120218212552_4_1_maaden
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http://www.afa.com.eg/uploads/papers/2012/files/120218212552_4_1_maaden.pdfTRANSCRIPT
18th AFA Int’l Annual Fertilizer Forum & Exhibition Feb., 7-9-2012,
Sharm El-Sheikh , Egypt Maritim Jolie Ville Hotel
Commissioning Experience of a Large Scale Ammonia Plant
Mr. Sayer Al-Mufadhali,
Staff Production Eng, Ma’aden Phosphate Co.
Saudi Arabia
2/18/2012
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CommissioningExperience ofaLargeScale
AmmoniaPlant
Ma’adenPhosphateCompany
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CONTENTS
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Introduction to Ma’aden Phosphate Company
Project Highlights
Features of Ammonia Plant
Commissioning Experience
Conclusion
2/18/2012
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MA’ADEN PHOSPHATE COMPANY
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Joint venture between the Saudi Arabian Mining Company (Ma'aden) and Saudi Basic Industries Corporation (SABIC)
Fully integrated Phosphatic Fertilizer Complex based on phosphate deposits at Al Jalamid to manufacture Diammonium Phosphate
Natural gas and Sulfur from ARAMCO
Al Jalamid mine in the north of the Kingdom comprises of a phosphate mine and a beneficiation plant
The phosphate concentrate transported by rail to Ras Al Khair through a distance of 1400 KMs
Ras Al Khair on the eastern coast of the Arabian Gulf 130 km north of Jubail has Ammonia, Sulfuric Acid, Phosphoric Acid and DAP plants
Ras Al Khair also has exclusive port facilities to export Ammonia and DAP
MA’ADEN PHOSPHATE COMPANY
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Production capacities at Ras Al Khair are as follows:
Ammonia: 3300 TPD
Sulfuric Acid: 3 streams each of 4500 TPD
Phosphoric Acid: 3 streams each of 1460 TPD
DAP: 4 streams each of 2250 TPD
Power Generation: 150 MW
Desalinated Water: 40000 M3/Day
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OVERVIEW OF THE INTEGRATED COMPLEX
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BENEFICIATION PLANT
PHOSPHORIC ACID PLANT
SULFURIC ACID PLANT
DAP PLANT
AMMONIA PLANT
PROJECT HIGHLIGHTS
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Project Execution
Samsung Engineering Company Limited as EPCcontractor on LSTK basis
Worley Parson as Project Management Consultant(PMC)
Uhde on advisory services to Samsung during projectstage and for supply of the critical equipments
Project kick started with EDC in May 2007 andperformance test completed in May 2011
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PROJECT MILESTONES
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Major Events Date Effective Date of Contract 28.05.2007Basic Engineering Commencement 30.10.2007Detailed Engineering Completion 26.05.2009Mechanical Completion 24.08.2010Lighting of Primary Reformer 29.12.2010Natural Gas Feed 07.01.2011Completion of LTS Catalyst Reduction 24.01.2011Methanator Catalyst Reduction 26.01.2011First Ammonia Production 11.02.2011Trial Test |Completion & Achievement of 100% Load 27.04.2011Completion of Performance Test 03.05.2011
PROJECT MILESTONES
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Performance Test Results
Consumption of Raw Materials & Utilities
Description Unit Expected FigureEnergy Consumption GJ/MT of NH3 31.078
Desalinated Water M3/MT of NH3 0.884Sea Water (DT=10°C) M3/MT of NH3 285.000
Description Unit Test Result
Energy ConsumptionGJ/MT of
NH328.283
Nox (NO2) Level, Primary Reformer Stack (Maximum 150)
Mg/Nm3 91.785
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AMMONIA PLANT LAYOUT
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FEATURES OF AMMONIA PLANT
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The Ammonia Plant is based on Uhde Standard Dual Pressure Concept (USDPC) process to produce 3,300 MT/day of anhydrous Ammonia in a single stream with purity of 99.8 % (min)
Desulfurization Unit: OneHydotreater reactor and twoZnO Reactors working inlead/lag/parallel operation
Primary Reformer: Top firedbox type furnace with 408tubes in 8 rows/combustionair fan with dual drive, 189burners (Low Nox)/ColdOutlet Manifold System
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FEATURES OF AMMONIA PLANT
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Removal of CO2 by absorption withaMDEA solution
Synthesis Gas Drying Unit: TwoMS adsorber vessels in parallel/three filters in parallel/oneregeneration gas heater
Ammonia Synthesis: Uhde DualPressure Process with TwoSynthesis SectionsOnce through Synthesis @ 110.0bar (Approximately 1000 MTPD)and Loop Synthesis @ 204.0 bar(Approximately 2300 MTPD)
Outlet Manifold System
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Leaks During Tightness Test for Primary Reformer Tubes
Pressure test of thesystem at 40 bar
340 flanges out of 408had leaks
All gaskets replacedand less torque appliedfor tightening
During retesting, 102flanges found to haveleaks
All the gaskets replacedwith torque of 300 NmThereafter, no moreleaks were observed
COMMISSIONING EXPERIENCE
2/18/2012
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COMMISSIONING EXPERIENCE
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Leaks During Tightness Test for Primary Reformer Tubes
Conclusion Excess torque resulted in gasket inner ring damage and bending of
outer ring 300-350 Nm found to give the required torque for tightness without leak
COMMISSIONING EXPERIENCE
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Damage to Demisters in the Steam Drum
During chemical cleaning, demisters were removed and reinstalled
System pressurized by steam to 50 barg to test the integrity
When opened for preparation of alkali boil out, 7 out of 13 demisters were found damaged Damaged Drum Demister
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COMMISSIONING EXPERIENCE
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Damage to the Demisters in Steam Drum
Analysis Chemical cleaning had four
stages of cleaning namely degreasing, acid pickling, neutralization and passivation
HCl used to correct the pH of the contents in the holding tank of the system
Migration of residual chlorides from the steam header during pressure test
The damage to the demisters caused by Chloride Stress Corrosion Cracking
Conclusion: Thorough rinsing essentialAll dead zones in the system to beincluded while rinsing
COMMISSIONING EXPERIENCE
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Heavy Wear of Worm Gear for Turning Device
The Worm Gears for the turning deviceof NG, SG, RF, PA CompressorTurbines and Generator Turbine werefound to have undergone severe wear
Overview and Damaged Condition of the Worm Gear
MHI Experience (Wear) Ferrite content to be <5% as
excess ferrite causes reduction inwear resistance
Application of surface treatmentby nitriding and lubricant coatingof the hardened worm gear toreduce the friction force on thesliding surface
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COMMISSIONING EXPERIENCE
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Possible Causes
Oil supply
Oil supply temperature, pressure and quality
Turning torque
Teeth contact of worm gear
Turning motor electric current
Worm gear strength
Hardness and ferrite content
Heavy Wear of Worm Gear for Turning Device
COMMISSIONING EXPERIENCE
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Results Oil supply check found to be satisfactory
Oil Supply temperature, pressure and quality within acceptable limits
No heavy contact of internal parts as manual turning can be done
Actual current of turning gear higher than expected for SG Compressor turbine. Rated current is 2.90A versus measured current of 2.75A
Worm gear strength found to be satisfactory
Hardness and ferrite content found to be satisfactory
Heavy Wear of Worm Gear for Turning Device
2/18/2012
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COMMISSIONING EXPERIENCE
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Conclusion
The actual required turning torque was above the design because of unknown condition due to increase in internal friction force
Hence, the existing worm gear has less safety margin for wear resistance
MHI to offer improved material
Heavy Wear of Worm Gear for Turning Device
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RecommendationTemporary Action (Material change of worm gear)
MHI have two materials for worm gears (Cast Iron & Copper Based Alloy) The wear resistance of copper alloy is higher than cast iron Recommended to replace cast iron type with copper alloy type
Permanent Action
The existing worm gear does not have sufficient wear resistance against unknown operating condition MHI is looking to introduce a new wear resistant material
COMMISSIONING EXPERIENCE
Heavy Wear of Worm Gear for Turning Device
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COMMISSIONING EXPERIENCE
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HP Steam Superheater
HP steam superheater could notsuperheat saturated steam
Less heat only available in theconvection box
The temperature of the HT shiftconverter was going up.Desulfurization Sectiontemperature came down
It was decided to stop the plantand inspect the HP Superheater
HP Steam Superheater
COMMISSIONING EXPERIENCE
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HP Steam Superheater
Steam Side Schematic of the Superheater
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COMMISSIONING EXPERIENCE
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HP Steam Superheater Observations
Cover plate of shroud dividing saturated steam inlet from superheated steam outlet found lifted and bent
All 32 bolts holding the cover plate on top of the shroud found sheared off. The material of 4 of the 32 bolts found to be different
Gasket material found on top of tube sheet
Gasket blown-out and gap between shell and expansion bellow found increased
Cover Plate Lifted-up and Bent
Sheared-off Bolts
COMMISSIONING EXPERIENCE
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HP Steam Superheater
Possible Causes
Possible damage during steam blowing through internals
Improper operation of plant during start-up/shut-down
Carry-over to HP steam super heater either from steam drum orsynthesis gas waste heat boiler system
Accumulation and sudden evaporation of BFW from attemperators u/sconvection bank
Improper installation of top cover after removing internal bypass duringchemical cleaning and steam blowing during pre-commissioning
Improper tightening of bolts/wrong bolt material
Improper tack welding of nuts leading to high stress of bolts
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COMMISSIONING EXPERIENCE
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HP Steam Superheater
Analysis During startup, no positive flow of steam through the super
heater coil
Steam venting through the start up vent at the steam drumitself
Entry of water and sudden generation of steam exceedingthe allowable pressure difference across the super heater
COMMISSIONING EXPERIENCE
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HP Steam SuperheaterModified Start Up Procedure
Gradual transfer of steam venting to start up vent downstream of thesuper heater establishing a positive flow of steam and not allowing anyresidual heat
Establishing adequate circulation in the WHB system through start upsteam
Lining up block valves of attemperator only when the skin temperature ofthe coils reaches 480°C
Monitoring the differential pressure across the steam super heaterduring start up
With this revised procedure, the plant was successfully startedwithout any problem
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COMMISSIONING EXPERIENCE
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Problem in Natural Gas Pressure Control System
Shutdown due to failure in managing two control valves in parallel in natural gas line
The 16” butterfly valve suddenly closed to “full close position” and the plant tripped
On another occasion, the valve suddenly started opening and closing repeatedly causing severe hunting of flow and plant tripping
In both cases, 16” butterfly valve was in auto mode and NG pressure at battery limit suddenly started hunting in a very unstable manner
Observations
There were common conditions on both occasion
Upstream pressure gone to 40 barg
Downstream pressure was 20 barg and there was a sudden surge of 3~4 bar
Controller command forced the valve to be fully closed within one minute
COMMISSIONING EXPERIENCE
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Problem in Natural Gas Pressure Control System
Possible Reason for Sudden Pressure surge
Pressure surges appeared when the upstream pressure was 40 barg and downstream pressure was around 20 barg
Differential pressure across the valve became greater than the critical pressure ratio possibly making shock waves downstream near the throat of the valve
When there is a high pressure drop across the valve (P up/P down >1.8), the flow characteristic through the valve are changed from sub-sonic flow to sonic (choked) flow
This supersonic flow in turn could generate shock waves downstream of the throat (valve) forming a localized pressure build-up
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COMMISSIONING EXPERIENCE
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Problem in Natural Gas Pressure Control System
Conclusion
Localized shock waves due to high delta pressure could be the reason
Not recommended to have aggressive action of the valve especially choked flow condition. The proportional band adjusted
Decided to keep the 16” Butterfly control valve on manual with constant opening and to keep the 6” Globe valve on auto to take care of pressure fluctuations
COMMISSIONING EXPERIENCE
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Impact of Fluctuation in NG Composition
Changes in gas composition at times very rapid
Could lead to plant trip sometimes
Observations Since plant commissioning,
varying composition of gas has been observed
Natural gas generally heavier Heavier hydro-carbons showing
heavy fluctuations within short span of time in the composition
Natural Gas Composition
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COMMISSIONING EXPERIENCE
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Impact of Fluctuation in NG CompositionImpact on Process
Process steam flow adjusted to maintain overall steam-carbon ratio of 3.0
High fluctuations and high carbon number in feed gas composition results in additional load on CO2 removal unit leading to higher CO2
slip
Action Taken
Close monitoring of plant parameters during fluctuations by adjustment of gas flow rate and/or process steam flow rate
Regular interaction between MPC and supplier to improve the natural gas quality and advance communication when there is any change in natural gas compositions
COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
Sequence of Events
Hot spot observed downstream of the Transition Duct
During a shutdown opportunity, the convection bank was opened and inspected
Gap observed between the ceramic fiber modules on the top and east side
Gap filled with ceramic fiber
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COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
View of the Gap being Filled Between the Ceramic Modules Downstream of Transition Duct
COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
Sequence of Events During inspection, gaps were also observed upstream of the
transition duct where the connection of the tunnel bricks exists with the ceramic fiber modules and in particular the castable lining behind the tunnel bricks
New fiber blankets fitted into the gaps and the tunnel bricks moved back into position
After a period of few months, hot spots observed upstream of the transition duct along the entire length
Channeling of hot gases through the gaps generated these hot spots
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COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
Transition Duct
COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
ConnectionofTunnelBrickstotheTransitionDuct
Close‐UpViewoftheTunnelBrickstoTransition Duct
Gaps Observed Between the Tunnel Bricks & Transition Duct Modules
View of the Cast Lining between the Tunnel Bricks and Insulation Modules
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COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
Connection of Tunnel Bricks to the Transition DuctClose-Up View of the Tunnel Bricks to Transition Duct
Gaps Observed Between the Tunnel Bricks & Transition Duct Modules
View of the Cast Lining between the Tunnel Bricks and Insulation Modules
COMMISSIONING EXPERIENCE
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Hot Spot in Reformer Convection Section
Action Taken
Steam sparger provided as a temporary solution
The permanent solution is to overcome the movement ofthe tunnel bricks during expansion and contraction of thefurnace during plant upsets
Recommendations from Kareena and Uhde are awaited
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CONCLUSION
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Commissioning of MPC’s Ammonia Plant was smooth
First production within 7 weeks from the time reformer waslighted and within 5 weeks after introduction of feedstock
Problems faced during commissioning of the plant handledsuccessfully and the plant throughput increased to therated capacity successfully
Having successfully stabilized the operations, MPC isembarking upon taking up the plant load further
Thank You40