energy quality and yield improvements in alkylationmeaning loop health %e 25.29 15.42 -9.9 70 –...

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5/18/11 1 Energy Quality and Yield Improvements in Alkylation DH Lee APST Inc. Biography APST is Advanced Process Solutions & Technology Started in 2007.1 To provide the best advanced process solutions and tech. Partners Expertune Inc. (www.expertune.com ) Tips Inc. (www.tipsweb.com ) Clients – Operations: Hanwha Chemical, Samsung Fine Chemicals, SK Energy, POSCO, Cheil Ind., Hyundai Oilbank, Honam Petrochemical, GS Caltex, Etc. Eng. & Etc. Samsung Electronics, Daewoo Eng. Doosan Heavy Ind. Etc.

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Page 1: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

5/18/11

1

Energy Quality and Yield Improvements in Alkylation

DH LeeAPST Inc.

Biography

• APST is Advanced Process Solutions & Technology– Started in 2007.1

– To provide the best advanced process solutions and tech.

• Partners– Expertune Inc. (www.expertune.com)

– Tips Inc. (www.tipsweb.com)

• Clients– Operations:

• Hanwha Chemical, Samsung Fine Chemicals, SK Energy, POSCO, Cheil Ind., Hyundai Oilbank, Honam Petrochemical, GS Caltex, Etc.

– Eng. & Etc.• Samsung Electronics, Daewoo Eng. Doosan Heavy Ind. Etc.

Page 2: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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2

Success StoriesClient DCS Benefits

Hanwha Chemical

Yokogawa

D3,

Honeywell

�VCM Plant – Process Stabilization, Energy Savings (2007.9)

�PVC Plant – Increased Safety Margin 50% ,3% Production Increase (2008.4)

�New Plant Stabilization of Oxy4/CA4 (2010.1)

�VCM Plant Energy Savings, 2% Energy Usage & US$ 2M Savings/Yr (2010.11~2011.3)

Samsung Fine Chemicals Yokogawa �ECH/PTAC Process, 5.4% Energy Savings at Distillation Column (2007.10)

SK Energy Yokogawa �Process Stabilization, Reduced Alarm 90% (2008.1)

POSCO Yokogawa �3% Fuel Savings by Excess O2 Optimization and NOx control at a Power Plant (2009.5)

Cheil Ind. Honeywell �Energy Savings at PC Plant , 5.5% Savings by Stab. and Opt. ( US$ 900K/Yr, 2008.7)

Hyundai Oilbank

Yokogawa,

Yamadake,

Emerson

�Whole BTX Plant Energy Savings, 4% Energy Usage ( > US$ 2.5 M/Yr, 2009.3)

�Installation Control Loops Monitoring System for the site ( US$ 1M/Yr, 2009.10)

�New Plant Stabilization of #2 HOU & Installation PlantTriage System (2010.9~ 2011.5)

Honam PetrochemicalHoneywell,

Yokogawa

�Energy Savings at PC Plant, 2% Energy Usage (2009.9)

�Energy Savings at BTX Plant, 2% Energy Usage (2010.3)

�Energy Savings at DMC, EG Plant, 2% Energy Usage (2010.7)

�Energy Savings at #3EG, MMA Plant (2010.11 ~’11.2)

�Expanding to other plant (2011.3 ~)

GS CaltexHoneywell,

Yokogawa

�Energy Savings at Alkylation & #3 Xylene unit, Energy Savings > 2%, (2010.3)

�New Plant Stabilization of VHCR (2010.8)

�Energy Savings at #2KD,Energy Savings >2%, (2010.11)

Abstract

• By applying PlantTriage and improving their efficiency could save average 2% energy usage in plant in Korea. It shows our approaches, procedure and results in Alkylantion.

Page 3: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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PlantTriage Usage In Korea

New Plant <Process

Stabilization)

• PID Optimization• H/W Issue

Diagnosis & Monitoring

Existing Plant<Performance Management>

• Control System KPI Management

• PID Optimization• H/W Performance

Monitoring

Setting KPI, Baseline & Thresholds

PlantTriage is …� Control System Performance Monitoring &

Management

� Collect real-time data from DCS/Historian, Store, Analysis and Report System

� Detect Control Performance issue & Efficient tool to solve the issue� H/W Issue : Valve, Sensor status, Size issue� S/W Issue : Tuning problem, Interaction issue, APC

performance� Root cause analysis� KPIs management� PID Optimization

KPI Trends of “A” Plant

Control System KPI Mng.

Real Time Data Collection / Store / Trend

Assessment / Analysis

Interaction Analysis

PID Optimization / Simulation

PlantTriageEtc.

Page 4: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Working Procedure

7

Control Loop Control Loop Control Loop Control Loop AssessmentAssessmentAssessmentAssessment

PID Tuning PID Tuning PID Tuning PID Tuning

& Logic & Logic & Logic & Logic ImprovementImprovementImprovementImprovement

Process Process Process Process OptimizationOptimizationOptimizationOptimization

Performance Performance Performance Performance MonitoringMonitoringMonitoringMonitoring

Steam

Reflux

DT

Impurity

UR

Setting Up Setting Up Setting Up Setting Up BaselineBaselineBaselineBaseline

Profit Profit Profit Profit CalculationCalculationCalculationCalculation

Key factors• Install PlantTriage first

– Set up with basic control information– PlantTriage gives some hint for improvement

• Tuning Issue / Hardware Issue / Process Characteristics / Operator Actions & etc.

• Setup Baseline – Set up baseline of energy usage, unit cost, product rate, loop health etc.

• Start from easy things– Tune PID parameters– Fix H/W problems as possible– Become a friend with operators

• Try to solve their trivial work / Listen their ideas / Include them as project member

– Analyze process for optimization• Use process simulator or data mining tool

• Make monitoring environment– Update PlantTriage configuration (Monitoring items, Baseline & Thresholds, Report

format and etc.)

• Report with benefits

Page 5: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Alkylation Unit

ReactorSystem

RefrigerantSystem

iC4 Makeup

DeC4

Olefin Feed

DeC3 Charge

Propane

DIB Bottoms

Reactor Effluent

DeC3

Refrigerant

DIB

iC4 Recycle

Butane

DeC3 Bottoms

DeC5

Alkylate

Pentane

Alkylation Reaction Mechanism

10

Page 6: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Control Loop KPIs

11

Before Improvement

(3/1~15)

After Improvement

(5/5~16)

Difference(Improvement)

Ref. Korean Companies

Meaning

Loop health %E 25.29 15.42 -9.9 70 – 100↑Overall

Performance Index

Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

Not In Normal , % 12.91 9.253 -3.7 About 30% Usage

Avg abs error, % 0.4026 0.4142 0.0 2Controller

Performance

Actions for Improvement

12

Flash Drum Level-Refrigerant Recycle

Temperature Control (Manual -> Auto), DeC3 #38

� Increase Controller Usage

Page 7: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Actions for Improvement

13

Temp Control : New(Manual -> Auto), DIB #58

� Install a New Controller � Build Soft Sensors

Alkylate RON

Alkylate RVP

Alkylate D90%

#1 (A) 84.7 +0.462345*156IO_ 2010-05-18 09:53:25 22.91 (Firs t @1 Min) No Description Defined**#2 (A) 156ai009.pv*6.894757 2010-05-18 09:53:25 17.04 (Snapshot @1 Min) No Description Defined**#3 (A) LAB_ALKY_ALKYLAT E_RVP 2010-05-18 09:03:10 25.90 KPA (Snapshot @1 Min) Alkylation Alkylate R/D RVP(NIR)**

35.00

15.00

35.00

15.00

35.00

15.00

2010-03-19 10:23:10 2010-05-18 10:23:10

New Plot T itle @ 60d0h0m0s

Actions for Improvement

14

Inferential

Analyzer

Lab_NIR

Reduced RVPVariation

�Alkylate RVP Inferential vs. Analyzer

Page 8: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Results

15

� KPIs Trend

Results

16

� Improved Process Conditions

Stabilized I/O Ratio Unformed Reaction Temperature (Contactor’s DT)

“0” Delta T

Page 9: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Results

Propane Purity % in DeC3 OVHD Propane

IC4 in NC4 / NC4 in DeC5 OVHD

� Increased Product Quality

Results

Alkylate

NC4

Propane(By product)

� Increased Product Rate

Page 10: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Results

19

Feed

Steam Usage

Iso C4 Makeup

� Reduced Steam Usage

ResultsBenefit Evaluation Sheet BaseBaseBaseBase EvaluationEvaluationEvaluationEvaluation GAPGAPGAPGAP

Period '10 03.01~03.15 10 05.01~05.11Average Operating Conditions

Contactor Temperature, °CIsobutane/Olefin Volume Ratio -0.3 Isobutane Content of Recycle, vol %Spent Acid Concentration, wt %

Fresh Feed Olefin Feed, FC001+FC506 -0.3 IC4 Make-Up, FC038 3.6

Average Fresh Olefinic Feed Composition of Olefins, vol %PropyleneI-Butane 0.1

1-Butene 2.0 Average Fresh Feed Characteristics

Mercaptan Sulfur, ppm (wt)Total Sulfur, ppm (wt)

Average Yield Composition of Product, vol %Propane -0.1%I-Butane 2.1%Alkylate 1.9%

Average Yield Composition of Product, Kl/hrPropane -0.1 I-Butane 1.4 Alkylate 1.2

Average Alkylate QualityOctane Number, RON -0.1 Reid Vapor Pressure, PSI 2.1 ASTM D-86 90% Distillation Point, °C

Utilized Capacity, KL/HrEnergy Consumption, Ton/Hr

Depropanizer, LP -0.1 Deisobutanizer, LP 0.4 Debutanizer, MP -0.2 Depentanizer, MP -0.2

sumsumsumsum -0.1 Refrigerator Compressor, HP

� Benefit Evaluation

Note: Benefit Calculation is skipped here

Page 11: Energy Quality and Yield Improvements in AlkylationMeaning Loop health %E 25.29 15.42 -9.9 70 – 100 ↑ Overall Performance Index Valve Travel, % /Day 2392 1380 -1,012 > 2000 % Stability

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Results & Conclusions

• Business Benefits– ROI was normally less than 2 months– Average energy savings was 2% by

improving control performance

• Technical Benefits– PlantTriage says

• What happen in your plant operation• What to do next

Questions?