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TRANSCRIPT
Presentation for 18th National
Award For “Excellence in
Energy Management-2017’’
1
Mangalam Cement Limited belongs to B.K.Birla Group
of Companies. Our first Plant was commissioned in the
year 1981, with an installed capacity of 4 lacs tons of
cement per annum.
Present capacity of cement production is 3.25 MTPA.
2
COMPANY PROFILE
3
COMPANY PROFILEUNIT-I UNIT-II UNIT-III CPP WIND MILL
CRUSHER TO
PACKING PLANT
CRUSHER TO
PACKING PLANT
NEW CEMENT
GRINDING UNIT &
PACKING PLANT
2 X17.5
MW
13 Nos WIND MILLS
OF 13.65 MW CAP.
INSTALLED AT
JAISALMER (RAJ.)
FLS, KILN 3000 TPD
WITH SIX STAGE
PREHEATER, INLINE
CALCINER,SF 12X33
CROSS BAR COOLER,
ATOX VCM and ATOX
VRM.
THYSSENKRIPP, KILN
4000 TPD WITH 5
STAGE PREHEATER,
INLINE CALCINER,
REPOL SR 312-IKN
GRATE COOLER,VCM
and VRM
THYSSENKRUPP,
CEMENT MILL 1.25
MTPA
ABL, CEMENT MILL
WITH VRPM AS
PREGRINDER IN
CLOSED CKT, LNV
SEPARATOR,
CAPACITY 0.8 MTPA.
THYSSENPRUPP
ROLLER PRESS,
CEMENT MILL WITH
ROLL PRESS IN
CLOSED CKT.
CAPACITY 1.2 MTPA
THYSSENKRUPP
ROLLER PRESS,
CEMENT MILL WITH
ROLL PRESS IN
CLOSED CKT.
CAPACITY 1.25 MTPA
4
5
S.No. Year Description of measures Saving in
TOE FY
01 2015-16 Implementation of auto start/stop software logic
in both compressor.26.43
02 2015-16Implementation of software logic in both bag
filter fan (G581FN1 & G581FN3) for auto stop
of bag filter fan.
19.51
03 2015-16 Logic made in PLC for auto start / stop of
heater.
5.34
04 2015-16 Changed loading pressure setting from 6 bar to
5.5 bar and unloading pressure setting from 7
bar to 6.5 bar of all 4 compressors of MGU
packing plant.
97.56
6
S.No. Year Description of measures Saving in
TOE FY
05 2015-16
After optimisation of lighting system 44 Nos
400 watt light fittings were removed from
different towers.
20.73
06 2015-16 Bag house discharge material taken directly to
final air slide via direct chute.
12.57
07
2015-16Bag filter fan inlet damper controlled & tuned
from CCR with fan current to save the power of
fan.
21.94
08
2015-16Electrical consumption reduced by controlling
ESP field current as per dust emission through
stack.
29.52
7
S.No. Year Description of measures Saving in
TOE FY
09 2016-17 Sealed false air from 37.0 % to 23.3 % in Coal Mill-I,
resulted in power saving of power Coal Mill Fan.23.54
10 2016-17 Sealed false air from 56% to 42.5 % in Coal Mill-II,
resulted in power saving of Coal Mill Fan. 32.51
12 2016-17Sealed false air from 28.0 % to 14.2 % in VRM-I
Circuit, resulted in power saving of VRM Fan.67.46
13 2016-17 Improved Power Factor in Kiln-II PCC Incomer 6.6 KV
from 0.85 to 0.95 .8.69
8
S.No. Year Description of measures Saving
in TOE
Investment
in lacs
01 2014-15Kiln-II: Duplex Graphite Lemmela Seal
Installation in place of Pneumatic Seal to
reduce false air entry.
450 13.20
02 2014-15 CM-II: Installation of DD Cones in all the
four Sepol Cyclones to reduce pressure
drop and replacement of double flap valves
by RALs to reduce false air ingress.
37 7.11
03 2014-15 Replacement of push feeder by sector
gate in Cement Mill-2. 9.87 5.00
04 2014-15Removal of two belt conveyors from LS
feeding circuit of VRM-1 by providing direct
chute to hopper.
35.62 0.50
9
S.No. Year Description of measures Saving
in TOE
Investment
in lacs
05 2014-15
Installation of de dusting cones (DD
cones ) in LNVT separator of VRPM and
both the cyclones of SEPOL separators in
Cement Mill-1.
58.92
2.20
06 2014-15 Installation of de dusting (DD) cone in
dynamic separator of VRM -1.92.79 1.75
07 2015-16
Made a Dam of height 800 mm in TAD to
restrict Tertiary Air flow rate and to reduce
excess air in secondary firing from 20 % to
10 %.
102.21 5.00
08 2015-16
Removed Silencers from all the cooler
fans to reduce the pressure drop ranging
from 60-150mmWG in all cooler fans of
KILN-1.
141.14 0.05
10
S.No. Year Description of measures Saving
in TOE
Investment
in lacs
09 2015-16 Filler material feeding arrangement by PS
pump in place of dense phase.105.26 1.00
10 2015-16Enlargement of Cooler Exhaust Duct Area
from 4.91 m2 to 9.62 m2 to reduce dust
loading in ESP KILN-2.
12.45 1.20
11 2015-16Enlargement of Preheater Down comer
Duct from 5.72 m2 to 10.00 m2 IN KILN-2.168.41
23.35
12 2015-16 Increase of Calciner Length from 48.0
meter to 64.0 meter IN KILN-2.194.63 66.12
11
S.No. Year Description of measures Saving
in TOE
Investment
in lacs
13 2015-16
Increase in cross section area of Tertiary
Air Duct (TAD) from 1.61 m2 to 3.36 m2
in KILN-2.
1550.27 42.55
14 2015-16
Enlargement of Smoke Chamber Area
from 4.74 m2 to 6.51 m2 in KILN-2. 62.33 4.09
15 2015-16
Increase of Inlet Duct Area of Bottom
Cyclone from 9.92 m2 to 13.03 m2 in
KILN-2
.
37.98 5.00
16 2015-16 Enlargement of Take off Duct Area from
5.58 m2 to 8.20 m2 in KILN-2.
19.21 9.15
12
S.No. Year Description of measures Saving in
TOE FY
Investment
in lacs
17 2015-16
Replacement of Kiln Inlet Seal from
Pneumatic Seal to Graphite Seal in
KILN-1.
165.31 5.00
18 2015-16
Replacement of belt conveyor
501BC3 & fixing of DPC of 150TPH
in KILN-1.
77.05 44.60
19 2015-16
Through modification of discharge
chute of 903BC5 lime stone fed in
hopper directly without running of
961BC1 and 961BC2 belts in KILN-
1.
50.73 7.78
20 2015-16Installation of auto delta to star
starter in G501BC6 & BC7
conveyor belts drives.
9.76 0.01
13
S.No. Year Description of measures Saving in
TOE FY
Investment
in lacs
21 2016-17
Reducing the preheater exit oxygen
from the level of 7% to 4% for
Kiln-I by restricting excess air flow
through TAD.
301.95 10.00
22 2016-17
Reduced the pressure drop through
modification in the separator fan
inlet duct of Cement Mill-3.
58.5220.00
23 2016-17 Installed VFD for 975BL1 (132kw)
root blower in KILN-1.21.28 8.00
24 2016-17 Installed VFD for 212FN2 (75kw) BF
fan in crusher section.22.04 5.00
25 2016-17 Replacement of chain type elevator
150 TPH by belt bucket elevator of
250 TPH in KILN-1.
85.12 30.00
14
15
85.61
82.55
78.23
80.74
78.27
75.44 74.73
73
78
83
88
2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
kwh/ton of cement
*
* Unit-I, Plant shutdown for Rehabilitation work
16
869860
803
716 709699
760 765 764
755 748738
798781
773
739731
720
680
720
760
800
840
880
2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
THERMAL SEC (GCV BASED)
KILN-I
COMBINED
KILN-II
National
Benchmark
International
Benchmark
Mangalam
Cement Limited
Specific Energy
Consumption Thermal
(Kcal/kg of clinker) (GCV
BASED )
680 650
KILN-I 699
KLIN-II 738
COMBINED 720
Specific Energy
Consumption Electrical
kWh/T of cement (Actual)
(100% PPC)
68 65
66.55
(ON PPC ONLY)
(YEAR 2016-17)
17
LOW DUE TO CABLE
THEFT PROBLEM
18
6.20%
8.30%
11.50%
10.20%
7.60%
8.90% 8.56%9.32%
4.00%
6.00%
8.00%
10.00%
12.00%
2009-10 2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
% OF WIND MILL POWER IN TOTAL POWER CONSUMPTION OF PLANT
Wind Power for Captive Use 2016-17 = 163.6 Lacs Units
So Saving in Mkcal = 53194.54 Mkcal
Saving in TOE = 5319.45 TOE
19
15.35%
26.05%
27.47%
31.11% 30.57% 31.08%
10.00%
15.00%
20.00%
25.00%
30.00%
35.00%
2007-10 2012-13 2013-14 2014-15 2015-16 2016-17
FLY ASH CONSUMPTION IN %
20
RE
DU
CT
ION
CO
2 E
MIS
SIO
N
Kg
/Kg
PP
CC
EM
EN
T
CO
2R
ed
uc
tio
n in
to
n
CO2 REDUCTION DUE TO HIGHER CONSUMPTION OF FLY ASH
IN PPC WITH REFERENCE TO 2011-12
18004
33551
66421
78055
15495
0.56000.5500
0.50640.4973
0.4962
0
10000
20000
30000
40000
50000
60000
70000
80000
90000
0.46
0.48
0.50
0.52
0.54
0.56
0.58
2012-13 2013-14 2014-15 2015-16 2016-17
CO2 Reduction in Tonne CO2 Emission, Kg/Kg Cement
Highest ever PPC Production
Less reduction due to less PPC
Production.
21
16.90%
18.10%
12.50%
10.20% 10.50%9.50% 9.56% 9.33%
6.00%
8.00%
10.00%
12.00%
14.00%
16.00%
18.00%
20.00%
2009-10 2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
PETCOKE CONSUMPTION IN % OF CLINKER PRODUCTION
85 % PETCOKE &
15 % INDIAN
COAL USED
57% PETCOKE &
43 % INDIAN
COAL USED
100% INDIAN
COAL USED
100% INDIAN
COAL USED
100% PETCOKE
USED100% PETCOKE
USED
100% PETCOKE
USED96.4% PETCOKE ,
1.4 % INDIAN COAL
& 2.2 % US COAL
USED
22
16.14%
17.01%
10.80%10.22%
13.45%
9.40% 7.95%9.02%
7.00%
9.00%
11.00%
13.00%
15.00%
17.00%
19.00%
2009-10 2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
BY USING PETCOKE REDUCTION IN % HGLS CONSUMPTION
23
SR.
NO
MEASURES TAKEN FOR
CO2 REDUCTION
2012-13 2013-14 2014-15 2015-16 2016-17
1. DUE TO REDUCTION IN
SPECIFIC HEAT AND
POWER CONSUMPTION
OF CLINKER W.R.T.
YEAR 2011-12
4123 14798 49101 48202 59003
2. DUE TO HIGHER USE
OF FLY ASH IN PPC
PRODUCTION W.R.T.
YEAR 2011-12
18004 33551 66421 78055 15495
3. DUE TO USE OF GREEN
POWER (WIND MILL
POWER FOR CAPTIVE
USE)
20367 13960 20477 17524 19638
TOTAL 42494 62309 135999 143781 94136
24
SR.N
O
MEASURES TAKEN FOR CO2
REDUCTION 2015-16 2016-17
1. BY NOT USING VEHICLES ON EVERY
MONDAY WHILE COMING TO OFFICE2.477 2.821
2. BY REDUCING SP HEAT RATE IN CPP27155 37677
TOTAL 27157 37680
26
27
11715 10432
30047
114868926 10063
2831
0
5000
10000
15000
20000
25000
30000
35000
2011 2012 2013 2014 2015 2016 2017(JAN-JULY)
GREEN BET DEVELOPMENT -YEAR WISE
GREEN BELT DEVELOPMENT
(PLANT, COLONY & MINES)
TOTAL PLANTATION 243967 (1991 TO July 2017)
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MANGALAM CEMENT LIMITED
REVIEW STATUS OF DEPARTMENTAL OBJECTIVES (Frequency - Monthly)
FORMAT NO. : F02-4460
UNIT : DEPT :
REV : No : VER : No : Date :
Obj No. Objective
Baseline Status Desired StatusFinal Target
Date
MONTHWISE STATUS
2015-16 2016-17 APR-16 TO MAR-17 YTD
Prepared By Approved By :
Checked By
31
32
33
ENCON EFFORTS PLANNED FOR THE NEXT THREE YEARS
34
Sr.
No
Description of projects Investment
Rs
Expected saving
1Installation of WHR in KILN I & II of 8.5MW & expected generation (net) is 545lacs units /year.
Rs 63 CRORES
Thermal energy saving17493 TOE
2Upgradation of KILN II by modifyingpreheater from 5 stage to 6 stage andupgradation of cooler
RS 15 CRORES
40 kcal/kg of clinker
3 Modification in UNIT -II CEMENT MILL V-separator material feeding system for increase in output & reduction in specific power consumption
20.16 LACS 8.88 LACS KWH
4 Modification in lime stone feeding system of VRM -I 10 LACS 3.15 LACS KWH
5 Reduction in plant lighting consumption by using of high efficient led lights in place of conventional lights.
23.3 LACS 10.10 LACS KWH
35
36
National Safety Award (Mines) 2011 – “ON LOWEST
INJURY FREQUENCY RATE” in the category of Highly
Mechanized Opencast Mines was given by the President of India in association with
Minister of Labour & Employment (Government of India) at Vigyan Bhawan- New
Delhi.
37
CFBP (Council of Fair Business Practices) Jamanalal
Bajaj Uchit Vyavahar Puraskar for Fair Business Practices
in Manufacturing Enterprises – SME category for the year
2014 was received from Hon’ble Former President of India
late Dr. A.P.J. Abdul Kalam .
38
Rajasthan Energy Conservation award - 2014
Was given by Honorable Energy Minister of Rajasthan.
39
National Award For “Excellence in Energy Management -
2015’ from CIIThis National award is given in recognition of Excellence in Energy
management in cement sector by CII. Award was given by chairman
Bureau of Energy Efficiency (BEE) Dr.Ajay Mathur on 3rd September
2015 at Hyderabad.
40
Productivity Award 2013 - 2014 from Rajasthan State
Productivity Council.This award is given in recognition of “ Improvement in Productivity
Performance” by Rajasthan State Productivity council . Award was
given by Honorable Minister for Industries Govt. of Rajasthan Shri
Gajendra Singh on 30th September-2015.
41
Energy Conservation Merit award – 2015 from Rajasthan
State Government.This award is given in recognition of Energy Conservation in Cement
Sector by Govt. of Rajasthan. Award was given by Energy Secretary of
Rajasthan state Govt. Shri Sanjay Malhotra on 14th December-2015.
42
National Energy Conservation Merit Award 2015 by
Ministry of Power – Government of India.This award is given in recognition of Energy Conservation for Cement
Sector. Award was given by chairman Bureau of Energy Efficiency
(BEE) Dr.Ajay Mathur on 22nd January 2016.
43
Award for outstanding Performance in Rural
Development by Employer Association of Rajasthan for
the Year 2014-15.This award is given in recognition for outstanding Performance in rural
development work by Employer Association of Rajasthan. Award was
given by Honorable Minister for Higher Education Shri Kalicharan
Sarraf on 25th Feb 2016 at Jaipur.
44
26th MINES ENVIRONMENT & MINERAL CONSERVATION AWARDS 2015-16
(Under the aegis of Indian Bureau of Mines, Ajmer Region)
Ist prize in the field of
“ TOP SOIL MANAGEMENT”.
45
26th MINES ENVIRONMENT & MINERAL CONSERVATION AWARDS 2015-16
(Under the aegis of Indian Bureau of Mines, Ajmer Region)
IInd prize in the field of
“ AFFORESTATION”.
46
Rajasthan Energy Conservation Award – 2016
Ist prize in Large Cement Sector of Rajasthan”.This award is given in recognition of Energy Conservation in Cement
Sector by Govt of Rajasthan. Award was given by Energy Secretary of
Rajasthan state Govt Shri Sanjay Malhotra on 14th December-2016.
47
Four Star Award to Morak Limestone Mines of M/s Mangalam
Cement Ltd. for Sustainable Development by Ministry of Mines
, Govt. of India at National Mineral Conclave -2016 at Raipur
Star Award Sustainable Development by Ministry of Mines ,
Govt. of India at National Mineral Conclave -2016
48
Award for outstanding Performance in Rural Development by
Employer Association of Rajasthan for the Year 2016-2017
This award is given in recognition for outstanding Performance in
rural development work by Employer Association of Rajasthan.
Award was given by Honorable State Finance Minister Shri Arjun
Ram Meghwal .
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Thank You
All