comparative seawater ro pretreatment evaluation using ... c/comparative seawater ro pretr… ·...
TRANSCRIPT
International
Desalination
Association
“Desalination: The Vision of Today and the Future”
Kader Gaid, Technical Department Veolia Water
Michel Canet, Executive Vice president,Veolia Water
Solutions & Technologies
Keith Craig, Techinal Manager Veolia Water Australia
Comparative Seawater RO Pretreatment
Evaluation Using Existing Plant and Pilot Plant
4 March 2009
4 March 2009
The pre treatment : The key of the success
4 March 2009
Turbidity< 0,5 NTU SDI < 4 No oxidant Low residual metal (Fe, Al) Low organic carbon content No algae cells Low particles counts
Objectives of the Pre treatment
4 March 2009
Mediterranean Sea
Turbidity: 1 – 10 NTU
TOC: 1- 3 mg/L
Algae
T°C : < 27°C
Estuary Europe
Turbidity : 50 NTU
TOC : 20 mg/l
Colour : 50 mg/l Pt/Co
T°C < 20°C
China Sea
TOC: 2- 4 mg/l
Algae
T°C : < 27°C
Turbidity < 5 NTU
TOC < 2 mg/l
T°C < 25 °C
Oman sea & Persic Gulf
Turbidity: 2- 15 NTU
TOC: < 3 mg/L
T°C : 15 – 35°C
algae
Turbidity < 5 NTU
TOC < 2 mg/l
T°C < 25°C
4 March 2009
Pre treatment design and evaluation for three plants
• Oman Sur (Sultanate of Oman) : Beach well
• Gold Coast (Australia) : Open intake
• Fujairah (UEA) : Open intake
1. Case of Oman Sur
BW Flow rate pumped m³/d 187 617
1. Case of Oman Sur Plant
The plant nominal capacity shall be 80 200 m³/d
33 beach wells split up into 3
areas corresponding to 3 main
underground water incomes
Piping network length of ~4000m
Wells yield 70 & 100 l/s result of :
best optimization
(OPEX/CAPEX)
limitation of equipments type
number
Water quality
parameter
New
BW-
6
BW-1 FW-1 BW-2 FW-2 BW-3 FW-3
SDI-15min (Millipore HAWP membrane)
0.8 1.3 0.5 – 0.6 0.8 0.9 0 -0.6 -
pH 7.4 7.4 7.4 7.3 7.3 7.3 7.3
TOC (mg/L) 0.67 < 0.5 0.5 0.79 0.5 < 0.5 0.81
Total Nitrogen (mg/L) 0.21 0.15 0.12 0.30 0.26 0.27 0.25
Total UV254 (/m) 0.83 0.74 0.72 0.86 0.78 0.65 0.81
Total Hydrocarbons (mg/L) < 0.1 < 0.1 < 0.1 < 0.1 < 0.1 < 0.1 < 0.1
1. Case of Oman Sur : Raw water quality
0
5
10
15
20
25
30
35
Abu Dhabi
(March -
June 2004)
Perth (Dec
2004)
Toulon (2005
- 2007)
Ashkelon
(2005-2006)
Carboneras
(Sept 2005)
Sydney (Aug
2006 - Feb
2007)
Sur, Oman
(Jan 2006)
Sur, Oman
(April 2007)
Koweit
(March 2007)
SD
I-3
min
1. Case of Oman Sur : Comparative SDI
1. Case of Oman Sur: Beach wells implementation
Optimized general layout
1. Case of Oman Sur : Beach wells pumping
Simple Filtration mono or dual media
Anti scalingFiltration
Cartridge
Filters
HP Pumps
RO Membranes
reminéralisation
Chlorination
treated water
tank
Shock
chlorination
• No Coagulant
• No acid
• No sludge treatment
3 existing plants working on the same
site does not use chemicals for the
pre treatment
• Shock chlorination
• Chlorine injection upstream of the seawater pumps is done in
order to control sea shell growth and sea flora.
• The chlorine is injected as chlorine solution which is
prepared by means of NaOCl.
Prechlorination type Shock treatment
Dose mg/l 2
Frequency 1 h / day
NaOCl solution concentration % 12.5
Cas of Oman Sur : Chlorination of the inlet
1st stage filter criteria
Feed Filter Flow rate m³/d 61,675
Number of Filters
Horizontal pressure filters
6
Dual Media Filtration pumice media -
Sand
600 mm
600 mm
Diameter of the filter m 3.50
Surface of a filter m² 42
Filter Cycle h 48
Filter velocity m/h 10.2
Feed Filter Flow rate m³/d 125,942
Number of Filters
Horizontal pressure filters
8
Filter velocity m/h 15.6
MonoMedia Filtration Sand 600 mm
Case of Oman Sur : Filtration
II nd stage filter criteria
Case of Oman Sur : Filtration
Case of Oman Sur : view of the pre treatment
The Gold Coast Desalination plant has been constructed as a part of
the Queensland State Government’s $9 Billion South East Queensland
Water Grid Strategy. This Strategy has been developed in response to a
growing population and unprecedented drought, which has seen the
region’s water storages fall to below 20% of capacity.
The project is a Design, Build and Operate contract with a fifteen
year operations and maintenance period.
The Alliance style project includes the delivery of a 125 ML/day
Seawater Reverse Osmosis plant, and the construction of two tunnels 2.0
and 2.2 kilometers long. 24.5 kilometers of delivery pipework has also
been constructed to connect the desalination plant to the SEQ Water
Grid.
2. Case of Gold Coast Desal Plant
The pipeline runs 24.5 kilometres from Tugun to Worongary
and connects to the South East Queensland Water Grid
Units Range
Nominal
capacity
m3/day 125,000
Annual
volume
m3/year 45,656,250
Plant
availability
% 94
Operation Day/year 343
Design
capacity
m3/day 133,000
4 March 2009
Parameters (Gold Coast Desal Plant)Units Range / Max value
Seawater design temperature Deg C 17 – 28
Seawater total dissolved solids design values mg/L 34,000 – 38,000
pH 7.6 – 8.3
Total suspended solids mg/L 10
Turbidity NTU 7
Bicarbonate as HCO3 mg/L 160
Carbonate as CO3 mg/L 30
Chloride as Cl mg/L 21,000
Sulphate as SO4 mg/L 3,000
Fluoride as F mg/L 1.8
Bromides mg/L 76
Dissolved hydrocarbons mg/L 0.10
Total organic carbon mg/L 4
Calcium mg/L 450
Magnesium mg/L 1,450
Sodium mg/L 11,700
Boron mg/L 5
Red tide in Gold Coast
Map of EPA
sampling locations.
• The pre-treatment pilot plant was constructed and
installed at Kropp Park at Tugun Beach.
• The pilot plant is a granular media filtration system that
can operate in contact or direct filtration mode.
• The seawater intake is located 1.5 km offshore from
Kropp Park in 24 m of water.
• The pre-treatment pilot plant and intake was
commissioned the week of the 4 September and runs
commenced week of 12 September 2006.
2. Case of Gold Coast DP : Pilot Plant
Parameter Value
Flocculation time 20 mins
Flocculation G value 75 sec-1,
Filtration rate 6.7 m/hr
Filtration time 29 hrs/31 hrs
Ferric Sulphate Dose Rate 6 - 18 mg/L
Cationic Polymer (LT 425) 0 – 0.21 mg/L
Coagulation pH 6.7
Filter Media
Sand / Australian filter coal
0.7 mm E.S. - depth 900 mm
1.5 mm E.S. - depth 800 mm
2. Case of Gold Coast : Pilot plant design
GCDA Pilot Plant
Raw Water SDI3, Filtered Water SDI15 after 5 hours, Chemical Dose Rates
0
5
10
15
20
25
30
0 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27
Run Number
SD
I3, F
err
ic S
ulp
hate
Do
se R
ate
(m
g/L
)
0
1
2
3
4
5
6
7
8
9
SD
I15
, C
at
Po
lym
er
Do
se R
ate
(m
g/L
)
Raw Water SDI3 Avg Ferric Sulphate Dose Rate (mg/L)
Avg Polymer Dose (mg/L) Filtered Water SDI15 after 5 hours
Fe2(SO4)3 =12-18 mg/L; pH =6.7 ; Filter Rate =6.7 m/hr; Cat Poly = 0.2 mg/L; Floc Time = 20 mins
0.0
1.0
2.0
3.0
4.0
5.0
6.0
0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30
Operation Time (Hours)
SD
I
0.00
0.05
0.10
0.15
0.20
0.25
0.30
Tu
rbid
ity (
NT
U)
SDI F1 Turbidity F1
Fe2(SO4)3 =12-18 mg/L; pH =6.7 ; Filter Rate =6.7 m/hr; Cat Poly = 0.2 mg/L;
Floc Time = 20 mins, Direct Filtration
0.0
0.3
0.5
0.8
1.0
1.3
1.5
1.8
2.0
2.3
2.5
0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30
Operation Time (Hours)
dP
(m
)
0.0
4.0
8.0
12.0
16.0
20.0
Ch
em
ica
l D
ose
Rate
s (
mg
/L)
DP F1 Ferric Dose Polymer Dose
Fe2(SO4)3 = 6-14 mg/L; pH =6.7 ; Filter Rate =6.7 m/hr; Cat Poly = 0 - 0.2 mg/L;
Floc Time = 20 mins, Direct Filtration
0.00
0.50
1.00
1.50
2.00
2.50
3.00
3.50
4.00
4.50
5.00
5.50
6.00
0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30 32
Operation Time (Hours)
SD
I15
0.0
4.0
8.0
12.0
16.0
Ch
em
ica
l D
ose
Rate
s (
mg
/L)
SDI15 Ferric Dose Cationic Polymer Dose
After 11 weeks testing the seawater SDI3 values have varied
from 11.5 to 25.2.
After the filter run is allowed to mature to filtered water SDI15
values around 3.0 through high doses of chemical coagulants,
the filter bed appears to reach a stabilisation which allows
chemical dose rates to then be decrease.
The direct filtration process at a filtration rate 6.7 m/hr has
proved effective with filter run times >40 hours. Results to
date indicate direct filtration at a filter rate of 6.7 m/hr with
a flocculation time of 20 minutes achieved suitable SDI15
values and filter run times.
Gold Coast Desalination water Treatment
coagulant
Floculant
acidantiscalant
Cartridge
filters
Dual media
filter
High
pressure
pumps
membranes
Remineralisation
Final
chlorination
Treated
water
CO2, Lime water
2. Case of Gold Coast :Flocculation tank sizing
19.9minResidence time 4 units
1,178m3Volume per unit
3uNumber of tanks in
series per unit
4uNumber of unit
345,394m3/dFilter feed water
Flocculation
19.9minResidence time 4 units
1,178m3Volume per unit
3uNumber of tanks in
series per unit
4uNumber of unit
345,394m3/dFilter feed water
Flocculation
119.3m2Filter area
Sand + Anthracite
Filter type
Dual media gravity filter
18uNumber of filter
119.3m2Filter area
Sand + Anthracite
Filter type
Dual media gravity filter
18uNumber of filter
1600mmTotal Height of media
layer
1600mmTotal Height of media
layer
6.6m/h
Filtration rate
- 18 filters (N) 6.6m/h
Filtration rate
- 18 filters (N)
2. Case of Gold Coast :Filtration design
13% (130 g/L of active
chlorine)
0 to 10 as active chlorine
Inlet of the intake pipe,pumping orDischarge pipe of the intake pumps
Concentration
Dosing rate
mg/L
Frequency
Injection point
NaOH
Liquid
1h/day
Concentration
Dosing rate
mg/L
Frequency
Injection point
NaOCl
Liquid
98%
35 maxi
Continuous
Static mixer prior
pre treatment
Concentration
Dosing rate
mg/L
Frequency
Injection point
H2SO4
Liquid
Frequency
H 2 SO 4
Liquid
40 %
4 maxi (Fe)
Continuous
Static mixer prior to pre- treatment
Concentration
Dosing rate
mg/L
Frequency
Injection point
Fe2(SO4 )3
Liquid
pre- treatment
Fe 2(SO 4 )3
Liquid
100 %
0.2 maxi
continuous
Static mixer prior to
flocculation
Concentration
Dosing rate
mg/L
Frequency
Injection point
Polyelectrolyte
Liq or Powder
100 %
0.2 maxi
continuous
flocculation
Injection point
Polyelectrolyte
Liq or Powder
TURBIDITY
0,0
1,0
2,0
3,0
4,0
5,0
6,0
7,0
8,0
9,0
10,0
08/12/08 18/12/08 28/12/08 07/01/09 17/01/09 27/01/09 06/02/09 16/02/09 26/02/09
NT
U
Internal Lab NATA Lab) Limit
TOTAL ORGANIC CARBON
0,0
1,0
2,0
3,0
4,0
5,0
6,0
7,0
8,0
9,0
10,0
08/12/08 18/12/08 28/12/08 07/01/09 17/01/09 27/01/09 06/02/09 16/02/09 26/02/09
mg
/L
NATA Lab Limit
.
2.Case of Gold Coast : SDI, TOC & Turbidity inlet water
0
5
10
15
20
25
30
35
13.12.2
008
17.12.2
008
20.12.2
008
2712
.200
8
30.12.2
008
02.01.2
009
05.01.2
009
09.01.2
009
12.01.2
009
15.01.2
009
18.01.2
009
21.01.2
009
27.01.2
009
30.01.2
009
02.02.2
009
05.02.2
009
09.02.2
009
12.02.2
009
15.02.2
009
18.02.2
009
SD
I 3 r
aw
wate
r
SDI 15 & Turbidity on the filtered water
0
0,5
1
1,5
2
2,5
3
3,5
4
4,5
13.1
2.2
008
16.1
2.2
008
18.1
2.2
008
20.1
2.2
008
22.1
2.2
008
28.1
2.2
008
30.1
2.2
008
01.0
1.2
009
03.0
1.2
009
05.0
1.2
009
07.0
1.2
009
10.0
1.2
009
12.0
1.2
009
14.0
1.2
009
16.0
1.2
009
18.0
1.2
009
20.0
1.2
009
22.0
1.2
009
27.0
1.2
009
29.0
1.2
009
31.0
1.2
009
02.0
2.2
009
04.0
2.2
009
06.0
2.2
009
09.0
2.2
009
11.0
2.2
009
13.0
2.2
009
15.0
2.2
009
17.0
2.2
009
20.0
2.2
009
SD
I 15
0
0,2
0,4
0,6
0,8
1
1,2
1,4
1,6
1,8
2
Tu
rbid
ity (
NT
U)
2. Case of Gold Coast : SDI & Turbidity
The sea water SDI3 has been around similar values as during
the pilot plant work from 16 to around 28.
The pre-treatment filters have been operating for 6 months and
are achieving SDI15 values of around 2.8 to 3.5 typically just
over 3.0 with filter run times in excess of 40 hours.
The initial acceptance testing at 33 and 66% have been
complete and now they are moving onto 100% testing.
2. Case of Gold Coast : six months of operation
4 March 2009
Gold Coast Desalination Plant
Gold Coast Desalination Plant
FUJAIRAHFUJAIRAH 1
- Degrémont
FUJAIRAH 2
- Veolia
Fujairah power and desalination plant (F1 and now there is F2) is a hybrid
plant at Qidfa', Fujairah in the United Arab Emirates. It is located next to the Qidfa
Power Station 5 kilometres (3.1 mi) south of Khor Fakkan and 20 kilometres
(12 mi) north of the city of Fujairah. The Fujairah plant is the first hybrid plant in
the Middle East, and the largest desalination hybrid plant in the world.
3. Case of Fujairah ( UEA)
Parameter Units
Design analysis
parameters
Temperature °C 22-33
pH 8.05
Turbidity NTU 3.33 (max)
TDS (Total Dissolved Solid) ppm 40,500
SDI (Silt Density Index) %/min 14.4 -28
Total Petroleum Hydrocarbon Content ppm < 0.1
Water flow rate base solution m3/day 365 882
Hourly flow base sol m3/h 15 245
Produced Flow m3/day 136 800
3. Case of Fujairah (UEA)
Sea water
Chlorination
Possible
acid
Coagulant
Flocculant
Flocculation
Dual media filters
Sea water
Shock
Chlorination
Acid
addition Coagulation
Flocculation
Dual media filters
Flotation
Fujairah 1 : existing Plant
Fujairah 2 : new Plant
0,0
5,0
10,0
15,0
20,0
25,0
19/4/08 0:00 9/5/08 0:00 29/5/08 0:00 18/6/08 0:00 8/7/08 0:00 28/7/08 0:00 17/8/08 0:00 6/9/08 0:00 26/9/08 0:00 16/10/08 0:00
Date and TimeNotes: TSS in mg/L
EPC
Range
value
3. Case of Fujairah - Seawater TSS monitoring
Exceptional bloom algae
“The 'red tide' happens every year but, for a number of reasons, this year it has been the worst for years. The size and spread of the occurrence has adversely affected fishing and tourism industries.”
Saif Mohammad Al Shara, Director of the East Region Office for the Ministry of Environment and Water
Gulf News, 18/11/08
SDI
0,0
5,0
10,0
15,0
20,0
25,0
30,0
35,0
19/4/08 0:00 9/5/08 0:00 29/5/08 0:00 18/6/08 0:00 8/7/08 0:00 28/7/08 0:00 17/8/08 0:00 6/9/08 0:00 26/9/08 0:00 16/10/08 0:00
Date and Time
SD
I 3
0,0
1,0
2,0
3,0
4,0
5,0
6,0
7,0
8,0
9,0
10,0
SD
I 15
Raw Water SDI3 Filtered Water SDI15 SDI3 Raw Water Moving Average SDI15 Filtered water Moving average
SDI during the complete two normal periods
SDI
0,0
5,0
10,0
15,0
20,0
25,0
30,0
35,0
40,0
27/8/08 0:00 1/9/08 0:00 6/9/08 0:00 11/9/08 0:00 16/9/08 0:00 21/9/08 0:00
Date and Time
SD
I 3
0,0
1,0
2,0
3,0
4,0
5,0
6,0
7,0
8,0
9,0
10,0
SD
I 15
Raw Water SDI3 Filtered Water SDI15 Filtered water SDI15 moving average Raw Water SDI3 moving Average
Seawater SDI3
Surface of the floatation tank
during normal operation
Surface of the same floatation
tank during a red tide event
Seawater Quality
“Red tide” aka “Harmful Algal Bloom”, caused by the phytoplankton specie Heterosigma sp. (class Raphidophyceae).
Courtesy of Elise Marquis, Research Associate at the United Nation University, Dubai. Used with permission.
Introduction SEAWATER Chemicals Performances Conclusion
Objectives:
Chemicals dosing:
H2SO4: < 25 mg/L as pure product
FeCl3 : < 7 mg/L as Fe in the first coagulation step
FeCl3 : 0 to 0.5 mg/L as Fe in the second
coagulation step
Filtered water quality:
SDI(15 min) less than 5 at all time
SDI(15 min) less than 4 more than 90% of the
time
Filtration cycle longer than 40 hours
3. Case of Fujairah : objectives of Pilot plant in conformity
Pretreatment diagram
Sea Water
Coagulation
Floatation
Dual media
filtration
NaHSO3
H2SO4
FeCl3
White water (mix of
floated water and
dissolved air)
Flocculation
Sludge
Polymer
FeCl3
Temporary
storage
Discharge back to
sea
Backwash
NaOCl
Fujairah :
Conclusion
A proper pre treatment is therefore considered to be the key to
successful RO plant operation
The choice of the pre treatment depends of the raw water quality
and its evolution during the year.
All the parameters have to be considered (red tide & bloom algae,
hydrocarbons,TOC, T°C) and not only Turbidity and SDI.
Pilot plant is recommended whenever it is possible.
The data collected by Veolia over the past 10 years allows us a
good understanding of the phenomena that occur in seawater, and
helps us offer the best solution