resolving intermittent vibration spikes on steam turbinesanalysis through experts helped early...

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Resolving Intermittent Vibration Spikes on Steam Turbines Rajakumar Thiagarajan Rotating Equipment Engineer Ashraf Abdelrahim Sr. Engineer Condition Monitoring Sankar Ganesh Lead MDS Engineer

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Page 1: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Resolving Intermittent Vibration Spikes on

Steam Turbines

Rajakumar Thiagarajan

Rotating Equipment Engineer

Ashraf Abdelrahim

Sr. Engineer Condition Monitoring

Sankar Ganesh

Lead MDS Engineer

Page 2: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Contents

• Background

• Machine description

• Data analysis

• Initial Analysis & Recommendations

• Machine Inspection results

• Subsequent Mechanical Failure Analysis

• Conclusions

• Lessons Learned

Page 3: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Background

Six Fresh Cooling Water Pumps:

4 Steam Turbines and 2 Motor driven pumps

Critical pumps in LNG production

Intermittent vibration spikes - Proactive detection on three

steam turbines using expert systems

The condition deteriorated and sporadic steam turbine trip.

Plant vulnerable to production loss

FCW

Tank

Sea

Water

Out

Sea Water

In

Make up

Pump A - F

Pump A - F

Schematic Diagram of Fresh Cooling Water System

Page 4: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Turbine Type: Back pressure (5 stage)

Bearings: Tilting pad

Seals: Mechanical Labyrinth

Coupling: Diaphragm

Power: 3840KW

Speed: 3602 RPM

Machine Description

PUMP

ST

Page 5: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Vibration is on the increasing trend and trips on high vibration

No correlation with the process parameters

Overall Vibration vs. Process data

Data Analysis

Green plot – Vibration Black, White, Red & Blue plots – Process parameters

Turbine vibration Process parameters

Page 6: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Abnormal Behavior – Significant Phase Angle

Change During Steady State (All Over 3600)

Data Analysis Cont’d..

Turbine NDE-X Turbine NDE-Y

Turbine DE-X Turbine DE-Y

Polar Plot – 1X Amplitude & Phase Angle

Page 7: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Flattened Orbit & Truncated Time Waveform due to Rub

Data Analysis Cont’d..

Direct Orbit Review During Vibration Excursion

Turbine NDE Turbine DE

Truncated Time waveform Flattened Orbit

Page 8: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Significant change in the Orbit Shape & Amplitude

(Change in Balance Condition Due to Thermal Bow)

Turbine NDE Turbine DE

Data Analysis Cont’d..

Direct Orbit Overlay – Comparison of Low & High

Vibration Amplitudes

Orange plot – when vibration is at minimum

Blue plot – when vibration is at maximum

Direct Orbit Becomes circular when

the vibration is at maximum

Page 9: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Thermal Bow Effect of Rub

High Spot

Heavy Spot 1X Orbit

1X Orbit

Rubbing Spot

Seal

A New High Spot

and Rubbing

Location

Increased

1X Orbit

W W

W W

a0 a0

a0

a0

Effective

Unbalance

mrW2 mrW2

mrW2 mrW2

Data Analysis Cont’d..

Page 10: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Phase angle change all through 360 degree

Data Analysis Cont’d..

Vibration Trend and Polar Plot – Reviewed for 2nd Steam

Turbine

Similar Behavior - Intermittent vibration Amplitude & Change

in Phase Angle

Intermittent vibration spikes

Page 11: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Phase angle change all through 360 degree

Data Analysis Cont’d..

Vibration Trend and Polar Plot – Reviewed for 3rd Steam

Turbine

Similar Behavior But Less Severity - Intermittent vibration

Amplitude & Change in Phase Angle

Intermittent vibration spikes

Page 12: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Initial Analysis & Recommendations:

Expert Analysts at site concluded the Rubbing Issue

is most likely due to

Carbonized oil buildup in the oil deflector / seal

area.

Recommended Action Items:

Inspect oil/steam seal areas for rubbing marks

due to deposit built-up / carbonized oil.

Page 13: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Machine Inspection Results

Carbonized deposits at NDE seal area

Oil Seal Area at Non Drive End Bearing of 1st Turbine

Rubbing Marks at the seal area due to oil carbonization is

evidenced.

Rubbing Marks on the shaft

Page 14: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Machine Inspection Results Cont’d.. Rotor Internals of 1st Turbine

No abnormalities noticed on the Rotor internal components.

Page 15: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Machine Inspection Results Cont’d..

Oil Seal Area at Non Drive End Bearing of 2nd & 3rd Turbine

Seal Area of 2nd Turbine Seal Area of 3rd Turbine

Oil Carbonization deposits and Rubbing Marks at the seal area

Based on the inspection results of 1st Turbine, no internal

checks carried out for the 2nd & 3rd Machines

Page 16: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Oil leak and migration to

steam end

Heavy Steam Leak from

steam gland

Carbonization Outside Operating

condition

Gland fins

clearance high

Ejector poor

performance

Sealing Air

pressure low

Breather

clogging

LO Supply

Pressure high

Design issue

Subsequent Mechanical Failure Analysis

Page 17: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Conclusions Primary Causes:

Low seal air pressure - Oil leakage, migration at steam gland

Contributed Causes:

Breather clogging - Oil leakage due to vapor accumulation

and high lube oil pressure inside the bearing housing

Design issues

Back pressure on the common return header - Wrong

elevation of breather on the Gearbox drain line

Oil shelter in close vicinity to the steam gland

Action Items:

Installed Pressure Gauge

Included breather cleaning task on the Equipment Strategy.

Modify the Breather elevation on the GB – being

implemented.

Page 18: Resolving Intermittent Vibration Spikes on Steam Turbinesanalysis through experts helped early detection of machine malfunctions. Findings on one steam turbine assisted to minimize

Lessons Learned Reduced Maintenance Cost and Down Time

Prognostic approach on the issues and accurate

analysis through experts helped early detection of

machine malfunctions.

Findings on one steam turbine assisted to minimize the

maintenance activities on other two steam turbines.

Presence of online diagnostic system helped to plan the

machine shutdown for the maintenance without impact

on the production.

Design issues – A lesson for future projects.

Absence of seal air pressure monitoring

Close vicinity of oil seal and steam gland

Wrong elevation of breather location on the Gearbox