a.1_ egat_experience with d11 steam turbine bowed rotor
TRANSCRIPT
Conference of The Electric Power Supply Industry 2016
EXPERIENCE WITH D11 STEAM TURBINE BOWED ROTOR OPERATION Mr.Sarun Sahanavin, Engineer Level 7, Operation Shift 4, Ratchaburi Combined Cycle Power Plant,
Electricity Generating Authority of Thailand, +66814414764, [email protected]
Mr.Peerapong Wanichthanarak, Engineer Level 5, Mechanical Maintenance Section, Ratchaburi Combined
Cycle Power Plant, Electricity Generating Authority of Thailand, +66851503515, [email protected]
Abstract- During a shutdown process for major overhaul at ratchaburi combined cycle power plant block
3 in 2009, the D11 steam turbine, which manufactured by GE, had experienced a bowed rotor problem. It had
caused a severe rub between turbine rotor and stationary part which resulted in HP/IP turbine casing crack at N2
packing male main fit. The casing was temporarily repaired by stitching method during major overhaul in 2009,
then needed a further welding repair during minor inspection in 2011, and finally a casing replacement during
planned outage in 2014.
Since major overhaul in 2009, a vibration high trip at a critical speed during a startup process, which
caused by a bowed rotor, had frequently occurred. It was solved by a field balancing but the problems still
remain at warm and hot condition. A startup process is improved by increase a reheat steam temperature at least
50 degF higher than a reheat upper metal temperature, control reheat pressure to roll steam turbine between 60-
70 psi, and startup manually by fast ramp rate. The results are 97.7% successful startups but vibration measuring
is rather high at warm and hot condition. It was solved by both low speed balancing and field balancing once
again during major overhaul in 2015 to ensure a responsive operation according to NCC’s command.
Keyword- D11 Steam Turbine, Bowed Rotor, HP/IP Turbine Casing, N2 Packing Male Main Fit, Vibration
High Trip
I. Introduction
During a shutdown process for major overhaul at ratchaburi combined cycle power plant block 3 in 2009,
the D11 steam turbine, which manufactured by GE, had vibration high trip at a critical speed. The maximum
casing vibration is 18 mils (Alarm 6.0 mils / Trip 9.0 mils)
It had caused a severe rub between turbine rotor and stationary part which resulted in HP/IP turbine
casing crack at both side of N2 packing head as shown in Fig. 1
Figure 1: HP/IP Turbine Casing Crack
The casing was temporarily repaired by stitching method, then welded repair later, and finally replaced
with a new casing.
Table 1 : Advantages and Disadvantages of Stitching, Welding and Replacement Casing
Method Advantages Disadvantages
Stitching - No casing distortion
- Short time to repair
- Temporarily repaired
Low alloy welding - Permanent repairs
- It takes a long time to repair
- There is risk of casing distortion
- Weaker than high alloy welding
High alloy welding - Permanent repairs
- It takes a long time to repair
- There is risk of casing distortion
- More difficult than low alloy
welding
Replace new casing - The root cause solution - It takes a long time to replace
casing
- Must be similar in dimensions to
the old casing
The casing was temporarily repaired by stitching method during major overhaul in 2009. Because it takes
short time to repair and has no effect on major overhaul schedule as shown in Fig. 2
Figure 2: Stitching Repair
During minor inspection in 2011, a casing crack was found at the same location and some stitching pin
disappear as shown in Fig. 3
Figure 3: Before-After Repaired by Stitching method
Casing Damage on 2009 Casing Damage on 2011
Therefore repair method was changed to low alloy welding as shown in Fig. 4
Figure 4 : Welding Repair HP/IP turbine casing RGC-C30
Finally a casing replacement during planned outage in 2014, a new HP/IP turbine casing had an
improvement design of N2 Shell Male Main Fit and N2 Packing Head to have more strength as shown in Fig. 5.
A casing Installation as shown in Fig. 6.
Figure 5 : New HP/IP Turbine Casing
Remove Crack and Grinding Groove Install Jig & Support Preheat @ 200 degC
Welding Post heat @ 350 degC Hardness Check
Figure 6 : HP/IP Turbine Casing Replacement
II. Main Content
Bowed rotor problem - RGC-C30 HP/IP turbine casing crack had caused a severe rub during shutdown
process for major overhaul 2009. It resulted in rotor bow as shown in Fig. 7. Maximum rotor run out have found
at middle of HP/IP Rotor with a measured value equals to 0.12 mm as shown in Fig. 8
Figure 7 : Bowed Rotor Problem
Pipe cutting Remove old casing Install new casing
Pipe welding Laser alignment Final assembly
Figure 8 : RGC-C30 Rotor Runout Measurement
The rotor eccentricity monitoring at control room is 3.6 mils as shown in Fig. 9, while the operating
permissive to auto start up is below 3.0 mils.
Figure 9 : Electricity Monitoring
Vibration high trip problem - Since major overhaul steam turbine in 2009, a vibration high trip at a
critical speed during a startup process happened frequently. A detailed steam turbine start up from 7-26 May
2009 as shown in Table 2
Table 2 : Start Up History After Major Overhaul RGC-C30
Start Up Condition Number of Start Number of Success
Cold Start 5 4
Warm Start 3 2
Hot Start 7 1
Total 15 7
The repetitive steam turbine rotor bow – First method to help a vibration high trip problem is using
steam to soak turbine at speed of 400 rpm for 30 min. and then at 1000 rpm for 60 min. repeatedly 3 times until
all shaft vibration have no change of phase angle. But this process cannot guaranteed a successful startup every
time and uses more fuel cost, so next method used is a field balance by putting weight 300 g. at turbine bearing
no.1
Since a field balance in 2009, the startup data during 2009 to 2010 still shown some problems when
startup with hot mode or warm mode. By doing further field balancing it can decrease a vibration at critical
speed, but likely cause problem at the normal operation at higher load and may cause a vibration high trip.
III. Results
Startup procedure improvement - Before D11 steam turbine auto start up, the requirement
parameters will be as following:
a. Steam Pressure and Temperature, b. Metal Temperature, c. Lube Oil Temperature, d. Eccentricity
When these values met the requirement, the operator will begin to roll turbine from turning gear to full
speed no load, synchronize to electrical transmission system, and then steam turbine flow change mode from
reverse flow to forward flow, inlet pressure control in-service and finally LP admission steam in-service.
The turbine acceleration rate will vary depends on calculated stress value. A vibration high trip may
occurs at critical speed about 1500 rpm as shown in Fig. 10
Figure 10 : D11 Steam Turbine Start Up Diagram
In Fig.11 during a start up steam turbine process, when a first admit steam to the turbine. It warms the
turbine and then start to rotate by RH steam. Then it changes to forward flow with an additional HP steam flow
through the HP turbine.
When a turbine speed reach 75%, the reverse flow valve mounted in CRH line will open to cool down
at HP Turbine (only hot start or metal temperature above 700 degF)
Figure 11 : Steam Flow Diagram
HP turbine bowed rotor has frequently cause a vibration high trip during start up process, although it
has been improved by a field balancing but the problem still remains.
To reduce the risk of being fined by contract of power plant purchase agreement, therefore the steam
turbine block 3 is prioritize as the last one to reserve shutdown. But on 14th
March 2010, National Control
Center (NCC) needed to reserve shutdown block 3 and then startup on 15th
March 2010. The results are RGC-
C30 cannot startup steam turbine according to NCC’s command, the operator attempted restart a steam turbine
until a successful 4th
startup on 17th
March 2010 as shown in Fig. 12
Figure 12 : Startup Steam Turbine Event from 15
th – 17
th March 2010
From analysis, the causes of vibration high trip is the rubbing between HP/IP turbine rotor and N2
packing. The only possibility collects from many startup is hot turbine starts with low steam temperature as
shown in Fig. 13
Figure 13 : Root Cause Analysis of Vibration High Trip
The data collecting of the difference between RH steam temperature and RH metal temperature during
start up steam turbine from 15th
– 17th
March 2010 shown that every time before turbine rolls a reheat
temperature difference (RHT_DIF) is less than 500 degF and met the requirement for auto start up permissive as
shown in Table 3
But the vibration high trip still remain which means the condition might not be appropriate for a bowed
rotor and needs to be adjusted to ensure a successful startup.
Table 3 : RH Steam/Metal Temperature Between Start Up in 15 – 17 March 2010
1st start 2
nd start 3
rd start 4
th start
TT_RHS1 : oF 550 688 489 581
TT_RHS2 : oF 541 681 480 575
TT_RHBUI1 : oF 767 707 488 464
TT_RHBLI1 : oF 526 466 274 267
TT_RHBLI2 : oF 506 448 259 257
RHT_DIF : oF 30 228 218 316
When comparing condition requirements between auto start up permissive and manufacture guide
(GEK 106752 & GEK 111301), there is one parameter that should be adjusted, it is a RHT_DIF. This parameter
is calculated from difference between an average of RH steam temperature and an average of RH lower metal
temperature. The steam turbine can auto startup when a RH temperature difference is lower than 500 degF, and
RH pressure (HRHP) must be over 1% as shown in Fig. 14
Figure 14 : D11 Steam Turbine Auto Start Up Permissive
The RH metal thermocouples were installed at 3 positions as following, one RH upper metal
temperature (TT_RHBUI1) and two RH lower metal temperature (TT_RHBLI1, TT_RHBLI2). The RH upper
metal thermocouple was installed near IP turbine rotor, and RH lower metal thermocouples were installed at RH
inlet pipe as shown in Fig. 15
Figure 15 : D11 Steam Turbine Reheat Metal Temperature Measurement
The position of RH upper metal thermocouple is closer to IP turbine than RH lower metal
thermocouples, so the measured value from RH upper metal thermocouple shows the true condition of IP
turbine.
From the trend of steam turbine during shutdown as shown in Fig. 16, the RH lower metal temperature
decrease faster than RH upper metal temperature. So when the turbine startup in hot mode or warm mode
chances are turbine will roll with low steam temperature, because the condition of auto start up permissive had
calculated RHT_DIF by average of RH lower metal temperature and excluded the RH upper metal temperature.
Figure 16 : RH Steam and Metal Temperture
The manufacture guide specify in GEK 111301 had defined the RH steam temperature must be 200-
250 degF higher than RH metal temperature as shown in Fig. 17. But in practice when the operator try to
increase RH steam temperature up to that point it will takes a lot of time. So an optimum adjustment for RH
steam temperature was changed to 50 degF higher than RH upper metal temperature.
Figure 17 : Allowable RH Steam Temperature for Roll Steam Turbine
The requirement of auto start up permissive defined a RH pressure more than 1% of design pressure.
The manufacture guide had specified RH pressure from 101-130 psi, and RH bypass pressure control valve set
point equal to 58 psi for cold start and 112 psi for warm / hot start.
To startup steam turbine by hot mode must have a very high RH steam temperature. Therefore, it needs
higher gas turbine load but doing so may cause a RH steam pressure too high which according to record, it had
caused vibration high trip in block 1 and block 2. Thus requiring to reduce flue gas flow by decrease HRSG
damper to 80%, and limit a RH steam pressure in the range of 60-70 psi.
The startup of steam turbine by auto mode, an acceleration rate is calculated by the control system based
on rotor stress as shown in Table 4. To avoid the risk of extensively operating at or near the critical speed, which
might cause rubbing and vibration high trip as shown in Fig. 18, operator chooses to do a manual start up by fast
ramp rate since on turning gear until full speed no load.
In conclusion, the startup procedures improvement to reduce a vibration high trip problem at critical
speed in steam turbine bowed rotor are as following:
a. Increase a reheat steam temperature at least 50 degF higher than a reheat upper metal temperature
b. Control a reheat pressure to roll steam turbine in the range of 60-70 psi
c. Start up manually by fast ramp rate
Table 4 : D11 Steam Turbine Start up Ramp Rate
Speed
%
Condition Acceleration
rate
TNHR_RS%
/ min
0-10 -
Fast 20
> 10 If stress > 50%
If 5 < stress < 50 %
If stress < 5 %
Slow
Medium
Fast
6.7
10
20
Figure 18 : Auto Start up Steam Turbine and Vibration High Trip Problem
IV. Conclusion
Since improvement a startup process in 2011 until a HP/IP turbine casing replacement in 2014, RGC-
C30 have a total startup of 20 times which divide into hot start 4 times, warm start 5 times and cold start 11
times. The result of startup are always successful. But even with a casing replacement the vibration
measuring is rather high at warm and hot condition, because steam turbine bowed rotor does not
replacement. To reduce vibration during normal operation, it was solved by both low speed balancing and
field balancing once again during major overhaul in 2015. Until now it had a 100% successful startup.
(Detail of startup as shown in Fig. 19)
Figure 19 : Detail Steam Turbine Start up after Replacement Casing Turbine
References :
GENERAL ELECTRIC COMPANY (1997). GEK 106752 : Basic Information for Starting and Loading
Reheat Combined Cycle Units.
GENERAL ELECTRIC COMPANY (2005). GEK111301: Allowable Steam to Metal Temperature Mismatch
Combined Cycle Units
GENERAL ELECTRIC COMPANY (2007). GEK110856d : Steam Seal System Requirements for Combined
Cycle Steam Turbines