safety hazards in urea plants v10 261117 - … shut down ... ref no. prevention measures reducing...

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Revision Hazard # Hazard & Initiating Event Consequences Safety Study Reference Link C L R Sponsor 1 Sponsor 2 Sponsor 3 Sponsor 4 Sponsor 5 Sponsor 6 C L R 1 V10, 26 November 2017 H1 Leaking flange of CO2 line One person passes out although a DCS alarm was on but unnoticed due to too many alarms during the start up phase Commissioning / Start Up Feed CO2 piping Yes Incident Database Incident XX-014 http://www.ureaknowhow.com/ukh2/round- Moderate Moderate 9 (High) 9 CO2 is heavier than normal air and can collect at lower elevations reducing oxygen content to dangerous low levels. A proper CO2 detector including DCS alarm should be present. Flange leakages are to be checked after a start up. Personal should be aware of the risks of CO2. Pay attention to alarm management and alarm inflation. Major Rare (5) Moderate 5 2 V10, 26 November 2017 H13 Acetic acid used for cleaning enters lube oil system of CO2 compressor via nitrogen network Severe damage to bearings/seals Maintenance Feed CO2 compressor Yes Incident Database Incident 09-005 http://www.ureaknowhow.com/ukh2/round- Insignificant Unlikely 2 (Low) 2 Perform risk analysis also for maintenance activiities, do not trust check valves to stop flow completely. Consult expert companies. Insignificant Rare 1 (Low) 1 3 V10, 26 November 2017 H31 Clogging of safety valve or other blow off devices upon activation due to solid formation of CO2 in blow off lines Pressures increase above design pressure, damage Operations Feed CO2 safety valves Yes HAZOP 2008 Meessen Stamicarbon Urea Plant Safety - A Review Moderate Moderate 9 (High) 9 Avoid stagnant lines at inlet (L/D<3) or provide tracing and insulation. Check that upstream temperature is above mentioned treshhold value (discharge 3rd and 4th stage downstream cooler are critical areas). Threshhold value at 80 bars is abt 45 degC and at 140 bars is abt 80 degC. Major Rare (5) Moderate 5 4 V10, 26 November 2017 H32 Fire due to leakage CO2 compressor lube oil Production loss, fire could be snuffed out before further damage Operations Feed CO2 compressor Yes Incident Database Incident 10-001 Minor Moderate 6 (Moderate) 6 Install fire detectors, cameras. Install oil system besides compressors / turbines. Minor Rare 2 (Low) 2 5 V10, 26 November 2017 H33 Fire / explosion during blow off due to icing and hydrogen ignition Damage plus possible casualties Operations Feed CO2 safety valves Yes Incident Database Incident XX-007 and XX-010 table/viewtopic.php?f=33&t=658 and Major Moderate (11) High 11 Lower explosion limit of hydrogen is 4 vol%, are these levels possible. Is fire possible ? Anybody has experience ? 6 V10, 26 November 2017 H34 Failure of separator of CO2 compressor causing wet corrosive CO2 Pipe failed during clamping Operations Feed CO2 section Yes Incident Database Incident 16-006 http://www.ureaknowhow.com/ukh2/round- Major Unlikely (8) High 8 The pipe was replaced by stainless steel. The efficiency of the liquid separator was improved. Do not apply clamps when the condition of the pipe is not clear. Apply experienced CO2 compressor vendors. In case of a leak stop the plant. Major Rare (5) Moderate 5 7 V10, 26 November 2017 H71 Rupture of HP CO2 line due to corrosion under insulation Unplanned shut down of the plant Operations Feed HP CO2 piping Yes Incident Database Incident XX-001 http://www.ureaknowhow.com/ukh2/round- Major Moderate (11) High 11 Insulated carbon steel at concerning temperatures has to be protected by a coating system or personal protection can be applied. Insulation should be in good condition. Regular inspections for atmospheric corrosion at critical areas is recommended. Be careful with flushing water. In case of a leak stop the plant. Major Rare (5) Moderate 5 8 V10, 26 November 2017 H94 Backflow from corrosive carbamate from synthesis to carbon steel CO2 feed line Failure HP piping Operations Feed HP CO2 piping Yes Incident Database Incident 16-004 http://www.ureaknowhow.com/ukh2/round- Major Almost certain (14) Intolerable 14 Two checkvalves in series with different design and high quality. Do not apply a design with vanes. Check valves to be installed in vertical line. Install a flushing connection upstream check valve to flush away solids. Install a fast closing MOV from DCS (some plants apply buffer vessel in CO2 supply line). Apply the specbreak upstream this MOV. Pay attention also to bypass / start up lines. In case of a leak stop the plant. Major Rare (5) Moderate 5 9 V10, 26 November 2017 H30 Explosion due to atmospheric corrosion of ammonia pipeline, erosion from process side Six fatalities and 25 people injured Operations Feed NH3 piping Yes Incident Database Incident 13-001 and XX-009 table/viewtopic.php?f=33&t=818 and Catastrophic Moderate (12) Intolerable 12 Do regular corrosion inspections. Colour ammonia lines for easy recognition. Assure proper quality of welds. Assure proper condition of insulation. What can be cause for erosion from process side, catalyst particles ? Any experience from others ? In case of a leak stop the plant. Catastrophic Rare (7) High 7 10 V10, 26 November 2017 H72 Significant wall thickness reduction of HP NH3 line due to atmospheric corrosion Repair during turnaround Operations Feed HP NH3 piping Yes Incident Database Incident XX-002 http://www.ureaknowhow.com/ukh2/round- Catastrophic Moderate (12) Intolerable 12 Apply a protective coating system on the pipeline also in the area of the clamp. Apply a glass fibre tape between the pipeline and the clamp. Avoid wetting of the pipeline during flushing the floor. Apply Good Practice when guiding a pipeline through concrete floors. In case of a leak stop the plant. Catastrophic Rare (7) High 7 11 V10, 26 November 2017 H74 HP NH3 pipelines ruptures due to backflow of corrosive carbamate Failure HP piping, large ammonia leak Operations Feed HP NH3 piping Yes Incident Database Incident 10-003 http://www.ureaknowhow.com/ukh2/round- Catastrophic Almost certain (15) Intolerable 15 Pay attention to high quality materials, proper design and installation of checkvalves, Install two checkvalves in series with different design, Pu spec break of pipe upstream fast closing Motor Operated Valve, Install flushing connection upstream checkvalves so that any solids can be flushed away from checkvalves. In case of a leak stop the plant. Catastrophic Rare (7) High 7 12 V10, 26 November 2017 H14 Isolation valve fails during maintenance HP NH3 pump 11 casualties, 10 injured Maintenance Feed HP NH3 pump Yes Incident Database Incident 92-002, N&S 2017 Fatima http://www.ureaknowhow.com/ukh2/round- Catastrophic Moderate (12) Intolerable 12 Install double block and bleed for isolation valves of HP NH3 and carbamate pumps or install blind plates, do proper maintenance on these block valves, limit number of people at these locations during maintenance, wear personal protection. Apply high quality vendor and higher alloy materials. Catastrophic Rare (7) High 7 13 V10, 26 November 2017 H2 Human error to solve a vibration problem of a valve in an ammonia line NH3 release to atmosphere Commissioning / Start Up Feed HP NH3 valve Yes Incident Database Incident 93-001 http://www.ureaknowhow.com/ukh2/round- Catastrophic Moderate (12) Intolerable 12 Prepare Standard Operating Procedures for operators and for start up and shut down phase. Perform vibration analysis on critical pipelines. Catastrophic Rare (7) High 7 14 V10, 26 November 2017 H35 same as H74 15 V10, 26 November 2017 H36 NH3 leak due to loosening packing ring of stuffing box HP reciprocating pump 3 people injured Operations Feed HP Pumps Yes Incident Database Incident 98-001 and 07-001 table/viewtopic.php?f=33&t=924 and Catastrophic Moderate (12) Intolerable 12 Perform proper (also preventive) maintenance on HP pumps, stuffing boxes have a limited lifetime Also check wear and tear of other related parts also like the condition of for example threads. Involve high quality and experienced companies. Catastrophic Rare (7) High 7 16 V10, 26 November 2017 H38 A rupture disc on NH3 system opened without proper noticing Large ammonia emission, complaints from neighbours Operations Feed NH3 heat exchangers Yes Incident Database Incident 98-002 http://www.ureaknowhow.com/ukh2/round- Moderate Unlikely (6) Moderate 6 Apply NH3 detection system for leaks of rupture discs as these do not close again after damage Moderate Rare (3) Moderate 3 17 V10, 26 November 2017 H39 NH3 pipeline weld joint fails Heavy ammonia leak Operations Feed NH3 piping Yes Incident Database Incident 08-001 table/viewtopic.php?f=33&t=1404 and Moderate Likely (11) High 11 Corrosion-fatigue resulting from combined action of an alternating stresses and corrosive environment. On line sealing of leakages either from pipes or weld joints should be avoided. Contrary to pure mechanical fatigue, there is no fatigue limit load in corrosion-assisted fatigue. Much lower failure stresses and much shorter failure times can occur in a corrosive environment. OMIFCO has decided not to do online sealing for any developed leakages on ammonia pipe lines. Consider Boreal NH3 detectors. Assure sufficient isolation possibilities (remotely controlled block valve) to limit ammonia emissions. In case of a leak stop the plant. Moderate Rare (3) Moderate 3 18 V10, 26 November 2017 H95 Severe corrosion of liquid NH3 transfer line due to corrosion under insulation Potential ammonia leak Operations Feed NH3 piping Yes Incident Database Incident XX-026 https://www.ureaknowhow.com/ukh 2/round-table/viewtopic.php?t=1588 Moderate Likely (11) High 11 Perform regular corrosion inspections. Assure proper insulation. Install an ammonia leak detection. Change to SS (also to avoid other corrosion risks like SCC due to oxygen. Moderate Rare (3) Moderate 3 19 V10, 26 November 2017 H40 Anhydrous ammonia splashes during sampling One person injured Operations Feed NH3 piping Yes Incident Database Incident XX-012 http://www.ureaknowhow.com/ukh2/round- Minor Almost certain (10) High 10 Apply proper sampling procedure. Perform job safety analysis. Wear sufficent personal protection Minor Rare 2 2 No: Hazard Scenarios Hazard Reference Information Mitigated Risk Ranking Support from our Sponsors Ref No. Prevention measures reducing Likelihood Mitigation measures reducing Consequences Loss Of Containment Risk Register Safety Hazards in Urea Plants V10: 26 November, 2017 Project phase Plant section Equipment item Unmitigated Risk Ranking Ref No.

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Page 1: Safety Hazards in Urea Plants V10 261117 - … shut down ... Ref No. Prevention measures reducing Likelihood Mitigation measures reducing Consequences Loss Of Containment Risk Register

Revision Hazard # Hazard & Initiating Event Consequences Safety Study Reference Link C L R Sponsor 1 Sponsor 2 Sponsor 3 Sponsor 4 Sponsor 5 Sponsor 6 C L R

1V10, 26

November 2017

H1 Leaking flange of CO2 line

One person passes out although a DCS alarm was on but unnoticed due to too many alarms during the start up phase

Commissioning / Start Up

Feed CO2 piping Yes Incident Database Incident XX-014 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1455

Moderate Moderate 9 (High) 9

CO2 is heavier than normal air and can collect at lower elevations reducing oxygen content to dangerous low levels. A proper CO2 detector including DCS alarm should be present. Flange leakages are to be checked after a start up. Personal should be aware of the risks of CO2. Pay attention to alarm management and alarm inflation.

Major Rare (5) Moderate 5

2V10, 26

November 2017

H13Acetic acid used for cleaning enters lube oil system of CO2 compressor via nitrogen network

Severe damage to bearings/seals Maintenance Feed CO2 compressor Yes Incident Database Incident 09-005 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1476

Insignificant Unlikely 2 (Low) 2 Perform risk analysis also for maintenance activiities, do not trust check valves to stop flow completely. Consult expert companies.

Insignificant Rare 1 (Low) 1

3V10, 26

November 2017

H31

Clogging of safety valve or other blow off devices upon activation due to solid formation of CO2 in blow off lines

Pressures increase above design pressure, damage

Operations Feed CO2 safety valves Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Moderate Moderate 9 (High) 9Avoid stagnant lines at inlet (L/D<3) or provide tracing and insulation. Check that upstream temperature is above mentioned treshhold value (discharge 3rd and 4th stage downstream cooler are critical areas). Threshhold value at 80 bars is abt 45 degC and at 140 bars is abt 80 degC.

Major Rare (5) Moderate 5

4V10, 26

November 2017

H32 Fire due to leakage CO2 compressor lube oil

Production loss, fire could be snuffed out before further damage

Operations Feed CO2 compressor Yes Incident Database Incident 10-001http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=309&p=7446#p7446

Minor Moderate 6 (Moderate) 6 Install fire detectors, cameras. Install oil system besides compressors / turbines. Minor Rare 2 (Low) 2

5V10, 26

November 2017

H33 Fire / explosion during blow off due to icing and hydrogen ignition

Damage plus possible casualties Operations Feed CO2 safety valves Yes Incident Database Incident XX-007 and XX-010

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=658 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=970

Major Moderate (11) High 11 Lower explosion limit of hydrogen is 4 vol%, are these levels possible. Is fire possible ? Anybody has experience ?

6V10, 26

November 2017

H34Failure of separator of CO2 compressor causing wet corrosive CO2

Pipe failed during clamping Operations Feed CO2 section Yes Incident Database Incident 16-006 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1438

Major Unlikely (8) High 8The pipe was replaced by stainless steel. The efficiency of the liquid separator was improved. Do not apply clamps when the condition of the pipe is not clear. Apply experienced CO2 compressor vendors.

In case of a leak stop the plant. Major Rare (5) Moderate 5

7V10, 26

November 2017

H71 Rupture of HP CO2 line due to corrosion under insulation

Unplanned shut down of the plant Operations Feed HP CO2 piping Yes Incident Database Incident XX-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=268

Major Moderate (11) High 11Insulated carbon steel at concerning temperatures has to be protected by a coating system or personal protection can be applied. Insulation should be in good condition. Regular inspections for atmospheric corrosion at critical areas is recommended. Be careful with flushing water.

In case of a leak stop the plant. Major Rare (5) Moderate 5

8V10, 26

November 2017

H94Backflow from corrosive carbamate from synthesis to carbon steel CO2 feed line

Failure HP piping Operations Feed HP CO2 piping Yes Incident Database Incident 16-004 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1428

Major Almost certain (14) Intolerable 14

Two checkvalves in series with different design and high quality. Do not apply a design with vanes. Check valves to be installed in vertical line. Install a flushing connection upstream check valve to flush away solids. Install a fast closing MOV from DCS (some plants apply buffer vessel in CO2 supply line). Apply the specbreak upstream this MOV. Pay attention also to bypass / start up lines.

In case of a leak stop the plant. Major Rare (5) Moderate 5

9V10, 26

November 2017

H30Explosion due to atmospheric corrosion of ammonia pipeline, erosion from process side

Six fatalities and 25 people injured Operations Feed NH3 piping Yes Incident Database Incident 13-001 and XX-009

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=818 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=903

Catastrophic Moderate (12) Intolerable 12Do regular corrosion inspections. Colour ammonia lines for easy recognition. Assure proper quality of welds. Assure proper condition of insulation.What can be cause for erosion from process side, catalyst particles ? Any experience from others ?

In case of a leak stop the plant. Catastrophic Rare (7) High 7

10V10, 26

November 2017

H72Significant wall thickness reduction of HP NH3 line due to atmospheric corrosion

Repair during turnaround Operations Feed HP NH3 piping Yes Incident Database Incident XX-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=269

Catastrophic Moderate (12) Intolerable 12Apply a protective coating system on the pipeline also in the area of the clamp. Apply a glass fibre tape between the pipeline and the clamp. Avoid wetting of the pipeline during flushing the floor. Apply Good Practice when guiding a pipeline through concrete floors.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

11V10, 26

November 2017

H74 HP NH3 pipelines ruptures due to backflow of corrosive carbamate

Failure HP piping, large ammonia leak

Operations Feed HP NH3 piping Yes Incident Database Incident 10-003 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=467

Catastrophic Almost certain (15) Intolerable 15

Pay attention to high quality materials, proper design and installation of checkvalves, Install two checkvalves in series with different design, Pu spec break of pipe upstream fast closing Motor Operated Valve, Install flushing connection upstream checkvalves so that any solids can be flushed away from checkvalves.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

12V10, 26

November 2017

H14 Isolation valve fails during maintenance HP NH3 pump

11 casualties, 10 injured Maintenance Feed HP NH3 pump Yes Incident Database Incident 92-002, N&S 2017 Fatima

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=280

Catastrophic Moderate (12) Intolerable 12Install double block and bleed for isolation valves of HP NH3 and carbamate pumps or install blind plates, do proper maintenance on these block valves, limit number of people at these locations during maintenance, wear personal protection. Apply high quality vendor and higher alloy materials.

Catastrophic Rare (7) High 7

13V10, 26

November 2017

H2Human error to solve a vibration problem of a valve in an ammonia line

NH3 release to atmosphere Commissioning / Start Up

Feed HP NH3 valve Yes Incident Database Incident 93-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=962

Catastrophic Moderate (12) Intolerable 12 Prepare Standard Operating Procedures for operators and for start up and shut down phase. Perform vibration analysis on critical pipelines.

Catastrophic Rare (7) High 7

14V10, 26

November 2017

H35 same as H74

15V10, 26

November 2017

H36NH3 leak due to loosening packing ring of stuffing box HP reciprocating pump

3 people injured Operations Feed HP Pumps Yes Incident Database Incident 98-001 and 07-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=924 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1425

Catastrophic Moderate (12) Intolerable 12Perform proper (also preventive) maintenance on HP pumps, stuffing boxes have a limited lifetime Also check wear and tear of other related parts also like the condition of for example threads. Involve high quality and experienced companies.

Catastrophic Rare (7) High 7

16V10, 26

November 2017

H38 A rupture disc on NH3 system opened without proper noticing

Large ammonia emission, complaints from neighbours

Operations Feed NH3 heat exchangers

Yes Incident Database Incident 98-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=764

Moderate Unlikely (6) Moderate 6 Apply NH3 detection system for leaks of rupture discs as these do not close again after damage

Moderate Rare (3) Moderate 3

17V10, 26

November 2017

H39 NH3 pipeline weld joint fails Heavy ammonia leak Operations Feed NH3 piping Yes Incident Database Incident 08-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1404 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic/php?f=33&t=1582

Moderate Likely (11) High 11

Corrosion-fatigue resulting from combined action of an alternating stresses and corrosive environment. On line sealing of leakages either from pipes or weld joints should be avoided. Contrary to pure mechanical fatigue, there is no fatigue limit load in corrosion-assisted fatigue. Much lower failure stresses and much shorter failure times can occur in a corrosive environment. OMIFCO has decided not to do online sealing for any developed leakages on ammonia pipe lines. Consider Boreal NH3 detectors.

Assure sufficient isolation possibilities (remotely controlled block valve) to limit ammonia emissions. In case of a leak stop the plant.

Moderate Rare (3) Moderate 3

18V10, 26

November 2017

H95Severe corrosion of liquid NH3 transfer line due to corrosion under insulation

Potential ammonia leak Operations Feed NH3 piping Yes Incident Database Incident XX-026 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1588

Moderate Likely (11) High 11 Perform regular corrosion inspections. Assure proper insulation. Install an ammonia leak detection. Change to SS (also to avoid other corrosion risks like SCC due to oxygen.

Moderate Rare (3) Moderate 3

19V10, 26

November 2017

H40 Anhydrous ammonia splashes during sampling

One person injured Operations Feed NH3 piping Yes Incident Database Incident XX-012 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1131

Minor Almost certain (10) High 10 Apply proper sampling procedure. Perform job safety analysis. Wear sufficent personal protection Minor Rare 2 2

No:Hazard Scenarios Hazard Reference Information Mitigated Risk RankingSupport from our Sponsors

Ref No. Prevention measures reducing Likelihood Mitigation measures reducing ConsequencesLoss Of

Containment

Risk Register Safety Hazards in Urea Plants V10: 26 November, 2017

Project phase Plant section Equipment itemUnmitigated Risk Ranking

Ref No.

Page 2: Safety Hazards in Urea Plants V10 261117 - … shut down ... Ref No. Prevention measures reducing Likelihood Mitigation measures reducing Consequences Loss Of Containment Risk Register

20V10, 26

November 2017

H3 NH3 leak due to a sight glass failure during start up

16 people injured Commissioning / Start Up

Feed NH3 pumps Yes Incident Database Incident 15-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1189

Catastrophic Moderate (12) Intolerable 12 Several recommendations are included in: http://www.ureaknowhow.com/ukh2/library/1190-2017-ureaknowhow-com-top-10-revamp-tools.html

Several recommendations are included in: http://www.ureaknowhow.com/ukh2/library/1190-2017-ureaknowhow-com-top-10-revamp-tools.html

Catastrophic Rare (7) High 7

21V10, 26

November 2017

H41

Large uncontrolled NH3 emission in case suction line of HP NH3 pump fails due to unwanted backflow scenario

As NH3 booster pump from NH3 plant keeps running, NH3 emission can be very large (SIL 3)

Operations Feed NH3 pumps Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Catastrophic Moderate (12) Intolerable 12 Install fast closing XEV to stop supply of NH3 from boosterpump or stop booster pump automatically. Wear personal protection when working on NH3 equipment

Catastrophic Rare (7) High 7

22V10, 26

November 2017

H37 CO2 breakthrough with ammonia recycle.

Internal corrosion, possible damage

Operations Feed NH3 recycle system Yes HAZOP http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=7&t=1519

Major Almost certain (14) Intolerable 14

Apply stainless steel liner with ammonia leak detection system or stainless steel buffer vessel. Apply stainless steel pipelines. Increase corrosion inspections of high pressure ammonia pump. Install a submerged medium pressure carbamate condenser upstream the washing column (also called MP Absorber).

In case of a leak stop the plant. Major Rare (5) Moderate 5

23V10, 26

November 2017

H15 Granulator door jammed close unexpectedly

One person injured Maintenance Finishing Granulation No Incident Database Incident XX-017 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1461

Moderate Almost certain (12) Intolerable 12 Mechanically secure the granulator doors in open position even when inspecting the granulator through open doors.

Moderate Rare (3) Moderate 3

24V10, 26

November 2017

H4

High pressure in suction line due to operating the melt pump with hot condensate and no / low flow conditions leading to steam formation

Sight glass damaged, 1 casualty and 2 people injured

Commissioning / Start Up

Finishing Melt pump Yes HAZOP Incident XX-013 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1303

Catastrophic Unlikely (10) High 10 Perform commissioning of melt pump with cold condensate, find alternative methods to test instrumentation. Apply a BUNGARTZ melt pump.

Catastrophic Rare (7) High 7

25V10, 26

November 2017

H12During construction of prill tower, accident occurred from high elevation

12 casualties, plant construction on hold

Construction Finishing Prill tower No Incident Database Incident 09-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=272

Catastrophic Unlikely (10) High 10 When working at high heights take care of extra security to avoid falling down. Inspect condition of carrier equipment

Catastrophic Rare (7) High 7

26V10, 26

November 2017

H16Julla falls down from 10 m height due to shearing of pinion of electrical winch

3 persons were badly injured and 2 fatalities was reported

Maintenance Finishing Prill tower No Incident Database Incident XX-008 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=896

Catastrophic Unlikely (10) High 10 Second holding of the julla to be made foolproof Catastrophic Rare (7) High 7

27V10, 26

November 2017

H17During cleaning or maintenance activities heavy lumps can fall down causing casualities

several casualties during several incidents

Maintenance Finishing Prill tower / Granulation

No Incident Database Incident 02-001 and 10-004

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=273 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=907

Moderate Almost certain (12) Intolerable 12 Working in a prill tower or granulator with urea lumps is dangerous: clean first maximum amount from outside. Make use of wet cleaning (refer to Nagarjuna paper)

Take care of proper protection Moderate Rare (3) Moderate 3

28V10, 26

November 2017

H18 Miscommunication during maintenance job

One injured Maintenance Finishing Reclaimer No Incident Database Incident XX-018 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1504

Moderate Moderate (9) High 9 Apply the safest possible procedure even if it takes more time Moderate Rare (3) Moderate 3

29V10, 26

November 2017

H19While trying to open clogged melt line, melt splasht out of 3-way valve or flange

one person injured (40 days in hospital) while wearing good personal protection

Maintenance Finishing Urea melt line Yes Incident DatabaseIncident 87-001 and XX-015 and

XX-016

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=329 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1457 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1460

Moderate Almost certain (12) Intolerable 12

Do not compromise on safety: Flush drain lines of urea melt lines twice per shift to ensure drain line is clear, perform job safety analysis to identify unsafe situations (e.g. no escape path close to 3-way valve, work with safety watches at risky situations. Be careful when heating up urea melt lines as gasses occur and pressures increase. Avoid overheating of urea melt lines, pay attention to no flow conditions. Apply a reliable melt pump.

Do not compromise on safety: Wear always the right and full cover personal protection.

Moderate Rare (3) Moderate 3

30V10, 26

November 2017

H20

People enter a pipeline (confined space) while welding was performed and welding gas was applied (inerts) leading to asphyxiation

Two casualties Maintenance Plant Confined spaces No Incident Database Incident 02-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=925

Catastrophic Unlikely (14) Intolerable 14 Apply proper precautions when entering confined spaces, measure oxygen, use a safeguard Catastrophic Rare (7) High 7

31V10, 26

November 2017

H21Crane collapses during maintenance job One casualty Maintenance Plant plant No incident Database Incident 15-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1140 Major Likely (13) Intolerable 13 Apply proper preparation procedures when using a crane, do a risk analysis Catastrophic Rare (7) High 7

32V10, 26

November 2017

H42 Gas pipeline ruptures Fire and plant shut down Operations Plant Piping Yes Incident Database Incident 11-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=451

Moderate Moderate (9) High 9 Apply high quality materials. Perform corrosion inspections of pipelines based on risk based inspection

In case of a leak stop the plant. Moderate Rare (3) Moderate 3

33V10, 26

November 2017

H22 Asphyxiation / unconscious while working on tank

one casualty, one person injured Maintenance Recirculation Atmospheric storage tanks

Yes Incident Database Incident 16-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1336

Catastrophic Likely (14) Intolerable 14 Pay attention that vapours can escape from vents from the tank while working on top of the tank. Perform a job safety analysis.

Catastrophic Rare (7) High 7

34V10, 26

November 2017

H5 Tank damages due to vacuum created in tank

Major damage Commissioning / Start Up

Recirculation Atmospheric storage tanks

Yes Incident Database Incident 15-003 & 03-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1273

Major Likely (13) Intolerable 13Be aware that condensing steam / gases by a cold stream can easily create vacuum, install a water seal on a tank as a 3" vent stack of 100 m height could not compensate the vacuum pressure in this incident

Major Rare (5) Moderate 5

35V10, 26

November 2017

H96Cracks in flash tank due to Chloride Stress Corrosion Cracking

Leak Operations Recirculation SS vessels and piping

Yes Incident Database Incident XX-028 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1590

Moderate Moderate (9) High 9 Assure proper insulation. Properly install tracing with spacers. Apply SS tracing. Apply coating on stainless steel when plant is located in marine atmosphere

In case of a leak stop the plant. Moderate Rare (3) Moderate 3

34V10, 26

November 2017

H43

Backflow from synthesis (discharge HP carbamate pumps) to recirculation (suction side) as during flushing mode the XPV (LPV) in the discharge is opened while people are in the area

Potential toxic ammonia release and/or high temperature/pressure carbamate release (SIL 2)

Operations Recirculation HP carbamate pumps

Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Major Moderate (11) High 11 Add position indicators on main blockvalves in order that XPV can only be opened in case pump is running or in case both pumps are stopped and blockvalves are closed

In case of a leak stop the plant. Major Rare (5) Moderate 5

35V10, 26

November 2017

H44Backflow from carbamate from synthesis causing reverse flow of HP centrifugal carbamate pump

Damage HP carbamate pump (SIL 2)

Operations Recirculation HP carbamate pumps

Yes HAZOP Moderate Moderate (9) High 9

Two checkvalves in series with different design and high quality. Apply duplex or super duplex as material of construction. Do not apply a design with vanes. Check valves to be installed in vertical line. Install a flushing connection upstream check valve to flush away solids. Install a fast closing XV which acts on TSHH in the line to the synthesis (some plants apply two XV in series).

In case of a leak stop the plant. Moderate Rare (3) Moderate 3

36V10, 26

November 2017

H45 Rupture of column due to hydrogen explosion

Major damage Operations Recirculation

MP scrubber, LP absorber and atmospheric

absorber

Yes Incident Database Incident 00-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1446

Major Moderate (11) High 11Install a hydrogen converter in CO2 feed, use ammonia feed from atmospheric pressure (no dissolved H2 and CH4), be aware of flushing with condensate which can increase H2/NH3 ratio (larger explosive area). Apply an explosion dome or 7 times higher design pressure.

Insignificant Rare (1) Low 1

37V10, 26

November 2017

H46 Rupture of ammonia water tank due to hydrogen explosion

Major damage Operations Recirculation NH3 water tank Yes Incident Database Incident 82-001 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1586 (2 incidents)

Major Moderate (11) High 11 Install a hydrogen converter in CO2 feed, use ammonia feed from atmospheric pressure (no dissolved H2 and CH4), consider explosion risks in ammonia tank

Moderate Rare (3) Moderate 3

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38V10, 26

November 2017

H47 Several scenarios lead to high pressure in the recirculation

Potential toxic ammonia release and /or high temperature /pressure carbamate release

Operations Recirculation Rectifyer Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Major Moderate (11) High 11Safety valve plus high pressure switch to realise the required Probability of Failure on Demand. The high pressure switch activates synthesis blocking situation. Apply a reliable pressure measurement. Apply a reliable safety valve.

Major Rare (5) Moderate 5

39V10, 26

November 2017

H23 Vent line of ammonia water tank explodes during grinding

One casualty and one injured Maintenance Recirculation Tanks Yes Incident Database Incident XX-020 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1513

Catastrophic Moderate (12) Intolerable 12Assure proper blinding (spectacle blinds, double block and bleed) when doing maintenance or inspections on a equipment item. Perform a risk analysis before starting the job. Apply proper winterising measures

Catastrophic Rare (7) High 7

40V10, 26

November 2017

H48Hot fluid splashes (this risk is high with process fluids which easily crystallise)

Injuries Operations

Recirculation, evaporation and

waste water treatment

Sample valves Yes HAZOP Moderate Moderate (9) High 9 Make use of Tyco (Yarway) sample valves with no dead volume at inlet side Moderate Rare (3) Moderate 3

41V10, 26

November 2017

H49 Sight glass ruptures One casualty and 2 people injured, all in one case

OperationsReciruclation/Evapor

ation/waste water treatment

Sight glass Yes Incident Database Incident XX-013 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1303

Catastrophic Moderate (12) Intolerable 12Several recommendations. Refer to Round Table discussion (refer to: http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1303). Apply non-cavitating BUNGARTZ pump.

Several recommendations. Refer to Round Table discussion (refer to: http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1303). Apply non-cavitating BUNGARTZ pump.

Insignificant Rare (1) Low 1

42V10, 26

November 2017

H50 Crystallisation risks in flare headers

Rupture of vessels in case safety valve cannot relief sufficiently

Operations Relief system Flare Yes HAZOP Catastrophic Unlikely (10) High 10 Pay proper attention to design (sufficient flushing, slope lay out, proper pipe diameters, etc) and operation procedures. Apply high quality safety valves designed for carbamate

Catastrophic Rare (7) High 7

43V10, 26

November 2017

H51 Exposion risks in flare headers Rupture of flare header Operations Relief system Flare Yes HAZOP Catastrophic Unlikely (10) High 10 Pay proper attention to design (sufficient flushing, etc) and operation procedures. Apply high quality safety valves designed for carbamate

Catastrophic Rare (7) High 7

44V10, 26

November 2017

H52 Drain line ruptures due to corrosion/erosion

Large loss of containment Operations Synthesis Drain piping system Yes Incident Database Incident 09-003 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1474

Catastrophic Unlikely (10) High 10 Better design of drain system with double block and bleed possibilities. Be aware that drain valves easily pass. Apply high quality vendor and higher alloy materials (duplex).

In case of a leak stop the plant. Catastrophic Rare (7) High 7

45V10, 26

November 2017

H53

316L UG High Pressure carbamate gas line ruptures due to condensation corrosion and dead end design

Large ammonia emission, plant shut down, no casualties

Operations Synthesis HP carbamate gas lines

Yes Incident Database Incident 11-003

https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=945&p=5045#p5045

Major Moderate (11) High 11

Avoid dead ends. Apply proper tracing and insulation so that condensation will be avoided (dew point typically higher than 160 degC), apply stainless steel with small grain size or apply higher alloy material (25-22-2 or duplex). Perform corrosion inspections for HP gas lines and weldolets. End of lifetime for 316L UG high pressure gas lines is some 30 years.

In case of a leak stop the plant. Major Rare (5) Moderate 5

46V10, 26

November 2017

H54 High Pressure reactor offgas line leaks from weld defect

Ammonia detectors alaram, plant shut down, no casualties

Operations Synthesis HP carbamate gas lines

Yes Incident Database Incident 15-004 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1555

Major Moderate (11) High 11

Apply proper tracing and insulation so that condensation will be avoided (dew point typically higher than 160 degC). Apply stainless steel with small grain size or apply higher alloy material (25-22-2 or duplex). Perform corrosion inspections for HP gas lines and weldolets. End of lifetime for 316L UG high pressure gas lines is some 30 years.

In case of a leak stop the plant. Major Rare (5) Moderate 5

47V10, 26

November 2017

H6Major leak at main flange high pressure carbamate condenser during start up after turnaround

Large ammonia emission, no casualties, delay of start up

Commissioning / Start Up

Synthesis HP Equipment Yes Incident Database Incident XX-023

https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1564&p=7785#p7785

Catastrophic Moderate (12) Intolerable 12

A tightness check was performed with MP steam prior to NH3 feed in. A tightness check at a higher pressure with less hazardous media such as nitrogen or CO2 is under development. Doublecheck design and actual bolt loads of HP equipment items. Make use of experienced and reliable fabricators for HP equipment and piping.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

48V10, 26

November 2017

H55 Failure of pressure bearing wall due to leak in overlay welding

Urea / carbamate leaked through insulation

Operations Synthesis HP Equipment Yes Incident Database Incident 78-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=883

Major Moderate (11) High 11 Perform corrosion inspections during turnaround. Apply higher alloy materials for repair or replacement of protective layer in HP equipment

In case of a leak stop the plant. Major Rare (5) Moderate 5

49V10, 26

November 2017

H56Failure of urea reactor due to no proper leak detection system (exact cause not clear)

Major damage Operations Synthesis HP Equipment Yes Incident Database Incident 77-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=885

Catastrophic Likely (14) Intolerable 14 Install a vacuum based leak detection system with a reliable and accurate ammonia detector. In case of a leak stop the plant. Catastrophic Rare (7) High 7

50V10, 26

November 2017

H57Leak in loose liner of urea reactor due to no proper leak detection system

Damage of carbon steel pressure bearing wall

Operations Synthesis HP Equipment Yes Incident Database Incident 79-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=886

Catastrophic Likely (14) Intolerable 14 Install a vacuum based leak detection system with a reliable and accurate ammonia detector. Pay attention to a proper design of the nozzles of HP equipment.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

51V10, 26

November 2017

H58HP scrubber ruptures due to not commissioning all leak detection holes

Major damage Operations Synthesis HP Equipment Yes Incident Database Incident 98-003 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1364

Catastrophic Moderate (12) Intolerable 12 Asssure the correct and complete installation of a leak detection system to all leak detection holes. In case of a leak stop the plant. Catastrophic Rare (7) High 7

52V10, 26

November 2017

H24Stripgas entered reactor during blocking in causing active corrosion of protective layer

Risk of damage of carbon steel pressure bearing wall

Maintenance Synthesis HP Equipment No Incident Database Incident 13-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1348

Catastrophic Unlikely (10) High 10

During blocking in monitor the vessel temperatures for any heat increases. If the temperatures increase by more than 20F, the synthesis loop must immediately be drained. Assure positive isolation of CO2 when the loop is blocked in by monitoring loop pressure. Ensure operators close the isolation valve downstream of HIC-1201. Modify the Urea Plant startup procedure to include lab analysis of the stripper bottoms for metals found in the stainless steel liner, specifically Ni as it will be dissolved in the solution. The first sample must be taken within 12 hours of startup and the second 24 hours later. If the values are stable or decreasing, no action is required. If the values are increasing, the plant will be shut down and drained.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

53V10, 26

November 2017

H59

Cracks from outside in carbon steel pressure bearing wall due to dripping of carbamate from a leaking flange

Major damage Operations Synthesis HP Equipment Yes Incident Database Incident 94-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1365

Catastrophic Unlikely (10) High 10 Avoid that leaking carbamate can drip on high pressure urea equipment. In case of a leak stop the plant. Catastrophic Rare (7) High 7

54V10, 26

November 2017

H60 Severe damage of liner (cause not clear)

Replacement of liner Operations Synthesis HP Equipment Yes Incident Database Incident 12-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1439

Assure a proper active vacuum based leak detection system with a reliable and accurate ammonia analyser

In case of a leak stop the plant.

55V10, 26

November 2017

H61Liner bulges and ruptures due to too high pressure behind the liner or due to draining the synthesis

Severe damage of liner and extensive repair

Operations Synthesis HP Equipment Yes Incident Database Incident 09-004 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1475

Catastrophic Moderate (12) Intolerable 12 Be aware that pressure difference over liner is very limited. Apply a vacuum based leak detection system. Be careful with draining, install a vacuum pressure measurement in synthesis

In case of a leak stop the plant. Catastrophic Rare (7) High 7

56V10, 26

November 2017

H62Tubesheet of PoolCondenser damaged due to erosion corrosion steam side

Leak in overlay weld was detected and plant was shut down

Operations Synthesis HP Equipment Yes Incident Database Incident 16-007 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1562

Catastrophic Moderate (12) Intolerable 12 Assure proper quality of steam condensate. Install stainless steel sleeves in tubesheet. In case of a leak stop the plant. Catastrophic Rare (7) High 7

57V10, 26

November 2017

H64Failure of titanium level pipe due to corrosion (hydrogen enbrittlement below fouling)

Large emission of carbamate / ammonia

Operations Synthesis HP Equipment Yes Incident Database Incident 16-005 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1436

Catastrophic Unlikely (10) High 10Be aware of fouling as below fouling active corrosion can occur or with titanium as material hydrogen enbrittlement (hydrogen is formed with carbamate corrosion reaction without oxygen present)

In case of a leak stop the plant. Catastrophic Rare (7) High 7

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58V10, 26

November 2017

H63Damage of carbon steel pressure bearing wall due to leakage of protecting sleeve in nozzle

Not clear but possibly bad design and thermal stresses

Operations Synthesis HP Equipment Yes Incident Database Incident 03-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1454

Catastrophic Moderate (12) Intolerable 12Pay attention in the detailed design and fabrication and inspection of nozzles of HP urea equipment. Install a proper leak detection system for loose liners. Perform corrosion inspections at regular intervals and pay attention to leaks in the urea plant.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

59V10, 26

November 2017

H97 Risk of cracks in SS nozzle of HP equipment and HP piping

Leaks, risk of loss of integrity Operations Synthesis HP Equipment and Piping

Yes Incident Database Incident XX-027 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1589

Catastrophic Unlikely (10) High 10Assure proper insulation. Install a cabine on top of reactor to protect against moisture and marine atmosphere. Properly install tracing with spacers. Apply SS tracing. Apply coating on stainless steel when plant is located in marine atmosphere

In case of a leak stop the plant. Catastrophic Rare (7) High 7

60V10, 26

November 2017

H7

Pressure gauge ruptures after HP flush pump is put in operation due to malfunctioning pressure control valve

Unsafe situation Commissioning / Start Up

Synthesis HP flush pump Yes Incident Database Incident 11-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=388

Catastrophic Unlikely (10) High 10 Assure proper functioning of pressure control valve and relief valve In case of a leak stop the plant. Catastrophic Rare (7) High 7

61V10, 26

November 2017

H65Tube rupture leads to high pressure on steam or cooling water side

Pressure on steam or cooling water side will be higher than design, damage with realease of carbamate and toxic ammonia

Operations Synthesis HP Heat Exchangers

Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Catastrophic Moderate (12) Intolerable 12

Sometimes steam side is protected by a rupture disc, but spurious activation has led to a large release. Steam side are also typically protected by a safety valve, which also blows off at tube rupture. Analysis has shown this safety valve is sufficient and blow off needs to be located to safe loaction (suitable for large ammonia release). In case of cooling water on shell side a rupture disc remains necessary (assure safey location of blow off).

Catastrophic Rare (7) High 7

62V10, 26

November 2017

H66 Failure of the tube to tubesheet weld

Carbamate entering the steam / cooling water side, potential risk of corrosion of carbon steel tubesheet

Operations Synthesis HP Heat Exchangers

Yes Incident Database Incident XX-006 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=880

Catastrophic Moderate (12) Intolerable 12 Apply a conductivity measurement to detect leak. Do not expand tubes in the tubesheet during fabrication of the heat exchanger.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

63V10, 26

November 2017

H98Failure of tube in tubesheet are due to chloride stress corrosion cracking

Carbamate entering the steam / cooling water side, potential risk of corrosion of carbon steel tubesheet

Operations Synthesis HP Heat Exchangers

Yes Incident Database Catastrophic Moderate (12) Intolerable 12Apply a conductivity measurement to detect leak. Do not expand tubes in the tubesheet during fabrication of the heat exchanger. Pay attention to chloride levels especially in case of austenitic stainless steels. Apply duplex materials.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

64V10, 26

November 2017

H67

Chloride from atmosphere (cooling water effluent, marine atmosphere) entering the steam condensate system via atmospheric steam condensate tank

Chlorides causing chloride stress corrosion cracking in for example the falling film high pressure carbamate condenser or high pressure scrubber in gap between tubes and tubesheet

Operations Synthesis HP Heat Exchangers

Yes HAZOP Catastrophic Moderate (12) Intolerable 12Assure always a higher pressure than atmospheric pressure in atmospheric steam condensate tank, check conductivity on steam side of HP heat exchangers leaks in tubes or tube-tubesheet welds. Apply (super)duplex materials.

Catastrophic Rare (7) High 7

65V10, 26

November 2017

H68

316L UG HP pipeline at inlet of reactor (conventional plant) ruptures due to erosion corrosion close to thermowell

Luckily no injuries, unplanned shut down and repair

Operations Synthesis HP pipeline Yes Incident Database Incident 09-006 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1515

Catastrophic Moderate (12) Intolerable 12Also take into consideration erosion corrosion caused by turbulence of internals in piping and vesselsApply better grades of materials like 25-22-2 or duplex.

Catastrophic Rare (7) High 7

66V10, 26

November 2017

H8 Leaking flange connection in high pressure pipeline

Risk of corrosion of carbon steel flanges, bolts and nuts, loss of integrity

Commissioning / Start Up

Synthesis HP piping Yes HAZOP Catastrophic Likely (14) Intolerable 14 Apply right torques and high quality materials. Use clean bolts and nuts which are both in good condition. Do not reuse lens rings.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

67V10, 26

November 2017

H26 Rupture of weldolet after trial to stop leak by installing a clamp

Four casualties and 4 people injured

Maintenance Synthesis HP piping Yes Incident Database Incident 00-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=292

Catastrophic Unlikely (10) High 10

Assure the quality of the applied materials fulfils the minimum requirements; Apply higher alloy materials (25-22-2 or duplex). Assure the quality of the installation and welding services. Apply better designs for weldolets with no dead volume. Pay attention to the right location of the weldolet (avoid gas phase). Perform proper inspections and testing during installation and after repair procedures (hydrotest, X-ray test of weld-o-let). Perform regular corrosion inspections of critical areas especially in plants older than 20 years. Never apply a clamp on a carbamate containing pipeline.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

68V10, 26

November 2017

H27 During hot bolting gasket fails One casualty Maintenance Synthesis HP piping Yes Incident Database Incident 14-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1016

Catastrophic Likely (14) Intolerable 14 Never apply hot bolting at high pressures In case of a leak stop the plant. Catastrophic Rare (7) High 7

69V10, 26

November 2017

H69 Rupture high pressure flange connection in synthesis section

Large ammonia/carbamate emission, complaints from neighbours

Operations Synthesis HP piping Yes Incident Database Incident 05-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=946

Catastrophic Likely (14) Intolerable 14

Carbon steel is not corrosion resistant and corrosion rate is very high. The installation of all equipment in the HP loop must be performed only by specialists with the right material. An independent check must be performed on all flanges in the HP section to check all dimensions. Grooves have been made in the carbon steel flange to allow the carbamate to escape

In case of a leak stop the plant. Catastrophic Rare (7) High 7

70V10, 26

November 2017

H70 HP butterfly valve twists leading to leakage

NH3/carbamate emission plus in ammonia plants risk for fire

Operations Synthesis HP piping Yes Incident Database Incident 10-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=333

Catastrophic Moderate (12) Intolerable 12 Pay proper attention to the installation of high pressure butterfly valves between flanges with lens gaskets, consider the new BHDT design for these valves

In case of a leak stop the plant. Catastrophic Rare (7) High 7

71V10, 26

November 2017

H73HP carbamate gas line ruptures due to strain induced intergranular cracking (SIIC)

Unsafe situation, large ammonia emission, plant shut down

Operations Synthesis HP piping Yes Incident Database Incident 09-002 and 12-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=404 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=927

Catastrophic Moderate (12) Intolerable 12

Apply proper tracing and insulation so that condensation will be avoided (dew point typically higher than 160 degC), apply stainless steel with small grain size or apply higher alloy material (25-22-2 or duplex). Perform corrosion inspections for HP gas lines. End of lifetime for 316L UG high pressure gas lines is some 30 years.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

72V10, 26

November 2017

H75

316L UG liquid outlet line HP NH3 stripper leaks due to relatively high temperature and as a consequence higher corrosion rates

Carbamate / ammonia can injure people

Operations Synthesis HP Piping Yes HAZOP Catastrophic Moderate (12) Intolerable 12Replace pipe by better material like 25-22-2 or duplex. Perform regular corrosion inspections. Apply continuous corrosion measurement (EMERSON Permasense). Refer to: http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1525

Catastrophic Rare (7) High 7

73V10, 26

November 2017

H76 Rupture of HP drain valve due to corrosion thread during leakage

4 people get injured, a great deal of damages, 5 days plant shut down

Operations Synthesis HP Piping Yes Incident Database Incident 17-001 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1571

Catastrophic Moderate (12) Intolerable 12Apply high pressure valves from a reliable and experienced high pressure urea valve vendor, In case of a leak stop the plant (pay special attention to leaks along threads), Assure the presence and pay proper attention to leak detection holes in high pressure valves

In case of a leak stop the plant. Catastrophic Rare (7) High 7

74V10, 26

November 2017

H77Crack in stripper liquid outlet pipeline due to heavy vibrations (this happened two times)

Leak, plant was shut down Operations Synthesis HP Piping Yes Incident Database Incident XX-024 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1574

Catastrophic Moderate (12) Intolerable 12Pay proper attention to vibrating pipelines. Perform vibration analysis of the piping system to determine better supporting system. In case of a leak stop the plant. Catastrophic Rare (7) High 7

75V10, 26

November 2017

H25Rupture of valve due to high pressure pocket during maintenance

In one incident one casualty, in another case one person injured

Maintenance Synthesis HP piping Yes Incident Database Incident 01-002 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=662

Catastrophic Moderate (12) Intolerable 12 Be aware that high pressure lines / valves can contain high pressure pockets and apply proper maintenance procedures taking this into account.

Wear proper personal protection. Catastrophic Rare (7) High 7

76V10, 26

November 2017

H78 High vibrations of discharge line HP reciprocating carbamate pump

High pressure carbamate line ruptures, hot carbamate sprays around, luckily nobody got injured

Operations Synthesis HP Pumps Yes Incident Database Incident XX-019 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1510

Catastrophic Moderate (12) Intolerable 12Pay proper attention to the the welding and installation of discharge pipelines of high pressure pumps. In case of severe vibrations, stop the plant and improve the installation, consider dampeners in case of reciprocating pumps. Install vibration detectors on vibration sensitive pipelines

Catastrophic Rare (7) High 7

77V10, 26

November 2017

H79 Failure of HP scrubber due to hydrogen explosion

Major damage Operations Synthesis HP scrubber Yes Incident Database Incident 74-001 and 00-002

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=884 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1446

Catastrophic Almost certain (15) Intolerable 15

Install a hydrogen converter in CO2 feed, use ammonia feed from atmospheric pressure (no dissolved H2 and CH4), monitor H2 content downstream hydrogen converter, never close inert valve, be aware of flushing with condensate in HP scrubber which can increase H2/NH3 ratio (larger explosive area). Apply an explosion dome HP scrubber

Insignificant Rare (1) Low 1

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78V10, 26

November 2017

H80Hot fluid splashes, balloon collapses during sampling at high pressure section

Injuries Operations Synthesis Sample valves Yes HAZOP Moderate Likely (11) High 11 Make use of the BHDT Zero Dead Volume HP Sampling Valve Moderate Rare (3) Moderate 3

79V10, 26

November 2017

H81 Rupture of HP stripper due to fabrication defect

12 casualties, 71 mln US$ financial loss

Operations Synthesis Stripper Yes Incident Database Incident 90-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=278

Catastrophic Moderate (12) Intolerable 12 Assure a proper design and experienced and qualified fabricator for HP urea vessels. Perform quality control during fabrication.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

80V10, 26

November 2017

H82 Several scenarios lead to high pressure in the synthesis

Potential toxic ammonia release and /or high temperature /pressure carbamate release (SIL 3)

Operations Synthesis Synthesis Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Catastrophic Almost certain (15) Intolerable 15Safety valve plus high pressure switch to realise the required Probability of Failure on Demand. High pressure switch activates synthesis blocking situation. Apply a reliable pressure measurement. Apply a reliable safety valve. Assure a proper blow off to safe location.

Catastrophic Rare (7) High 7

81V10, 26

November 2017

H28 Steam supply to the HP stripper during blocking in situation

Pressure higher than design, damage (SIL 3)

Maintenance Synthesis Synthesis Yes HAZOPDieltjes SIL

Classification in Urea Plants

Catastrophic Unlikely (10) High 10Safety valve plus high pressure switch to realise the required Probability of Failure on Demand. Switch activates synthesis blocking situation (closing steam supply). Apply a reliable pressure measurement.

Catastrophic Rare (7) High 7

82V10, 26

November 2017

H9 Failure of flanged head connection of a urea reactor

Major damage Commissioning / Start Up

Synthesis Urea Reactor Yes Incident Database Incident 10-005 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1276

Catastrophic Moderate (12) Intolerable 12Avoid a design with a cooling jacket, apply a proper vacuum based leak detection system with an accurate and reliable ammonia detector. Never flush leak detection circuits with steam or condensate or water.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

83V10, 26

November 2017

H10Reactor ruptures due to bad maintenance practice of closing the manway cover

One person injured due to toxic ammonia (double lung transplantation)

Commissioning / Start Up

Synthesis Urea Reactor Yes Incident Database Incident 01-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=515

Catastrophic Moderate (12) Intolerable 12 Apply proper maintenance procedures and experienced and qualified services companies. Apply the right gaskets. Treat high pressure urea vessels as critical equipment

In case of a leak stop the plant. Catastrophic Rare (7) High 7

84V10, 26

November 2017

H83Rupture of reactor due to active corrosion due to weld defect in weld clip to liner

Rupture of reactor leading to severe damage to the plant, 10 people injured inside and 90 people outside the battery limits

Operations Synthesis Urea Reactor Yes Incident Database Incident 92-001http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=267&p=1188#p1188

Catastrophic Moderate (12) Intolerable 12

Proper active vacuum based leak detection system for loose liners with a reliable and accurate ammonia detector in operation, procedure to shut down the plant in case a leak is identified, apply a full penetration weld, proper quality control of critical welds, proper design of clip so that proper welding is possible, use high alloy welding material, include clip welds in corrosion inspection program

In case of a leak stop the plant. Catastrophic Rare (7) High 7

85V10, 26

November 2017

H85

Rupture of reactor due to stress corrosion cracking of carbon steel pressure bearing wall due to flushing of leak detection system with water and bad design leak detection holes in multi layer vessel

4 casualties, 32 injured Operations Synthesis Urea Reactor Yes Incident Database Incident 05-001 and 95-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=276

Catastrophic Moderate (12) Intolerable 12

Flushing leak detection systems with steam or condensate can introduce substances leading to stress corrosion cracks in the pressure bearing carbon steel wall. A proper sealing (design) is required between the leak detection holes and the first carbon steel layer. The same is valid for the nozzles of a high pressure urea equipment item.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

86V10, 26

November 2017

H86Rupture of urea reactor due to cracks in carbon steel behind the liner

Significant part of plant was destroyed, plant never started up again, no casualties

Operations Synthesis Urea Reactor Yes Incident Database Incident 04-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=550

Catastrophic Moderate (12) Intolerable 12 Avoid any contamination in space between loose liner and carbon steel. Do not flush a leak detection system with water

In case of a leak stop the plant. Catastrophic Rare (7) High 7

87V10, 26

November 2017

H87 Rupture of urea reactor due to defect in titanium liner

Massive damage and long period forced shut down

Operations Synthesis Urea Reactor Yes Incident Database Incident 90-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=618

Catastrophic Moderate (12) Intolerable 12Apply an active leak detection system with an accurate and reliable ammonia detector. Perform corrosion inspections at regular intervals. Choose higher alloy material of conctruction for protective layer

In case of a leak stop the plant. Catastrophic Rare (7) High 7

88V10, 26

November 2017

H88

Rupture of reactor due to stress corrosion cracking of carbon steel pressure bearing wall due to cooling jacket

Stress corrosion cracking Operations Synthesis Urea Reactor Yes Incident Database Incident 64-001 and 59-001

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1443 and http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1444

Catastrophic Unlikely (10) High 10Do not apply cooling jackets for HP urea equipment. Do not flush leak detection systems with water. Take care of proper insulation of HP equipment so that water / moisture cannot enter. Build a shelter on top of HP equipment.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

89V10, 26

November 2017

H84

Rupture of or cracks in pressure bearing wall due to atmospheric corrosion (Nitrate stress corrosion cracking)

Repair during turnaround or new reactor required

Operations Synthesis Urea Reactor Yes Incident Database Incident XX-003 and XX-004

http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=270, http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=275

Catastrophic Moderate (12) Intolerable 12

Regular corrosion inspections also for atmospheric corrosion is recommended. Take care of a proper aluminum cover sheeting to avoid ingress of water contaminated with nitrate and/or urea (especially at critical locations like supports, insulation rings). In case of risk of nitrate (or urea) contamination carbon steel equipment and piping operating at temperatures in between -10 and +240 oC have to be coated. The angle iron insulation support ring should be fixed on the carbon steel shell in area with a lower stress level. Consider a shelter on top of HP vessels.

In case of a leak stop the plant. Catastrophic Rare (7) High 7

90V10, 26

November 2017

H89 Explosion / damage of motor Major damage Operations Synthesis, Hydrolyser

HP pumps, hydrolyser pump

Yes Incident Database Incident 16-001 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1294

Major Unlikely (8) High 8 Pay attention to proper alignment, perform regular and preventive checks on condition (vibrations) of heavy duty centrifugal pumps

Major Rare (5) Moderate 5

91V10, 26

November 2017

H90Crystallisation of carbamate and clogging upstream or downstream safety valve

High pressures than design leading to potential damage and carbamate / NH3 release

Operations Synthesis/Recirculartion

Safety valves Yes HAZOP

2008 Meessen Stamicarbon Urea

Plant Safety - A Review

Catastrophic Moderate (12) Intolerable 12

Trace pipeline upstream safety valve, trace body of safety valve and flush body and downstream pipeline of safety valve (best solution is LESER Flush safety valve). Note: A rupture disc upstream the safety valve introduces risks that parts of the rupture disc get stuck in the safety valve (source AICHE 1966 Safety Problems in Urea Plants)

Catastrophic Rare (7) High 7

92V10, 26

November 2017

H29Failure of wooden structure of cooling water unit in some 15 Indian plants

Significant damage and production loss

Maintenance Utilities Cooling water unit No Incident Database Incident XX-005 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=516

Minor Moderate (6) Moderate 6 Check design of wooden structure and avoid large weights at higher elevations, do proper quality control, perform proper corrosion inspections

Minor Rare (2) Low 2

93V10, 26

November 2017

H91 Fire in cooling water unit due to leak in heat exchanger

2 mln US$ financial loss and 55 days out of operation

Operations Utilities Cooling water unit Yes Incident Database Incident 97-001http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=298. Minor safety risk but catastrophic financal risk

Minor Likely (8) High 8 H2 and NH3 analyser in each cooling water cell (FFBL) Minor Rare (2) Low 2

94V10, 26

November 2017

H11 Boiler explodes due to explosive mixture in boiler

3 casualties and 5 people injured Commissioning / Start Up

Utilities Steam boiler Yes Incident Database Incident 16-003 http://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?f=33&t=1392

Catastrophic Moderate (12) Intolerable 12

Boilers, furnaces and reformer to be charged with fuel gas only when furnace draft fans are put into operation. Standard operating procedure to be modified accordingly. Fuel gas line leak test to be strictly done with nitrogen. Proper interdepartmental communication to be ensured between maintenance supervisor and control room and work area to be cleared of contract workman before initiating start up activities.

Catastrophic Rare (7) High 7

95V10, 26

November 2017

H92Explosion poly-ethylene tank due to reaction between hypochlorite and urea

One person died and several injured

Operations Utilities Storage tank Yes Incident Database Incident 08-002 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1563

Catastrophic Unlikely (10) High 10 Apply always Safety First and do not hurry. Read MSDS's. Train people. Be careful with reusing containers.

Catastrophic Rare (7) High 7

96V10, 26

November 2017

H93Explosion ammonia water tank due to combining NH3 and urea plant drain system

Damage the vessel, pipeline and instrumentation around it. No casualties.

Operations Waste water treatment

Ammonia water tank Yes Incident Database Incident XX-022 https://www.ureaknowhow.com/ukh2/round-table/viewtopic.php?t=1553

Catastrophic Unlikely (10) High 10 Separate drain and vent system for ammonia and urea plant. Prepare proper Standard Operating Procedures for draining and venting for start-up and normal cases in both ammonia and urea plants.

Catastrophic Rare (7) High 7