*' employee bulletin - boeing ch-47...

6
( *' EMPLOYEE BULLETIN No. 75-38 November 25, 1975 UTTAS 001 ACCIDENT SEQUENCE ESTABLISHED- AIRCRAFT REPAIRABLE The sequence of events in UTTAS aircraft 001 accident have been clearly established. During buildup maneuvers toward the 85 knot autorotative pull-out point of the structural demonstration an RPM overshoot to approximately 125% of normal RPM was encountered. During the RPM overshoot the most forward section of the tail rotor drive shafting (be- tween the main transmission and the intermediate transmission) contacted a work step in the aft transmission compartment. The contact with this step tore the first section of shaft causing it to fail and eliminating the drive torque to the tailrotor. This, of course, resulted in the loss of direc- tional control. Due to the low airspeed and low altitude existing following this occurrence, it was impossible to get the aircraft into a forward flight speed regime where adequate vertical tail effectiveness would provide direc- tional control of the aircraft. The aircraft came down into a patch of dense oak woods. Accident Investigation Board The U. S. Army has established an official military accident investigation board headed by Colonel Dennis Boyle to investi- gate the accident. The Company is cooperating fully with the Board. Any official public releases will be made by the Army Board. UTTAS aircraft 002 and 003 have been cleared by the Army to resume their flight test program. Also, the Army's Pilot Evaluation Program is proceeding as planned, operating with autorotative RPM restrictions which will avoid the recurrence of the 001 problem. - more -

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Page 1: *' EMPLOYEE BULLETIN - Boeing CH-47 Chinookww.chinook-helicopter.com/news/Boeing/CH-47C_Slings_UTTAS_001...tional control. Due to the low ... get the aircraft into a forward flight

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*' EMPLOYEE BULLETIN

No. 75-38 November 25, 1975

UTTAS 001 ACCIDENT SEQUENCE ESTABLISHED­AIRCRAFT REPAIRABLE

The sequence of events in UTTAS aircraft 001 accident have been clearly established. During buildup maneuvers toward the 85 knot autorotative pull-out point of the structural demonstration an RPM overshoot to approximately 125% of normal RPM was encountered. During the RPM overshoot the most forward section of the tail rotor drive shafting (be­tween the main transmission and the intermediate transmission) contacted a work step in the aft transmission compartment. The contact with this step tore the first section of shaft causing it to fail and eliminating the drive torque to the tailrotor. This, of course, resulted in the loss of direc­tional control. Due to the low airspeed and low altitude existing following this occurrence, it was impossible to get the aircraft into a forward flight speed regime where adequate vertical tail effectiveness would provide direc­tional control of the aircraft. The aircraft came down into a patch of dense oak woods.

Accident Investigation Board

The U. S. Army has established an official military accident investigation board headed by Colonel Dennis Boyle to investi­gate the accident. The Company is cooperating fully with the Board. Any official public releases will be made by the Army Board.

UTTAS aircraft 002 and 003 have been cleared by the Army to resume their flight test program. Also, the Army's Pilot Evaluation Program is proceeding as planned, operating with autorotative RPM restrictions which will avoid the recurrence of the 001 problem.

- more ­

Page 2: *' EMPLOYEE BULLETIN - Boeing CH-47 Chinookww.chinook-helicopter.com/news/Boeing/CH-47C_Slings_UTTAS_001...tional control. Due to the low ... get the aircraft into a forward flight

001 Repairable

On Saturday, November 22, a CH-47 Chinook piloted by A. J. Hutto and Al Santa Maria airlifted the UTTAS aircraft from the crash site to the company's facility at the Calverton, Long Island test center. Today, 001 is being brought back to Center 3 at Boeing Center.

Since shortly after the accident took place, a team from Boeing Vertol has been "on the scene" determining the extent of damage to the aircraft.

The main fuselage structure is essentially undamaged. The tail rotor has four blades still attached to the straps in proper connection to the tail rotor hub and shaft even though the tail boom broke loose from the aircraft. Based upon detailed examinations of the damaged aircraft, the company is recommending to the U. S. Army that 001 be re­paired and returned to flight status.

Impact on Program

We are reviewing the impact of the accident on our schedule for delivery of aircraft for the Government Competitive Test. A delay of approximately one month is currently in­dicated based on developing and qualifying an adequate fix for the tail rotor shaft and then completing the aircraft Structural Demonstration program.

Crashworthiness Demonstrated

Just as every dark cloud has its bright lining, this accident was a spectacular demonstration of the crashworthiness of the YUH-61 design. Both of our pilots, Frank Duke and Ron Mecklin, were uninjured and there was no fire.

During entry into the woods the main rotor blades and tail rotor blades contacted a number of oak trees ranging in diameter from 6" to 15". The transmission is firmly in place in the aircraft structure with no evidence of any movement of the transmission and transmission mounting struc­ture. For example, it was possible to open the hatch immediately aft of the transmission with no evidence that any structural deformation of the butt line beams on which the hatch tracks are mounted had taken place.

more

Page 3: *' EMPLOYEE BULLETIN - Boeing CH-47 Chinookww.chinook-helicopter.com/news/Boeing/CH-47C_Slings_UTTAS_001...tional control. Due to the low ... get the aircraft into a forward flight

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CH-47C Chinook, piloted by A. J. Hutto and Al Santa Maria, returns 001 UTTAS to Calverton flight test facility.

Page 4: *' EMPLOYEE BULLETIN - Boeing CH-47 Chinookww.chinook-helicopter.com/news/Boeing/CH-47C_Slings_UTTAS_001...tional control. Due to the low ... get the aircraft into a forward flight

The following photographs taken at the Calverton test center on Saturday, November 22, show the structural integrity demonstrated by the rotor system and airframe structure.

Page 5: *' EMPLOYEE BULLETIN - Boeing CH-47 Chinookww.chinook-helicopter.com/news/Boeing/CH-47C_Slings_UTTAS_001...tional control. Due to the low ... get the aircraft into a forward flight

-..,.-..,-:-------------f--f'---,,BOEINC (

MISHAP REPORT i;; ~;-' II q 1 ~ '. ~ !

11/20/75 F. H. Duke

15.3"Ae.g •

1 11 '.\1

i 140011/18/75 I

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2 hours

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l!~cbnic River AIr?­i calverton, N. Y. -: .__ . __ I

I ~::: i ! t: 1\ r I (l: i '".J I .;

!15,400 1bs

i 1330 I . ._•.__• .•._

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15,920 1bs

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~~ I . .. .=~£ .. to Peconic River & :~j No.2 engine transmission oil pressure dropped Chase Plane <=, to minimum in-flight limit. AIC landed at Mattituck ~~l Alp &.res~rviced, hover checked & returned to

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~ OTHE R ---=N"-'o"'--=t:....- _ - ', ...~ U DUST ---.I LOW CLOUDS Applicable, x' Not APM1"",,'c=a=b=-"'l'-"e~ _

~ l c·No·t < I D LL\EL: ~ '_,'_cl~: I0 ,ICL'NTAINS C- "','.'..'L-~--.­Not Applicablec T_~__~.:..' _P_p_l_l_'_<::_a_b_l_e _ .f ~ 0 THE R -----­

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Page 6: *' EMPLOYEE BULLETIN - Boeing CH-47 Chinookww.chinook-helicopter.com/news/Boeing/CH-47C_Slings_UTTAS_001...tional control. Due to the low ... get the aircraft into a forward flight

"lODEL

:= ACCIDENT~: .. ILANDING:, 'B'" SATL~~KA£-" • , of<~ 'B:,r,ill£';-~--;- ""-~;,\>-,;.,,,~{~~~p-.,,-,~NON-la"'-:. ,.., 0' ,"" lXl PRECAUT I ONERY RECOVERABLE _,._,., " , <~ ~;;:; L...JMAJOR ."4' ':"Fi i 0 FORCED ': MAJOR' , , =~ '0 I • SUBSTA""I;':' MilleR. :' NO DM~AGE EXPLOS'ION ':;--:~S~ISHAP ~ti INCIDENT j:=JCOMBAT DAMAGE i LIMITED 1--1 OTHER MISHAP

179

§OVERHAUL ROPERATION':' -'" OPERATION .j OPERATION !JDPERAT I ON

22 TOW I Nt'a f R£AR FLrGh~ ------------1---1 I 23 SL I NGiHO 1ST ",::>OK -UP16 GO AROUND~ SIDE FLIGhT

1-­ 24 SL I NG/HO/ST FrELEA:SE>;;'17 'ROTOP. SHUTDOWNtol CL 1MB

251 GROL'ND SERV I CE. ,,"18 ROT:JR FOLD111 GESCENT

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~~,Developed leak in #2 hydraulic boost system. Low quantity caution light was <:::0' ;~ followed by loss 'of oil pressurE7 and loss' of _#2 SAS.- 7 ~ "

DEW POINT '-"1 WIND .-' ­',\lND DIRECTlON ,. ,. VELOCIT":C , .<jO. ,

Cd LING I,T EMP 0',c(F. l. , NW at 10,.. '-, 10 knotsNo'factor 2 7 '!;I," .......:.r'. :::.;.~-:. 12ia:.""':"'" ,,;.

TURBULENCE3: §' ,~' F~G, ',- ,,0 HA I L ,'" r. THUN'DERSTO~MS "8 MODERA:T,E -:;~'" ~EJ' "\i GHTEN,:iNG ,'::::i;~, " SEVERE, ',"~";;';-~ OTHER --'- ~'____ ~ 'IG,NG'U"DU'i'i- ~'U- LOW ClOU~S",

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ec D -olTt::_~,a:: \U 'FT. D

Aircraf,t landed at Salem Airport. Determined leak to be"'tail rotor : :, ,contro1 actuator. Isolated the #2 boost lines to the tail-'rotor "

and re-serviced the svstem and returned to Wilmington:": - ' ~- '- ~.1°'Li""----..~;'"II' 'j, .­... ~ \ .... ~ ..._,- ....'!

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