problems faced & sug for improvement
TRANSCRIPT
OUR ACHEIVEMENTS .
Eco Bypass duct total ash was evacuated through the system , thus avoiding
ash dumping outside .
Both sources ( Fdr - 1 & 2) for Marshaling Box of Start Up XFMR -2 ,
UAT-3A/3B were fed from one section of Station ACDB . Now they are provided
from both sections I.e source - 1 from sec - A & source-2 from sec -B.
During boiler hydro-test the temp. of TB of MDBFP was going high after a
prolonged period of operation on recirculation . The FST temp was also going
high due to operation of the pump on recirculation . The TB temp was
brought under control by reducing the FST temp as fresh makeup was taken
to the system & hot water was drained .
MAJOR PTW'S ISSUED DURING THE PERIOD .
APRDS from Unit- 2 to Unit- 4 was isolated for attending the AS 169 valve
passing problem . During this time steam to St- II FOPH was not available ( 36
hrs)
St- II HFO temp had dropped From 90 deg C to 60-65 deg C ( For operating
Units 4/5/6 )
During 3UA 11 Kv bus Shutdown all the 9 compressor’s control supply were
fed from one Service Water XFMR .
Similarly 4 Compressors out of 9 compressors were fed from one Transfomer
during 3UA/3UB 11 kv bus isolation for O/H job .
During US SWGR- Sec B isolation the Power supply to 220 V DCDB is fed
through the DG set via EMCC via Ch- 2. Incase of problem in DG set the
DCDB is fed from Batteries Only .
Bat Ch- 1 is from USS Sec- B
Bat Ch- 2 is from EMCC/ USS Sec- B
Hence to avoid the above problem Bat Ch - 1 source to be changed to
USS Sec- A.
MAJOR PROBLEMS EXPERIENCED DURING RECOMMISSIONING .
AREA : BOILER & AUXILIARIES
During APH water washing the Zero meter area got flooded as the Hopper
Drains are not provided for the above purpose .
Also the duct & other equipment are getting damaged due to falling of acidic
water from the APH .
The Drain Back side of PA/FD fan is getting clogged with CHP coal as the
reject chute of CHP is just above the drain .
Operation of dampers at ESP inlet & outlet , ID fan inlet are unsafe as vertical
ladders are not provided with cage .
Mechanical isolation of HAG was difficult as they were not properly approachable .
AREA : TG & AUXILIARIES
CW water box vent/drain are connected to the same funnel causing problem
during draining .
Duct draining took more time as gravity draining facility is not there .
There is no valve provided for duct draining .
CW duct was drained by loosening the dummy flanges
Portable dewatering pump was not available from the beginning .
AOP starting during Oil flushing got delayed as it was tripping on Fire
protection .
TG ECW system drained thrice to attend the H2 cooler & other valves
problem .
Exciter Cooler Valve passing problem has caused water falling on the
Generator bus duct continuously . To avoid such problem proper dummy of the
line is to be done after removal of exciter cooler .
After Synchronisation of the unit even though the drain valves got closed on
torque setting & Close LS feedback has come , it was observed that the drain
temp. were maintaining HI . They were manually further tightened & torque
setting was increased .
While cleaning PHE of TG ECW/SGECW the water was falling directly on the
equipment's / panels at TG “0”0 Mtr as there is no proper drain provision .
AREA : ELECTRICAL SYSTEMS
Difficulty was experienced in Heating the water for CO2 filling by wood
burning .
TG Hall EOT crane was having only one power source from Unit- 3 SSSWGR -
Sec- A . When PTW issued on this section the entire day EOT crane was not
available . This has happened as the 2nd source envisaged was not
commissioned .
The SWGRS which O/H job can be planned in normal time were planned during
O/H period .
(Ex- ACMCC-5 /EACMCC-5 etc)
The Breaker /Equipment Module indication lamps were not made available due
to shortage of lamps .
MDBFP- C suction flow transmitters were behaving erratically causing tripping
of BFP in 2 occasions .
SUGGESTION FOR IMPROVEMENT .
All the pending defects of the unit before shutdown are to be compiled
system/equipment wise & to be included in the Maintenance job plan for their
liquidation during the overhauling .
Such points are to be closely monitored in the daily overhauling meeting .
Standby supply source for critical systems & equipment are to be identified
earlier & to be provided for issuing PTW on the respective SWGR .
Ex - Boiler Lift / EOT Crane /TG hall Lift /Lighting at various places .
Boiler inside lighting AC/DC to be taken from the source provided by EMD .
PM PTWs can be avoided during overhauling .
To Minimise Isolation & Normalisation the Elect PTW/ Mech PTW are to be
clubbed together as far as possible .
With in EMD the different groups can take the PTW simultaneously (
SWGR/XFMR/Relay testing etc)
PTW on equipment's to be taken on Sec wise such as LHS / RHS Ex -
ID/FD/PA fans - A first & then - B . Also the LOP’s to be cleared by all the
Dept , So that The recommissioning activities can start in a phased manner.
Temporary dewatering pumps in condenser pit to be commissioned before unit
S/D.
Proper Approach to CT area Riser main valves & lighting to be provided to do
the necessary isolation & normalization in the Night
Proper Approach / illumination for SW Blow-down / Chlorination Plant water line
valves near CW ICV are to be provided to carry out the operation in the
Night .
MODIFICATIONS REQUIRED FOR IMPROVEMENT .
Gravity draining facility for CW duct as well as water box ( ref the sketch). This will reduce the drain timings of duct to a larger extent .
The sump pit pump discharge is to be staggered to avoid the overflow of drain at “A” Row .
Permanent power supply source for temporary dewatering pump in the Condenser pit .
BA I/O panel 3rd supply source to be provided for giving PTW on Bus coupler panels , (BAMCC/BMCC etc).
If Unit-3 BA I/O panel supply fails then the other units 4,5,6 PLC communication also fails .
ARV at end of Riser Main hdr at CT Area for duct charging & Draining .
Separate Drain system for Eco Ash Hopper during 2nd pass water washing . ( As discussed for APH Hopper system)
Tapping points from FH line at Eco bypass Hopper area for hopper & duct cleaning.
Power supply for Unit- 3 Lift & inside lighting are from different source ,to be provided from same source /same swgr .
2nd source for Chimney /Aviation Lighting (Now from Unit- 3 ESP Board - C) Permanent Dewatering power supply source for the CT Basins from
the Adjacent Units so that Cold Basin dewatering & subsequent cleaning will not be affected when CTMCC goes under PTW.
To avoid wood burning & heating the water for CO2 purge any one of the following may be provided .
Hot water header having connection from all the units . Provision of steam heating .
APH water wash line strainers are located in an inaccessible location , to be modified .
CONDENSER
Water Box Drain
Condenser Inlet side
Drain
Condenser Outlet side
Drain
Existing “C “ Row Drain
Existing “A “ Row Drain
VentVent
Floor Level
-ve Mtr Floor
Proposed Modification
PAPH-A HOPPER-1
PAPH-A HOPPER-2
Proposed drain hdr to boiler "0" mtr Drain
line with gradient .
150 nb Botterfly valve
Proposed APH hopper drain
line