recollections of a uk boiling water reactor · 2018-03-05 · being a boiling water reactor and...
TRANSCRIPT
Recollections of a UK Boiling Water Reactor
INTRODUCTION
This document is a summary of some thoughts and
recollections from operating experience with the
Steam Generating Heavy Water Reactor (SGHWR)
at Winfrith. Whilst the reactor systems were
complex and numerous, this document
concentrates on aspects that may be common to
issues that affect more conventional boiling water
reactors. SGHWR had many unique features such
as a rapid acting liquid shutdown system, direct
emergency cooling water injection and vertical
primary circuit pressure tubes, however, it was
basically a boiling water reactor (~330 MW(th))
with direct production of steam fed to a
conventional 100MW turbine alternator.
I hope the readers of this report and those hearing
the associated presentation will find the
information in it of interest and value.
My thanks go to the staff at Winfrith, both past and
present, who were colleagues at the time and have
helped me find some of the old photographs and
drawings that I have used.
BACKGROUND AND CREATION OF THE PROTOTYPE
In the early 1960s, the UK was looking for options for moving on from the first generation of Magnox
power stations which were just getting into their stride. The prototype advanced gas cooled reactor
started operation at Windscale in 1962, but other options were being considered. With an eye to
developing the export market, a design that could be “modularized” was looked for.
Out of this work the United Kingdom Atomic Energy Authority (UKAEA) developed the Steam
Generation Heavy Water Reactor design. The concept was radically different from previous power
reactors built in the UK in that a single pressure vessel was replaced by pressure tubes, and it was
light water cooled, direct cycle and heavy water moderated; however, it shared many characteristics
with the already proven CANDU design.
2
The Authority gained approval from government to
construct a medium size, electricity generating
prototype at its reactor development facility
recently opened at Winfrith Heath in Dorset. The
project involved a number of private sector power
industry partners including International
Combustion and AEI. Construction started in 1962
and commissioning in early 1967. The reactor first
went critical in September 1967, was first
connected to the local electrical grid system on the
24th December. It reached nominal full power for
the first time in late January 1968.
There was an extensive development programme
over the following years, but once the commercial
One of the steam drums development of the SGHWR concept was set aside
in the late 1970s, the plant continued to operate on
a semi-commercial basis, reliably generating electricity to feed both the rest of the Winfrith site and
the local electricity grid.
Rising costs, ageing materials and enhanced safety standards led to the decision to cease generation
in 1990 after 23 years of operation. The plant then entered a post operational clean out stage.
Since then, the plant has gone through periods of decommissioning interspersed with times of care
and maintenance when funding was low. Final decommissioning is now in hand with the objective
of the land reverting to heathland by 2023.
SGHWR BASICS
3
PRIMARY CIRCUIT The SGHWR primary light water cooling circuit was in two symmetrical halves, each having 52
vertical pressure tubes (with associated feeder and riser pipes), two primary circulating pumps and
one steam drum. The fuel assemblies (consisting initially of 36 pins filled with low enriched uranium
dioxide pellets and latterly with 57 pins) were suspended on hanger bars within the pressure tubes.
Force-circulated water was allowed to boil as it passed over the fuel with about 10% being converted
to steam. The steam and water were divided in the water separator/driers located within the steam
drums and then passed forward to the turbine alternator where the two circuits’ outputs were
combined.
Provision was made for a limited degree of superheating in eight separate pressure tubes in the
periphery of the reactor core, but development of fuel for these channels was never completed.
Feed water from the conventional feed plant was delivered to the ends of the steam drums.
MODERATOR AND REACTIVITY CONTROL Whilst some neutron moderation occurred within the light water coolant surrounding the fuel, the
majority of this function was provided by heavy water in a segregated circuit. The heavy water was
kept at near atmospheric pressure and at low temperature and was contained in a calandria through
which the pressure tubes passed.
Short term reactivity control was
achieved by raising and lowering the
level of heavy water in the calandria
and medium-term control was by
changing the concentration of boric
acid in solution. Long term control
was by differential fuel loading.
Reactor shutdown was ensured by
rapid dumping of the heavy water
into storage tanks, but reactor trip
systems triggered valves that
flooded 12 segregated tubes inside
the calandria with lithium borate
solution which shut the nuclear
reaction down within 2 seconds.
TURBINE AND BLED STEAM SYSTEMS The turbine, alternator and feed water systems were basically commercial systems adapted slightly
for the circumstances. The systems varied from those used at the time in coal fired plants in two key
respects: the turbine was designed for saturated steam and much of the feed water plant was
enclosed in concrete cells. These latter cells were required to allow for the likely low-level
contamination of the systems with radioactive material and to shield the normal working areas from
the associated radiation dose rates.
Due to their potentially radioactive content, non-condensable gasses arising in the condenser had to
be removed by electrically driven air pumps before being filtered and discharged to the atmosphere.
4
A feed water polishing plant was provided that treated 100% of the feed flow to limit the level of
impurities. This used powdered ion exchange resin on pre-coated leaves that filtered and treated
the feed water flow.
Two 100% condenser extract pumps and two 50% electrically driven boiler feed pumps were
provided. The feed system included conventional low-pressure and high-pressure feed heaters and
a deaerator tank, but all of these were housed in concrete cells.
REFUELLING The design included the capability for on load refuelling using a carousel arrangement in a large
pressure vessel that could be connected to the primary circuit at the reactor charge face. However,
this system was problematic and was never commissioned. Instead, an off-load system was used
that operated at atmospheric pressure during reactor maintenance outages.
OPERATING EXPERIENCE
The following notes are personal recollections of operation issues and problems associated with the
working of the reactor and its systems. It concentrates on those issues that are associated with it
being a boiling water reactor and does not
explore aspects of the heavy water, pressure
tube or reactor control systems. The
operational problems were common to those
experienced with contemporary boiling water
reactors.
By nature, many of the problems related to
the operation of the systems as a whole, and
cannot be treated in isolation; however, they
are summarized below by plant system, from
steam, through feed water to primary circuit.
STEAM SYSTEMS
Live steam, direct from the reactor primary circuit, came with a significant “load” of nitrogen-16.
This short-lived radionuclide is generated by neutron absorption in oxygen in the primary circuit
water and is carried forward to the turbine in the steam. This was recognized as an issue at the time
of design and a large shield wall was provided between the HP cylinder of the turbine and the
instrumentation area where routine access was needed. The following diagram shows the radiation
dose rates that were generated around the turbine. Whilst this proved successful, there remained
the problem of on-load maintenance of the turbine. Problems with the turbine governor systems or
control valves would either require shutdown or maintenance staff to work in high dose rate areas
to resolve the issues.
Turbine floor during reactor operations
5
Radiation dose rates on the turbine floor
Being a direct cycle plant, with limited steam drying capability (but note superheating proposals
referred to above), steam at the turbine stop valves was wet/saturated. This caused erosion of the
turbine blades which required significant work during reactor outages. If the turbine was not
scheduled for partial dismantling, then the work was in difficult and unpleasant conditions with the
added problems associated with low level radioactive contamination.
Problems in the early operational days with fuel can failures (see below) and “tramp” uranium on
new build fuel assemblies led to the presence of low levels of uranium in the primary circuit. As a
consequence, fission products could be found in the steam circuits. Whilst this caused problems
with maintenance (see below) it could also cause short term airborne issues when there was a plant
steam leak. Whilst, on a conventional plant, a steam leak could be either lived with in the short term
or easily repaired, at SGHWR, the
associated airborne xenon and krypton
would cause operational and radiation
protection issues.
Both activated corrosion products and
longer-lived fission products were carried
forward in the steam systems. This
resulted in contamination of the turbine
and bled-steam systems. Whilst the levels
of radiation and contamination were never
high enough to prevent hands-on
maintenance, they did make the operations
Turbine floor during overhaul
6
more complex. The operations had to be carried out in radiologically controlled areas with
contamination control requirements, exposure control and waste management issues.
Of course, corrosion and erosion products were also carried forward through the feed system and
into the primary circuit where they were exposed to neutron irradiation to become radioactive and
cause further issues as discussed below.
FEED HEATERS These were conventional items of equipment,
but were located in the feed heater cell to
allow for the control of the radiological issues
anticipated. Whilst this was generally
successful, maintenance again was difficult.
Being within a cell, major work (like removing
a heater shell) meant lifting the cell roof on
the turbine floor. Not only did this “break-
through” the normal contamination barrier,
but it could only be done when no
maintenance was being undertaken on the
turbine, as the cell roof was the lay down
area for this latter work. Laying out feed heater shells
The initial material for some of the feed heater tube bundles was found to be excessively prone to
erosion and corrosion resulting in difficulties with primary circuit impurity control. These were
replaced by more appropriate materials in mid-life.
FEED SYSTEM As above, much of the feed system suffered from a degree of erosion and corrosion; all of these
causing problems with primary circuit impurity control. However, as with other boiling water
reactors of the time, extensive use of Stellite as a valve seat material caused particular problems.
Stellite is high in cobalt and any material released into the primary circuit became activated in the
neutron flux as cobalt-60. This became the dominant aspect of radiological protection during the life
of the reactor. Most of the staff exposure was due to this material. Whilst much of the Stellite was
replaced early in the reactor life with other materials, the damage was done and the material is a
significant component of the waste materials even now after 28 years (over 5 half-lives).
Condenser tube failure was a significant threat to the primary circuit conditions and great emphasis
was placed on the response to such events. Major leaks and the associated rise in feed water
conductivity would require a manual reactor trip.
The feed system was a significant source of oxygen ingress. This was a significant contributor to
corrosion and its associated problems. As such, significant efforts had to be made to minimize
ingress and to reduce the dissolved oxygen levels by extensive feed water dosing.
In the plant design, a decision was made to adopt 100% condensate polishing using the Powdex
system (combined filtration and ion exchange). The system allowed the clean-up plant to be placed
7
upstream of the deaerator, rather than at the condenser outlet more typical of conventional ion-
exchange approaches.
The Powdex process is a powdered ion-
exchange resin that is pre-coated onto filter
leaves. Whilst this was generally very
successful, it did generate a significant
volume of radioactive waste. This material
has since been encapsulated in cement in
stainless steel drums and is due to be
disposed of to LLWR this year (2018).
Additionally, the Powdex plant had to be
operated with a significant degree of care.
Any breakthrough of the resin into the feed
system would cause phosphate
contamination which then led to primary
circuit chemistry problems and higher levels of radiation on the turbine systems.
PRIMARY CIRCUIT As noted above, contaminants in the feed water caused, not only materials issues in the
components, but radiological difficulties when it came to maintenance work. Blowdown of the
primary circuit was used to limit the concentrations, but, because of its radioactive content, this
blowdown had to be routed into the feed system rather than to waste. The design discharged the
water into the low-pressure feed system pipework immediately upstream of the polishing plant.
Unfortunately, the design was imperfect, as the flashing of the high temperature blowdown water
caused vibration issues, particularly with the polishing plant itself. Latterly, a blowdown cooler was
installed that resolved this issue.
Impurities in the feed water concentrated in the primary circuit. This plated out in all areas, but
when this occurred on the inside of the pressure tubes and the surface of the fuel, the material
would then become activated in the neutron flux. Subsequently, it became remobilized and resulted
in radioactive contamination of other parts of the primary circuit, steam systems and feed water
pipework. This impurity deposition reached levels in the early stages such that fuel pins were
affected and there were some failures allowing escape of fission products into the primary coolant.
This was addressed both by improved feed water control and by the adoption of a 57-pin fuel
assembly design.
Particular problems arose with the presence of “dead legs” in the primary circuit where radioactive
material would concentrate and form a radiation hot spot.
In common with other light water reactors across the world at the time, trials were undertaken with
primary circuit decontamination techniques in an effort to reduce radiation exposure for the
maintenance workforce. Initial operations used the TURCO process, but this proved too corrosive to
the key primary circuit components and would limit the number of times the process could be
conducted. It was, however, successful in the object of reducing primary circuit radiation dose rates.
Subsequently, UKAEA worked with the Central Electricity Generating Board to develop the Low
Oxidation State Metal Ion (LOMI) process. This less aggressive approach resulted in very good
decontamination performance with acceptable levels of circuit corrosion. This process was later
Powdex unit
8
refined with the use of a pre-treatment phase using nitric acid and potassium permanganate to
enhance the dissolution of chromium. The disadvantages of such systems are the increased volume
of waste generated and the presence of heavy metals in plant effluents. The LOMI process
continues to be used in the nuclear industry.
OPERATIONAL CONTROL OF RADIATION EXPOSURE AND RADIOACTIVE CONTAMINATION The use of a direct cycle approach (combined with a lack of experience in the associated issues) led
to a significantly higher level of radiation exposure to the workforce when compared to a gas cooled
reactor or PWR.
In the early years of operation, radiation protection was not as demanding as it became following
the introduction of the Ionising Radiations Regulations (IRRs). Members of maintenance and
operations staff were exposed to levels of radiation exposure that would today seem
unacceptable. The exposures of some key members of the maintenance team with specific skills
and experience were particularly difficult to manage.
After the introduction of the IRRs, additional efforts were made to reduce exposures and this,
together with growing experience and improved decontamination meant that both individual
and total exposures were
significantly reduced.
Low level contamination of the
steam and water circuits meant that
most maintenance had to be
undertaken in radiologically
controlled areas – over barriers and
with separate active area clothing.
This meant not only low-level
exposure to the workforce, but loss
of time and effort in crossing
barriers etc, the requirement for
monitoring effort and the
generation of amounts of secondary
wastes. In particular, working on feed system, air
pumps, feed heaters etc in enclosed spaces results in a significant loss of efficiency
and makes working areas more cramped and unpleasant.
OTHER OPERATIONAL ISSUES The SGHWR was a very rewarding plant to operate, however, most of the stories about reactor
kinetics, control systems, start-up and shut-down, and steam system dynamics don’t relate directly
to it being a boiling water reactor, but to its use of heavy water as a moderator and the associated
systems. However, the dynamic links between reactor power, steam pressure in the drums and
mechanical governor in the turbine did lead to some interesting excursions when the grid frequency
changed rapidly. Significant changes were made to the automatic control systems to improve
system stablility.
Air pumps cell during maintenance
9
Also notable was the steam void reactivity co-efficient. When the reactor was designed, it was not
known whether or not this co-efficient would be positive or negative and additional mechanisms
were included to allow this to be adjusted. It worked out in practice to be significantly negative – i.e.
the reactor power would fall if the steam generation rate rose, giving negative feedback on most
transients. This was a significant factor in favour of this design over the RBMK pressure tube reactor
of the USSR which has a significantly positive co-efficient – a significant factor in the Chernobyl
accident.
SUMMARY AND CONCLUSION
SGHWR had a number of design and operational shortcomings associated with being a direct cycle
plant; however, it was remarkable that the facility generated successfully for 23 years bearing in
mind the speed and economy of its design and construction.
Around the world, much experience has been gained from operating boiling water reactors of all
types. International collaboration and the embedding of the lessons learnt in the design,
construction and operation of an advanced design has every prospect of providing safe and cost-
effective power for current and future generations.
ABOUT THE AUTHOR
John Lindsay joined the UKAEA at Winfrith in 1983 after gaining a degree in Electrical Engineering at
Nottingham University and spending five years with British Rail. After undergoing three years
training and gaining sufficient plant experience, he was authorized as a Shift Manager. When on
duty, he was responsible for the plant operations and management of the operations team of
operators, supervisors and health physics staff. He remained in this post for the latter years of the
plant’s operations and the first two years post final shutdown.
Once the major hazards (spent fuel and heavy water) were removed from the plant, he left the
UKAEA to join the Nuclear Installations Inspectorate, (now the Office for Nuclear Regulation). After
23 years with the NII/ONR he returned to Winfrith working for Magnox as safety manager for the
decommissioning of the adjacent Dragon high temperature reactor plant.