure. This condition prevented process steam from entering the Primary Reformer, due to the lack of differential pressure. The indicated steam flow leveled out at 19 Mlblhr, but this appears to be an erroneous indication. For the next 30 minutes the process gas flow meter indicated that there was a flow to the Primary Reformer of approximately 9 MSCFH, while there was no steam flow to the Primary Reformer.

AMMONIA TECHNICAL MANUAL

After 30 minutes, operators opened the front­end vent, which is located at the HTS reactor in­let. For the next 10 minutes , the process gas flow indication remained relatively stable. This action depressurized the process gas preheat coi ls and the desulfurizer through the Primary Refonuer. During this time, the process gas pressure remained above the steam header pres­sure, so the natural gas that was vented during this period passed through the refonuer with no process steam.

After several attempts, the Auxiliary Boiler was brought online. The 550 psig (3,800 kPa) steam header pressure started to increase and process steam began to flow to the Primary Refonuer.

The primary refonner catalyst had been exposed to natural gas in the absence of the steam for approximately 40 minutes, resulting in severe catalyst coking.

The process gas valves (which also served as emergency shutoff valves) were removed and sent to an outside repair shop for testing. The testing revealed that one of the valves was leak­ing through, allowing natural gas to leak into the process after the process gas trip occurred.

Root Cause Analysis and Lessons Learned

This incident began when the carrier gas flow used for L TS reduction was suddenly stopped resulting in the process air trip (due to high air to gas ratio). This trip started cascaded events

AMMONIA TECHNICAL MANUAL 244

which led to a full plant shutdown and damaged the primary refonner catalyst.

The carrier gas flow was stopped due to synthe­sis gas leaking into the L TS reduction loop. This could have been avoided by installing iso­lation blinds at all potential leakage points dur­ing a L TS catalyst reduction.

The location of the process gas flow orifice also contributed to the failure. Since the orifice is upstream of the carrier gas branch the ratios cal­culated for the process air and gas trips were in­accurate. This flow element will be relocated to downstream of the carrier gas branch to elimi­nate this issue.

The use of the flow control valves as shutdown valves was also a contributing factor. It was discovered that the control valves were Class IV leakage rated. These valves were replaced with Class V leakage rated valves. Also, as a tempo­rary measure, a motor operator was installed on the block valve upstream of the process gas con­trol va lves. On process gas trips, the flow con­trol valves will close, and the upstream block va lves wi ll be closed by the motor operator.

As a pennanent solution, dedicated shut-off va lves (in a double block and bleed arrange­ment) will be installed, with a dedicated flow measurement element. This system is being de­signed for installation at Mosaic's Faustina Ammonia Plant (See Figure 3).

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Natural Go> Feed

Mosaic Faustina's Planned Process Gas Configuration

FIC-la/lb

Hydrogen for LTS Reduction

f Heating Coils and l Desulfufizer

FI ·57 Orifice

II E>El

FI-S8 Orifice

"

Process Steam -

_Q,1_Q, ." Primary Reformer

FIC-! Orifice

LTS Heat-up/ Carrier Gas

LTSand LTS Guard Vessels

Figure 3. Planned Configuration of Natural Gas Flow to Primary Reformer and LTS Reactors

Current Performance

After the primary reformer loading was com­pleted, the L TS main bed catalyst was success­fu lly reduced and put on-stream. After the tum-

:Time

Production Rate. STPD

N G Feed, MSCFH 0/0 of R eported Proc. StealTl , L bs/Hr 0/0 of Reported C H4, Dry lTlo le% E xit Temperature, OF ATE OF S/G SIC DP M easured, Psig DP Ca lc ulated, P s ig

DP Ra tl 0 (Rep I c ale)

Flux. BTU/Hr-Fr

Cata lys t Type

around, the catalysts were both perfonning well. The pressure drop across the primary reformer was reduced by 26% from end-of-run to sta rt­of·run (See Table I) .

EOR SOR

1537 1589

1 3 11 .45 1 363 105.0 1 00.0

205,000 222,000 100. 0 100.0 13.23 1 3.65

1437 1427 6.6 12.5 3.29 3.43 3.26 3. 40 39 31

1 8.7 21 . 0

2.09 1 . 47 23. 503 24. 375

Corrpetltor Reforrvtax 210 Reforr.Aax 330

Table 1. SOR and EOR Performance of Primary Reformer at Mosaic

The L TS main bed perfonnanee also improved greatly from 0.22 mol % CO slip to 0.11 mol%

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CO slip with Clariant ShiftMax® 217 installed (see Table 2).

AMMONIA TECHNICAL MANUAL

Time EOR SOR

Production Rata , STPO 1537 1565

Inlet CO, % 0.44 0.49 Exit CO, % 0.22 0.11 Equil. CO, % 0.11 0.11 Conversion, % 66.1 98.9 ATE, of 69.2 3.3 Inlet Temp. , of 405 388

DT Measured, of 4.0 10.0 DT Calculated, of 3.0 8.5 DP Measured, Psig 12 B DP Calculated, Psig 7.5 7.4

DP Ratio r.:""/C.lcJ 1.60 1.08 DGSV, SCFH/Ft3 4970.6 5130. 1 Catalyst Type Corrpetitor ShiftMax 217

Table 2. SOR and EOR Peiformance oj LTS Main bed at Mosaic

Clariant and Mosaic expect both the primary re­fonner and low temperature shift catalyst to en­joy long lives.

AMMONIA TECHNICAL MANUAL 246

Conclusions

This incident resulted in significant losses due to both lost ammonia production and the ex­pense of replacing the primary reformer catalyst before its expected end of life.

Through cooperation and collaboration between Mosaic, and Clariant, the plant was able to de­termine the root cause of the refonner pressure drop issue and quickly replace the catalyst to al­low resumption 0 f ammonia production.

References

[ I] 1. Richardson, J. Wagner, R. Drucker, H. Rajesh, Uni1ed Catalyst, Inc., AIChE Ammonia Safety Symposium Meeting 1996. [2] P. Kumar, N. Ringer, Clariant, Nitrogen and Syngas Meeting 2015.

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