fsrug meeting, january 25-28, 2016 san antonio, txfsrug.org/presentations2016/7.pdfbearing rather...
TRANSCRIPT
FSRUG Meeting, January 25-28, 2016
San Antonio, TX
Heater Drain Pump Issues
Presented by:
Mark Barber, Rotating Equipment Repair
Chris Packard, DC Cook
Subject Pump
Subject Pump
Ingersoll Rand 8 X 23 PH
1780 RPM
2 Stage
Subject Pump
The Coupling
Subject Pump
Pump History
Design Modification
• CE bearing housing changed in 2002 to incorporate sealed roller
bearing rather than babbitted journal bearing.
• This was done to minimize oil leakage.
Pump History
• TE bearing housing changed in 2002 to incorporate sealed roller
bearing rather than babbitted journal bearing with integral Kingsbury
thrust bearing.
• Done in effort to minimize oil leakage.
Pump Failures/Timeline
• A series of failures occurred:
• February, 2015: Planned 10-year maintenance performed.
• Rotor only sent out for refurbishment. Shaft replaced.
• Installation went well; turned freely on 3/26 at ambient temperatures.
• On 3/29, mechanical binding occurred during “hot alignment” checks.
• April 9, 2015: Pump disassembled. IB 2nd stage case ring bound to impeller ring
(“curl of metal”). Rotor sent to vendor.
• April 15, 2015: Vendor recommended opening up case ring to impeller running
clearances from 0.015-0.020 to 0.033-0.035 to alleviate binding issues.
• April 20, 2015: Pump assembled; rotated freely at ambient temperatures.
• A rub was noticed at a single point during “hot alignment” checks.
• April 27-28, 2015: Pump coupled and “bump checked” for rotation. Appeared to
rotate freely. On the night of 4/28, it was “aligned for its PMT tripped on a Low-
Low heater level transient.” The pump was reset. Subsequent effort to start
pump tripped motor on high amps with no flow/pressure observed.
• April 30, 2015: Entire pump removed and sent to Rotating Equipment Repair.
• Upon disassembly, it was noted:
• The shaft was made from AISI 4340 (low alloy steel).
• The case rings’ od’s were slightly pinched in their respective fit bores.
• The OB sleeve and nut had galled within its respective bushing.
• Impeller wear turn(s) had picked up galls to respective case rings.
• Shaft sleeve keyways were “end-milled.”
Disassembly Facts
Repair Plan Development
• Resultant repair plan was based on following facts:
• Due to rubbing evident more so on one end of pump, casing ring receiving
bores were suspected to be non-concentric in casing (not a singular rotor
centerline).
• Casing fits to respective stationary components were found to be out of
specification.
• As always, component materials were verified and some peculiarities were
found with the shaft. Shaft run-out necessitated its replacement.
• Impeller wear turn rubs necessitated their refurbishment.
• Bearing carrier was out of spec and required replacement.
• Shaft sleeves were replaced; keyways were milled for full key engagement.
Pump Upgrades
• A series of upgrades were implemented:
• New shaft was manufactured of martensitic SS rather than AISI 4340 as found.
• The following items were laser welded with 420 SS per ASTM B815 (450-560
BHN):
• Impeller wear turns
• Intermediate sleeves
• Shaft sleeve nuts
• New case rings manufactured from hardened 420 SS; running clearances
restored to 0.018-0.020”.
• Casing joint ground; fit bores machined concentric to one another.
• Gib blocks were manufactured for outboard end of pump casing.
The Smoking GunStarring (in alphabetical order):
• Coupling/Alignment
• Bearing Housing Design Changes
• Procedures
• Shaft Material
• Trust
• Actual coupling data states coupling can tolerate up to
0.115” radial misalignment. However, do not be fooled
into allowing excessive rim misalignment. To be sure,
install “Permalign” type laser alignment devices to
record operating temperatures vs. cold for use in
vertical rise. MINIMIZE HOT ALIGNMENT!!!
The Coupling
• Rotating Equipment Repair was brought on site to supervise the installation
and alignment of the pump.
• Soft foot checks were performed; shims were used to make corrections,
taking into account any thermal rise considerations.
• The inboard end of pump casing was put on existing dowel pins; inboard
end hold-down bolts were fastened.
• This resulted in bolt-bound condition of outboard end casing hold down
bolt holes.
Alignment
CE
DISCHARGE
SUCTION
TE
AS-FOUND ON-SITEJOB #: 20150186CASING HOLD-DOWN STUDS
ROTATING EQUIPMENT REPAIRW248 N5550 EXECUTIVE DRIVESUSSEX, WI 53089
BOLT-BOUNDCONDITION
Alignment
• INCLUDE ACTUAL DATA FROM CHRIS PACKARD!!!1
2
3
4
6 7 8
10
9
Drawing Pt. 1 2 3 4
Front Right 106.4 132.4 228.6 244.3
Front Left 102.2 132.4 191.2 205.4
Back Right 111.4 135 207.6 229.4
Back Left 103 114.4 175.6 249.8
AVE 106 129 201 232 167
Pump Support Leg Temperatures Drawing Pt. 6 7 8 9 10
Left 115.2 167.2 107.8 129 110
Right 114.8 155.6 106.2 126.8 110.6
Center
AVE 115 161 107 128 110
AVE (6-8) 128
OVERALL AVE 122
Motor Temperatures
Alignment
Thermal Rise Equation
ΔL = L * αL * ΔT
Pump
ΔT = 77°
ΔL = 18” * 5.6x10-6 * 77
ΔL = 0.0077”
Motor
ΔT = 32°
ΔL = 18” * 5.6x10-6 * 32
ΔL = 0.0032”
Therefore, set pump approximately 0.004” lower than motor.
• Alignments critical for proper pump and motor longevity.
• Thermal rise calculation
• The pump support is very well-ventilated; nearly centerline-mounted.
• Motor is well-ventilated.
Bearing Housing Design Changes
• Intent was to eliminate oil leaks and thus increase pump reliability.
• It is unclear whether MTBF has increased or decreased due to change from
babbitted journal bearings to ball bearings. The design change uses sealed
bearings, so there is a finite life expectancy of the bearings versus properly
designed and lubricated babbitted bearings.
Procedures
Pump
Number
Noun
Name RPM
Target Vertical Offset [Ref 7.2.1j]
Horizontal
Offset
Horizontal/ Vertical
Angularity
T 1-PP-22N
T 1-PP-22M
T 1-PP-22S
T 2-PP-22N
T 2-PP-22M
T 2-PP-22S
Heater
Drain 1780
WHEN Casing temp is <100°F,
THEN align Motor Shaft
0.005 to 0.009 high
WHEN Casing temp is
100°F to 250°F (Unit 1) OR
100°F to 200°F (Unit 2) Do Not perform alignment
WHEN Casing temp is
>250°F (Unit 1)
OR >200°F (Unit 2), THEN align
Motor Shaft 0.000 to 0.004 high
-0.001" to
0.001"
-0.002" to
0.002"
• Confusing procedure.
• Unless there is no alternative, NEVER PERFORM ANY HOT ALIGNMENTS!
Shaft
• Previous vendor made design change proposal to AISI 4340
• IR spec called for .12 chrome
• Coefficient of thermal expansions
• AISI 4340 13.6x10-6
• .12 chrome 5.6x10-6
• Practically this dictates that for a 250° ΔT
• AISI 4340
• 250 x 13.6x10-6 = 0.0034”
• .12 chrome
• 250 x 5.6x10-6 = 0.0014”
• Creates potential for impellers/sleeves becoming interference fit when that is
not intent of design. Face runout can then be accentuated putting the shaft
in a bow. Loose fits, as intended, allow for bore to face runout issues being
minimized.
Trust
• Just because a repair has been specified, best to “trust but verify.”
• Is pump casing machined as specified?
• To check in place, affix a precision bar, mounted in bronze bushings, to ends of casing.
• Align best possible to stuffing box bushing receiving bores.
• Using dial indicator, sweep each stationary component receiving bore to verify
they run concentrically with one another.
• Any run-out effectively reduces running clearances.
Bad Actor?
Who was the “bad actor?”
In order of influence on failure:
1. Alignment. Bolt bound condition of OB pump mounting feet
holes.
2. Procedure: HOT ALIGNMENTS
3. Trust. Verify that what you had specified work scope to be is
what you received. Scrutinize vendor design changes
carefully. They may be a good idea; they may not.
4. Shaft material. This relates to #3 above.
5. Bearing housing design changes.